Crash of a Dassault Falcon 20DC in Boise

Date & Time: Nov 27, 1999 at 0134 LT
Type of aircraft:
Operator:
Registration:
N216SA
Flight Type:
Survivors:
Yes
Schedule:
Omaha - Boise
MSN:
16
YOM:
1966
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
19519
Captain / Total hours on type:
341.00
Aircraft flight hours:
28855
Circumstances:
After extending the gear for landing, the down-and-locked indication (green light) for the left main gear was not illuminated. The crew performed the emergency checklist procedures for abnormal gear extension with no success. The aircraft subsequently landed with the left main landing gear retracted. Inspection of the landing gear revealed that the pin (part number MY20248-001), which is part of the forward gear door lock, was corroded and cracked at the point of rotation, preventing proper movement of the gear door uplock.
Probable cause:
Failure of the forward gear door lock pin. An inoperative landing gear door and inadequate maintenance inspection of the aircraft were factors.
Final Report:

Crash of a Cessna T303 Crusader in Midvale: 6 killed

Date & Time: Mar 2, 1998 at 1805 LT
Type of aircraft:
Registration:
N727RT
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Boise - Boise
MSN:
303-00090
YOM:
1981
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
7743
Captain / Total hours on type:
319.00
Aircraft flight hours:
1675
Circumstances:
Radar data indicated that the aircraft completed a figure-eight maneuver at about 3,000 feet AGL, with an estimated airspeed of 140 knots and approximate 40 degree bank angle before leveling out at the completion of the maneuver. The radar data then indicated level flight before a rapid descent. A witness reported observing the aircraft in visual conditions and flying at a high altitude and that it 'appeared fast.' The witness stated that he observed the aircraft make a wide, shallow left turn, then turn back the other way. The nose of the aircraft then started to gradually lower, and the airplane eventually came straight down and started to spin. The witness lost sight of the airplane behind hilly terrain and he did not see the impact. Postaccident examination of the wreckage indicated that the aircraft collided with the terrain in a slight nose-down attitude, located in a gully with approximate 30 degree bank angle. The aircraft then slid downhill to the right and came to rest with the fuselage upright and the empennage was twisted to the right and inverted. No evidence was found to indicate a mechanical failure or malfunction.
Probable cause:
The pilot's failure to maintain aircraft control.
Final Report:

Crash of a Douglas C-47A-1-DL in Boise: 2 killed

Date & Time: Dec 9, 1996 at 1803 LT
Operator:
Registration:
N75142
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Boise – Salt Lake City
MSN:
9173
YOM:
1943
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
15447
Captain / Total hours on type:
5502.00
Aircraft flight hours:
34124
Circumstances:
The DC-3C took off on runway 10L and immediately executed a right turn followed by a left turn back toward the airport declaring a fire aboard. Dark night visual meteorological conditions existed. Witnesses observed 'flames' or an 'orange glow' coming from the right engine. A small number of aluminum fragments identified from the aft edge of the right engine accessory cowling were found along the ground just short of the ground impact site. These fragments displayed signs of heat distress but no significant melting. An examination of the right engine and accessory section revealed no evidence of a preimpact fire, and sooting and metal splatter on the leading edge of the right horizontal stabilizer was minimal. Spectral analysis of radio transmissions revealed no evidence of significant divergence of engine RPM between the two engines. Postcrash propeller examination revealed approximate blade pitch angles of 18-19° and 30-32° for the right and left propellers respectively upon impact. Propeller slash mark dimensions associated with the right propeller resulted in propeller RPM of approximately 1,750 to 2,570 over a range of 68 to 100 knots respectively. The first officer advised the PIC (broadcasting over the tower frequency) 'we're gonna stall' approximately 10 seconds before the impact. The aircraft was in a left turn back toward runways 28 left and right when the right wing struck the ground and the aircraft cartwheeled to a stop. A postcrash fire destroyed the cockpit area and inboard right wing.
Probable cause:
A fire within the right engine compartment of undetermined cause and the pilot-in-command's failure to maintain airspeed above the aircraft's minimum control speed. A factor contributing to the accident was the dark night environmental conditions.
Final Report:

Crash of a Mitsubishi MU-2B-36 Marquise in Malad City: 8 killed

Date & Time: Jan 15, 1996 at 0618 LT
Type of aircraft:
Registration:
N693PA
Flight Phase:
Survivors:
No
Schedule:
Salt Lake City - Pocatello
MSN:
693
YOM:
1977
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
8
Captain / Total flying hours:
8925
Captain / Total hours on type:
1200.00
Circumstances:
A Mitsubishi MU-2 departed Salt Lake City, Utah, and climbed to 16,000 feet MS on an IFR flight to Pocatello, Idaho. While in cruise flight, the MU-2 encountered structural icing conditions. According to radar data, the MU-2 began slowing from a cruise speed of about 190 knots with slight deviations from heading and altitude. The airspeed decreased to about 100 knots, and the flight crew declared an unspecified emergency, then radio contact was lost. The MU-2 began a right turn, then it entered a steep descent and crashed. The pilot of a Beech 1900 (about 12 minutes in trail of the MU-2), stated that he encountered moderate rime icing at 16,000 feet. The Beech pilot activated his deice boots (3 times) and descended to 12,000 feet to exit the icing conditions. The MU-2 flight manual warned that during flight in icing conditions, stall warning devices may not be accurate and should not be relied upon; and to minimize ice accumulation, maintain a minimum cruise speed of 180 knots or exit the icing conditions. An investigation determined that the captain of the MU-2 was aware of deficiencies in the timer for the deice boots, as well as other maintenance deficiencies. The captain's medical certificate was dated 11/17/94; he was providing executive transportation for compensation under an agreement for "contractual flights," under 14 CFR 91. Although icing conditions were forecast in the destination area, no icing was forecast for the en route portion of the flight.
Probable cause:
Continued flight by the flightcrew into icing conditions with known faulty deice equipment; structural (airframe) ice; and failure of the flight crew to maintain adequate airspeed, which resulted in the loss of aircraft control and collision with terrain. A factor relating to the accident was: the en route weather (icing) condition, which was not forecast (inaccurate forecast).
Final Report:

Crash of a Rockwell Aero Commander 560 in Ketchum: 2 killed

Date & Time: Sep 8, 1995 at 1310 LT
Operator:
Registration:
N731R
Flight Type:
Survivors:
No
Schedule:
Elko - Hailey
MSN:
560-0219
YOM:
1955
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3400
Circumstances:
The aircraft was VFR inbound to the Hailey airport when the pilot contacted the tower at 1247 and reported 10 miles south. During the next 7 minutes the pilot and controller communicated back and forth and the pilot never visually acquired the airport. A number of witnesses located north of the airport observed the aircraft flying northbound along the highway into upsloping, mountainous terrain at an estimated altitude of 400 feet above ground, and with the landing gear extended and the engines developing power. The aircraft was described as low and slow and was observed to dip its wings during a left turn and then descend steeply to the ground. The aircraft impacted terrain in a steep nose down attitude. There was no evidence of flight control or powerplant malfunctions. High density altitude conditions existed at the accident site. Toxicological examination revealed a finding of 0.068 ug/ml and 0.183 ug/ml of Chlorpheniramine (an over-the-counter antihistamine) in kidney and heart tissue respectively.
Probable cause:
The pilot-in-command's failure to maintain adequate airspeed during a turn resulting in a stall/spin. Factors contributing to the accident were the pilot-in-command's becoming geographically disoriented as well as his improper in-flight decision, and mountainous terrain.
Final Report:

Crash of a Lockheed C-130E Hercules near Bliss: 6 killed

Date & Time: May 13, 1995
Type of aircraft:
Operator:
Registration:
62-1838
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Boise - Colorado Springs
MSN:
3801
YOM:
1963
Flight number:
Sumit 38
Location:
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
After departure from Boise-Gowen Field, en route to Peterson AFB in Colorado Springs, the crew encountered technical problems with the engine n°2. The crew declared an emergency and elected to divert to Mountain Home AFB. About 20 minutes into the flight, the engine n°2 compressor disintegrated. The aircraft entered an uncontrolled descent and crashed 12 miles north of Bliss. All six crew members were killed.
Crew:
Lt Col Robert Buckout, Commander
1st Lt Lance Daugherty, pilot,
Cpt Geoffery Boyd, navigator,
CMSgt Jimmy Vail, flight engineer,
M/Sgt Jay Kemp, loadmaster,
S/Sgt Michael Scheideman, loadmaster.
Probable cause:
The cause of the crash was that the number 2 (inside left wing) engine had a buggy undertemp sensor, causing the crew to enrich the fuel mixture, leading to an actual engine overtemp. One of the fuel lines ruptured or melted, causing the fire, and one of the crewmen hit the fire carts, but the fire re-erupted moments later, and there were no more extinguishers available for that engine. One of the pins that was supposed to melt in an engine fire, releasing the engine from the AC, failed to release the engine properly, while another worked properly. Still half connected to the wing hard point, the engine torqued at an awkward angle, causing severe wing and fuselage damage, which led to the crash.

Crash of a Piper PA-46-310P Malibu in Mountain Home: 1 killed

Date & Time: Nov 22, 1993 at 0111 LT
Registration:
N84PM
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Twin Falls - Boise
MSN:
46-8408004
YOM:
1984
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1915
Captain / Total hours on type:
457.00
Circumstances:
The pilot had been charged with 'lewd and lascivious conduct with a minor.' He was jailed on Friday and released on bond on Saturday. During a meeting with a friend in the pilot's car on Sunday evening, he was drinking beer. The friend said the pilot made comments referring to intentionally crashing the aircraft and that 'he didn't want to die, but didn't know of any other way.' He had a gun in the car and told the friend 'don't call the police or I'll kill myself sooner.' The pilot departed Twin Falls at about 2230 on Sunday night in his PA-46. He flew to Boise, ID (via Ely, NV) before turning back toward Twin Falls. After passing over Boise, intermittent radio contact was made between the airplane and approach control. Radar vectors and descent were issued. Radar contact was lost during descent and pilot announced descending thru 11,000 feet; 38 seconds later, he reported at 6,000 feet. Ground impact was at 4,650 feet. Toxicology tests of the pilot's lung and muscle tissue showed an alcohol level of 175 & 117 mg/dl (0.175% & 0.117%). No preimpact failure of the aircraft was found.
Probable cause:
The pilot's intentional suicide and impairment from consumption of alcohol.
Final Report:

Crash of a Dassault Falcon 10 in Hailey

Date & Time: Aug 26, 1993 at 1430 LT
Type of aircraft:
Operator:
Registration:
F-BYCV
Flight Type:
Survivors:
Yes
Schedule:
Saskatoon – Great Falls – Hailey
MSN:
93
YOM:
1976
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3440
Captain / Total hours on type:
40.00
Aircraft flight hours:
8607
Circumstances:
Because of the failure of the thrust reverser relay circuit board, the thrust reversers failed to deploy when selected by the pilot. Because the reversers failed to deploy, the 'reversers in transition' lights, and the 'reversers deployed' lights did not illuminate. Even though the aircraft flight manual warns against moving the reverser throttle levers into the power range without the illumination of these lights, the pilot did so anyway. The pilot continued to select reverse power even after the activation of the throttle mismatch warning horn, resulting in an increase in forward thrust while attempting to stop. During this sequence of events the second-in-command moved the parking brake lever to full override, locking the main wheel brakes and overriding the antiskid system.
Probable cause:
The pilot-in-command's improper procedures. Factors include failure of an electrical relay, inoperative thrust reverser, poor crew coordination, and the second-in-command's improper procedures.
Final Report:

Crash of a Convair CV-240 in Boise

Date & Time: Jul 27, 1993 at 1317 LT
Type of aircraft:
Registration:
N156PA
Flight Type:
Survivors:
Yes
Schedule:
Boise - Boise
MSN:
324
YOM:
1953
Location:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2128
Captain / Total hours on type:
1400.00
Copilot / Total hours on type:
1
Circumstances:
Left seat pilot was receiving a flight check for ATP and CV-240 type rating; right seat pilot was FAA OPS inspector. Following a simulated single-engine approach the airplane landed wheels up. Left seat pilot had received a total of 1.4 hrs left seat training in CV-240 prior to this flight; log book not endorsed.
Probable cause:
The pilot's failure to extend the landing gear, and the check pilot's inadequate supervision. A factor in the accident was the pilot's inadequate upgrade training by the company.
Final Report:

Crash of a Beechcraft B60 Duke in Fairfield

Date & Time: Jul 16, 1993 at 1405 LT
Type of aircraft:
Registration:
N75CX
Survivors:
Yes
Schedule:
Hermiston – Fairfield
MSN:
P-337
YOM:
1975
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1062
Captain / Total hours on type:
363.00
Aircraft flight hours:
2256
Circumstances:
On Friday afternoon, July 16, 1993, at 1405 mountain daylight time, a Beech B-60, N75CX, registered to the pilot, overran the end of the runway and impacted terrain while landing at the Camas County Airport, Fairfield, Idaho. An IFR flight plan was filed for the business flight, conducted under 14 CFR 91, which departed Hermiston, Oregon at 1244, July 16, 1993. Visual meteorological conditions prevailed in the area. The private certificated pilot and passenger Peter W. VanKomen were seriously injured. Passenger Chris A. Carrow suffered minor injuries in the accident. The aircraft was destroyed in the mishap. There was no fire. Witnesses reported the pilot landed on runway 7, near the center of the 2950 feet long gravel airstrip and was unable to stop on the runway. The aircraft skidded off the east end of the runway where it impacted a ditch and dirt embankment. The Camas County Sheriff reported he examined the aircraft tire marks on the runway, which according to his measurement, started 1400 feet from the west end of the runway (See Sheriff Report). The sheriff indicated in his report that a witness, Bill Simon, stated in an interview that the pilot landed in downwind conditions, estimated to be 15 to 20 knots. Witness David Coffin, a private pilot, reported the two wind socks on the strip were fully extended, indicating the wind was blowing from west to east at a velocity in excess of 25 MPH, and gusting 30 to 35 MPH. The surface aviation weather observation, taken at Hailey, Idaho, 24 miles northeast of the accident site at 1350 MDT, July 16, 1993, was recorded as 3000 feet scattered clouds, visibility 30 miles, temperature 65 degrees F., dew point 29 degrees F., wind 210 degrees at 10 knots and altimeter 30.05 inches Hg. The density altitude at the Camas County Airport was calculated to be 6488 feet. The airport facility directory indicates the Camas County Airport has a single 2950 by 40 feet dirt runway, oriented 070 and 250 degrees. The elevation at the airport is 5058 feet above mean sea level.
Probable cause:
The pilot's improper inflt planning/decision in selecting the wrong runway for landing. A factor relating to the accident was the strong tailwind weather conditions.
Final Report: