Crash of a Beechcraft D18S in Fort Collins

Date & Time: Nov 30, 1995 at 1330 LT
Type of aircraft:
Operator:
Registration:
N8603A
Flight Type:
Survivors:
Yes
Schedule:
Fort Collins - Fort Collins
MSN:
A-557
YOM:
1951
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7000
Captain / Total hours on type:
800.00
Circumstances:
The pilot-owner/operator, who was seated in the right seat, said the left seat pilot made the approach to runway 15. The wind was reported as being from the southwest at 20 knots with no reference to gusts. He said the pilot aligned the airplane 40 feet left of runway centerline and failed to flare. The airplane contacted the runway, bounced back into the air with the right wing high, and began drifting to the left. The right seat pilot took control, first trying to lower the wing then attempting to abort the landing. The airplane struck the ground and cartwheeled. The left seat pilot said he was 'receiving training' from the pilot-owner and was 'not at the controls' at the time of the accident.
Probable cause:
The second pilot's failure to compensate for wind conditions and his improper recovery from a bounced landing, and the pilot-in-command's inadequate supervision of the flight. Factors were the second pilot's lack of landing experience in the airplane make/model, and the gusty crosswind conditions.
Final Report:

Crash of a Rockwell Gulfstream 690C Jetprop 840 in Golden: 1 killed

Date & Time: Dec 22, 1992 at 2022 LT
Operator:
Registration:
N81TR
Flight Type:
Survivors:
No
Site:
Schedule:
Rifle - Denver
MSN:
690-11690
YOM:
1981
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
5400
Captain / Total hours on type:
910.00
Aircraft flight hours:
7768
Circumstances:
While in a descent for arrival at the destination airport, the aircraft sustained structural failure with the right outer wing, horizontal stabilizer, and vertical stabilizer separating from the aircraft. The aircraft impacted approximately 10 miles from the planned destination. According to radar data and other research, the descent was conducted at vne and known severe turbulence was present in the area at the time of the accident.
Probable cause:
The pilot flying the aircraft beyond the design maneuvering speed and exceeding the design stress limits. A factor was: clear air turbulence.
Final Report:

Crash of a Mitsubishi MU-2B-25 Marquise in Broomfield

Date & Time: Nov 20, 1992 at 1840 LT
Type of aircraft:
Operator:
Registration:
N473FW
Flight Phase:
Survivors:
Yes
Schedule:
Broomfield - Las Vegas
MSN:
269
YOM:
1973
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
13753
Captain / Total hours on type:
4200.00
Aircraft flight hours:
3406
Circumstances:
In preparation for a cross country flight with takeoff occurring during a snow storm, the aircraft was loaded in the hangar and towed out by fbo personnel. Following the tow, the torque link was not properly connected and separated during the takeoff run. Due to a loss of nose wheel steering, the takeoff was aborted. The aircraft departed the side of the runway during the abort and the nose wheel was sheared off causing damage to both engines, wings, the fuselage, and landing gear. All four occupants escaped uninjured.
Probable cause:
A failure by FBO personnel to properly connect the nose wheel torque link after towing the aircraft.
Final Report:

Crash of a Piper PA-42 Cheyenne III in Grand Junction: 3 killed

Date & Time: Oct 31, 1992 at 0815 LT
Type of aircraft:
Operator:
Registration:
N250TJ
Survivors:
No
Schedule:
Moab - Grand Junction
MSN:
42-8001024
YOM:
1980
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
4700
Aircraft flight hours:
4784
Circumstances:
The commuter air carrier departed Moab, Utah, and flew to Grand Junction, CO, via rnav direct Macks intersection. After crossing macks intersection, the airplane turned right but instead of intercepting the localizer course, the airplane continued on a slightly divergent track to the east of the localizer. The pilot told control tower personnel, 'I'm showing twelve miles out on the ILS...getting real...erroneous signal, here. Any complaints?' the pilot was advised no difficulty reports had been received. The airplane impacted a mesa one minute later about five miles to the left of the localizer course. The cockpit was destroyed and no meaningful information was obtained from the navigational radios. All of the airport's navigational aids were later flight checked and no discrepancies were found. Although Vmc prevailed at the airport, the accident site was above the reported ceiling height. All three occupants were killed.
Probable cause:
Improper ifr procedure and resultant disorientation which resulted in a collision with terrain.
Final Report:

Crash of a Mitsubishi MU-2B-60 Marquise near New Castle: 6 killed

Date & Time: Mar 5, 1992 at 1002 LT
Type of aircraft:
Registration:
N303CA
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Fort Worth – Rifle
MSN:
1518
YOM:
1981
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
1265
Captain / Total hours on type:
154.00
Circumstances:
The airplane impacted mountainous terrain approximately 10.5 dme from the airport while executing a LOC/DME instrument approach. The airplane was configured for landing. The elevator trim jackscrew was approximately 18° nose up. The altitude preselect, coupled to the sperry autopilot system, was set at 9,500 feet. Minimum descent altitude until reaching the final approach fix is 9,500 feet. Final approach fix is located at 9.3 dme. Twenty four prescription and nonprescription drugs were found aboard the airplane. The pilot's toxicology report disclosed 0.206 (ug/ml, ug/g) chlorpheniramine, an antihistamine, in his liver fluid. According to an FAA flight surgeon, this would equate to approximately .034 ug/ml in blood. Therapeutic dosage is .01 to .04 ug/ml. The drug is contraindicated for flying due to its capability of producing drowsiness. Chlorpheniramine is an ingredient found in comtrex, one of the drugs found aboard the airplane. All six occupants were killed.
Probable cause:
An inadvertent stall during an instrument approach with the autopilot engaged. A factor was: the pilot's physical impairment from a prescription drug.
Final Report:

Crash of a Swearingen SA26T Merlin II in Glenwood Springs

Date & Time: Feb 13, 1992 at 2055 LT
Type of aircraft:
Registration:
N26JB
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
Schedule:
Grand Junction - Denver
MSN:
T26-163
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8600
Captain / Total hours on type:
750.00
Aircraft flight hours:
3988
Circumstances:
The pilot of the air ambulance feathered the right propeller after reporting 'a bit of a problem' with the right engine. He attempted to divert to the nearest suitable airport, but after receiving its latest weather report, elected to return to base. The airplane made a left turn, reentered IMC, and impacted a mountainside on a magnetic heading of 092°. The heading to the airport of intended landing was 272°. The accident occurred during a snowstorm at night. All five occupants survived and were rescued the following afternoon. Thick grease on the right engine fuel control camshaft prevented a spring from returning the 3d cam to a lower altitude position. The cam was found struck on the shaft at a position equating to an altitude of approximately 15,000 feet. The fuel flow schedule for flight idle was below specifications. In addition, shroud material was found delaminated from the left engine second stage compressor housing.
Probable cause:
Malfunction of the right engine fuel control that caused the engine to flame out, and delamination of the left engine compressor shroud. Factors were: the pilot became disoriented, the mountainous terrain, the dark night, and the weather conditions.
Final Report: