Crash of a Grumman G-21A Goose off Avalon: 1 killed

Date & Time: Sep 17, 1979 at 1715 LT
Type of aircraft:
Operator:
Registration:
N22932
Flight Phase:
Survivors:
Yes
Schedule:
Avalon - San Pedro
MSN:
B139
YOM:
1945
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
13300
Captain / Total hours on type:
4000.00
Circumstances:
After takeoff from the bay of Avalon, the twin engine seaplane lost height and crashed into the sea. A passenger was killed while three other occupants were injured, the pilot seriously.
Probable cause:
Airframe failure during initial climb after the elevator tab control system failed. The following contributing factors were reported:
- Inadequate maintenance and inspection,
- Fatigue fracture,
- Up elevator cable separated 3 to 4 feet forward of station 29.
Final Report:

Crash of a Douglas DC-7CF in Barstow: 1 killed

Date & Time: Jun 22, 1979 at 2012 LT
Type of aircraft:
Registration:
N357AL
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
45229/904
YOM:
1957
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
Just after liftoff from Barstow-Daggett Airport, both engines n°3 and 4 lost power. The crew attempted an emergency landing when the airplane lost height and crashed in flames in an open field. A pilot was killed while five other occupants were injured. The aircraft was destroyed by a post crash fire. Illegal smuggling flight.
Probable cause:
Engine malfunction during initial climb due to inadequate preflight preparation. The following contributing factors were reported:
- Improper fuel grade,
- Improperly loaded aircraft, CofG,
- Failed to abort takeoff,
- Partial loss of power on two engines,
- Forced landing off airport on land,
- 2,981 lbs over maximum gross weight,
- N°3 & 4 engines showed severe detonation damages,
- Fueled with 100 octane,
- Smuggling flight.
Final Report:

Crash of a Grumman G-21A Goose off Avalon: 1 killed

Date & Time: Apr 14, 1979 at 1007 LT
Type of aircraft:
Operator:
Registration:
N11CS
Survivors:
Yes
Schedule:
San Pedro - Avalon
MSN:
1166
YOM:
1942
Crew on board:
1
Crew fatalities:
Pax on board:
10
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
9335
Captain / Total hours on type:
455.00
Circumstances:
On approach to Avalon (Santa Catalina Island) in marginal weather conditions with low clouds and fog, the pilot decided to initiate a go-around after noticing boat wakes. Doing so, the seaplane stalled, lost height and crashed into the sea few hundred yards off Pebbly Beach. The pilot and two passengers were seriously injured while seven other occupants escaped with minor injuries. A passenger drowned.
Probable cause:
Stall during a go-around after the pilot misjudged distance, speed and altitude. The following contributing factors were reported:
- Failed to maintain flying speed,
- Low ceiling,
- Fog,
- Visibility two miles or less,
- Low altitude straight-in approach toward seaplane ramp,
- Go-around after noticing boat wakes.
Final Report:

Crash of a Nord 262A-33 off Los Angeles: 3 killed

Date & Time: Mar 10, 1979 at 1752 LT
Type of aircraft:
Operator:
Registration:
N418SA
Flight Phase:
Survivors:
Yes
Schedule:
Los Angeles - Santa Maria
MSN:
41
YOM:
1967
Flight number:
WI235
Crew on board:
3
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
8500
Captain / Total hours on type:
879.00
Copilot / Total flying hours:
5600
Copilot / Total hours on type:
424
Aircraft flight hours:
11300
Circumstances:
On March 10, 1979, Swift Aire Lines, Inc., Flight 235, an Aerospatiale Nord 262, N418SA, was being operated as a scheduled passenger flight from Los Angeles, California, to Santa Maria, California. About 1745 PST, flight 235 departed the commuter passenger terminal at the Los Angeles International Airport to taxi to the end of runway 24L via the parallel taxiway. The flight was operating on an instrument flight rules (IFR) flight plan; there were four passengers and three crew members on board. At 1748:11, the crew reported that it was ready for takeoff, and at 1749:04, the flight was cleared to taxi into position on runway 24L and hold. At 1749:34, the tower controller cleared the flight for takeoff and cautioned "possible turbulence, preceding heavy departure. You'll be more than 6 miles in trail." The crew acknowledged the clearance and began the takeoff roll. At 1750:27, the flight was changed over to the departure control radio frequency. At 1751:08, the crew of Flight 235 reported, "We got an emergency, we are going down." The departure controller asked if the flight wanted to return to land. At 1751:14, the crew replied, "We lost both of them." Witnesses who were located along the flightpath of the aircraft at the time of the accident stated that when the aircraft lifted off the runway exhaust smoke from both engines was visible, and when the aircraft crossed the departure end of the runway, the right propeller was observed slowing to a stop. As the aircraft crossed the shoreline, popping sounds were heard from the left engine, and the aircraft stopped climbing and turned north paralleling the shoreline. The witnesses did not hear any engine sounds after the aircraft turned parallel to the shoreline. The witnesses also stated that as the aircraft flew north along the shoreline, it descended in a wings-level attitude, it contacted the water smoothly, bounced twice, impacted the water in a nose down attitude, and sank almost immediately. The flight attendant, who was seated in a rear passenger seat during the takeoff, said that she listened to the crew over the intercom until she heard the gear-up call by the captain and that, until the gear-up call, everything had been normal. At that point, she removed her headset. Shortly thereafter, she noticed that there was no engine noise, and she looked out of the window. Seeing that the aircraft was over water, she then briefed the passengers on crash landing and ditching procedures. She stated that before the aircraft struck the water, the crew had given her two aural warnings of an emergency landing. One passenger stated that acceleration was good during the takeoff and climb out to about 300 to 400 ft. Ile said that shortly after he heard the landing gear go up, he heard a pop, and the right engine lost power and stopped running. This was followed by an increase in power on the left engine, and the aircraft continued to climb momentarily. Then, as it leveled off, the left engine quit. He said it appeared that the captain tried to restart the left engine. The accident occurred during the hours of dusk.
Probable cause:
The National Transportation Safety Board determines that the probable cause of the accident was the flightcrew's mismanagement of an emergency procedure following an autofeather of the right propeller which resulted in their shutting down the remaining engine. Contributing to the accident was the unavailability of vital restart information to the crew. The following findings were reported:
- Shortly after landing gear retraction, the right propeller autofeathered and the engine shut down,
- The right engine shutdown was followed closely by the shutdown of the left engine,
- A leak or break in the propeller pressure line to the autofeather selector probably caused the right propeller to autofeather and the engine to shut down,
- The left engine was shut down inadvertently,
- The left engine probably was shut down because the flight crew failed to properly identify the engine on which the autofeather occurred and moved the left power lever to the stop position,
- A possible restart attempt was not successful because the flight crew was probably unaware that feathering the propeller was a prerequisite to a successful airborne restart,
- The engine restart procedures contained in the aircraft operations manual did not contain sufficient information to effect a restart from an unfeathered condition,
- After the left engine was shut down, there was enough altitude and time available for the crew to get a restart,
- The fatalities occurred when the crewmembers and passenger became trapped or disoriented, or both, by the fast, rushing water that entered the aircraft after it was ditched in the Santa Monica Bay.
Final Report:

Crash of a Piper PA-31-310 Navajo in Hart Mine

Date & Time: Jan 14, 1979 at 1700 LT
Type of aircraft:
Operator:
Registration:
N6567L
Flight Type:
Survivors:
Yes
Site:
Schedule:
Kennewick - San Diego
MSN:
31-489
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5270
Captain / Total hours on type:
35.00
Circumstances:
En route from Kennewick to San Diego, the pilot encountered problems and elected to make a precautionary landing in Hart Mine, California. The airplane crashed in a desert area and was destroyed. All three occupants escaped with minor injuries.
Probable cause:
Controlled collision with ground while in traffic pattern-circuit after the pilot misjudged altitude. The following contributing factors were reported:
- Suspected mechanical discrepancy,
- Kennewick Airport closed during reported departure time,
- Reported flight distance not possible with fuel on board.
Final Report:

Crash of a Grumman G-73 Mallard off Avalon

Date & Time: Jan 14, 1979 at 1640 LT
Type of aircraft:
Operator:
Registration:
N95DF
Flight Phase:
Survivors:
Yes
Schedule:
Avalon - Long Beach
MSN:
J-19
YOM:
1947
Crew on board:
2
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6500
Captain / Total hours on type:
85.00
Circumstances:
While taking off from the Avalon harbour, the seaplane struck three successive waves. On impact, the left engine and the left were torn off. The aircraft came to rest and was damaged beyond repair. All 11 occupants escaped with minor injuries.
Probable cause:
Engine tearaway during takeoff run after the crew selected an unsuitable terrain and failed to abort takeoff. The following contributing factors were reported:
- Premature liftoff,
- Overload failure.
Final Report:

Crash of a Beechcraft G18S in Sacramento: 2 killed

Date & Time: Jan 4, 1979 at 1738 LT
Type of aircraft:
Operator:
Registration:
N104KC
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Sacramento - San Francisco
MSN:
BA-492
YOM:
1960
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
17000
Captain / Total hours on type:
2000.00
Circumstances:
At liftoff, the twin engine airplane stalled and crashed in flames by the runway. The aircraft was destroyed and both pilots were killed.
Probable cause:
Stall during initial climb after the crew failed to abort takeoff and failed to maintain flying speed.
Final Report:

Crash of a Rockwell 680W Turbo Commander II in Lucerne Valley

Date & Time: Nov 11, 1978 at 0300 LT
Registration:
N94HD
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
Schedule:
San Diego - Las Vegas
MSN:
680-1811-28
YOM:
1968
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5420
Captain / Total hours on type:
1105.00
Circumstances:
While in cruising altitude on a flight from San Diego to Las Vegas, the pilot suffered physical impairment. The airplane crashed in a desert area near Lucerne Valley. The pilot was seriously injured and the aircraft was written off.
Probable cause:
Controlled collision with ground after the pilot suffered in-flight physical impairment. Two micrograms per milliliter of benzodiazepine found in his blood sample.
Final Report:

Crash of a Boeing B-52D-75-DO Stratofortress at March AFB: 5 killed

Date & Time: Oct 19, 1978 at 0730 LT
Type of aircraft:
Operator:
Registration:
56-0594
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
March - March
MSN:
17277
YOM:
1956
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
Shortly after takeoff from March AFB, while on a local training mission, the airplane went out of control and crashed in a huge explosion about 2,5 miles southeast from the airfield. A crew member was seriously injured while five others were killed.

Crash of a Learjet 24 in Lancaster: 1 killed

Date & Time: Oct 17, 1978 at 0913 LT
Type of aircraft:
Operator:
Registration:
N123RE
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Lancaster - Lancaster
MSN:
24-154
YOM:
1967
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
8390
Captain / Total hours on type:
379.00
Circumstances:
The crew departed Santa Ana in the early morning to follow a training program at Lancaster-General William J. Fox Airport. He was completing several touch-and-goes when control was lost during initial climb. The airplane swerved on runway and eventually crashed. The copilot was seriously injured while the captain was killed.
Probable cause:
Ground loop and controlled collision with ground during initial climb after the crew failed to maintain directional control while completing touch and go landing.
Final Report: