Crash of an ATR42-320F in Madang

Date & Time: Oct 19, 2013 at 0915 LT
Type of aircraft:
Operator:
Registration:
P2-PXY
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Madang – Tabubil – Kiunga
MSN:
87
YOM:
1988
Flight number:
PX2900
Location:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7110
Captain / Total hours on type:
3433.00
Copilot / Total flying hours:
3020
Copilot / Total hours on type:
2420
Aircraft flight hours:
24375
Circumstances:
On 19 October 2013, an Avions de Transport Régional ATR42-320 freighter, registered P2-PXY (PXY) and operated by Air Niugini, was scheduled to fly from Madang to Tabubil, Western Province, as flight PX2900 carrying a load tobacco for a client company. There were three persons on board; the pilot in command (PIC), a copilot, and a PNG experienced DHC-8 captain whose function was to provide guidance during the approach into Tabubil. The PIC was the handling pilot and the copilot was the support monitoring pilot. The flight crew taxied to the threshold end of runway 25 intending to use the full length of the runway. The take-off roll was normal until the PIC tried to rotate at VR (speed for rotation, which the flight crew had calculated to be 102 knots). He subsequently reported that the controls felt very heavy in pitch and he could not pull the control column back in the normal manner. Flight data recorder (FDR) information indicated that approximately 2 sec later the PIC aborted the takeoff and selected full reverse thrust. He reported later that he had applied full braking. It was not possible to stop the aircraft before the end of the runway and it continued over the embankment at the end of the runway and the right wing struck the perimeter fence. The aircraft was substantially damaged during the accident by the impact, the post-impact fire and partial immersion in salt water. The right outboard wing section was completely burned, and the extensively damaged and burnt right engine fell off the wing into the water. Both propellers were torn from the engine shafts and destroyed by the impact forces.
Probable cause:
The following findings were identified:
- The investigation found that Air Niugini’s lack of robust loading procedures and supervision for the ATR 42/72 aircraft, and the inaccurate weights provided by the consignor/client company likely contributed to the overload.
- The mass and the centre of gravity of the aircraft were not within the prescribed limits.
- The aircraft total load exceeded the maximum permissible load and the load limit in the forward cargo zone ‘A’ exceeded the zone ‘A’ structural limit.
- There was no evidence of any defect or malfunction in the aircraft that could have contributed to the accident.
Final Report:

Crash of a Cessna 208B Grand Caravan in Likawage

Date & Time: Oct 11, 2013
Type of aircraft:
Operator:
Registration:
5H-KEN
Flight Phase:
Survivors:
Yes
Schedule:
Likawage – Dar es Salaam
MSN:
208B-0384
YOM:
1994
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The single engine aircraft was engaged in a charter flight from Likawage to Dar es Salaam, carrying one passenger and two pilots. Ready for takeoff at threshold, the crew applied full power and maintained brakes. Despite the engine did not reach the takeoff power, the captain released brakes and initiated the takeoff roll. The aircraft rolled for about three-quarters of the runway when the engine reached the takeoff power. But the aircraft failed to rotate, continued, overran and eventually collided with trees, bursting into flames. All three occupants were slightly injured and the aircraft was partially destroyed by fire.

Crash of a De Havilland DHC-6 Twin Otter 310 in Kudat: 2 killed

Date & Time: Oct 10, 2013 at 1450 LT
Operator:
Registration:
9M-MDM
Survivors:
Yes
Schedule:
Kota Kinabalu - Kudat
MSN:
804
YOM:
1983
Flight number:
MWG3002
Location:
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
14
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
4700
Aircraft flight hours:
56828
Aircraft flight cycles:
108882
Circumstances:
A de Havilland Canada DHC-6 Twin Otter 310, operated by MASwings, sustained substantial damage in an accident at Kudat Airport (KUD), Malaysia. The copilot and one passenger died, four others were injured. MASwings flight MH3002 operated on a domestic flight from Kota Kinabalu Airport (BKI) to Kudat. The captain was the pilot flying for this sector and the first officer was pilot monitoring. As the aircraft was approaching Kudat Airfield, Kudat Tower reported the weather conditions to be: wind at 270 degrees at 17 kts gusting 31 kts. The aircraft continued the approach on runway 04 and leveled off at 500 feet with flaps set at 10°. At this point the crew noticed that the approach for runway 04 had a strong tail wind. This was evident from the indicated airspeed observed by the crew which indicated 100 kts where the airspeed for flaps 10° should be 65kts. The windsock also indicated a tail wind. Noticing the approach for runway 04 was a tail wind condition, the crew decided to go around at a height of 500ft. Maintaining runway heading, the crew initiated a go around climbing to 1,000ft making a left tear drop and reposition for runway 22. On the approach for runway 22 the captain informed the first officer that if they could not land they would return to Kota Kinabalu. The aircraft was aligned with the centerline of runway 22 and 20° flaps was set. The aircraft continued to descend to 300ft. At this point the wind appeared to be calm as the aircraft did not experience any turbulence and the captain told the first officer that he was committed to land. Upon reaching 200ft the captain called for the flaps to be lowered to full down. As they were about to flare the aircraft to land, approximately 20ft above the runway, the aircraft was suddenly hit by a gust of wind which caused the aircraft to veer to the right with the right wing low and left wing high and the nose was pointing 45° to the right of runway 22. The crew decided to go around by applying maximum power; however the aircraft did not manage to climb successfully. The flaps were not raised and were still in the full flaps down position as the crew thought the aircraft was still low hence the flaps were not raised. The aircraft continued to veer to the right with right wing low and managed to only climb at a shallow rate. The aircraft failed to clear the approaching trees ahead and was unable to continue its climb because the airspeed was reducing. The presence of a full flaps configuration made it more difficult for the aircraft to climb. As the aircraft was on full power on both the engines, it continued to fly almost perpendicularly in relation to the runway and at a low height above the ground. The aircraft hit a tree top at the airfield perimeter fencing, disappeared behind the row of trees, hit another tree behind a house. It hit the right rear roof of the house, ploughed through the roof top of the kitchen, toilet and dining area, hit the solid concrete pillars of the car garage and finally hit the lamp post just outside the house fence. It swung back onto the direction of the runway and came to rest on the ground with its left engine still running. A woman and her 11-year old son who were in the living room at the time escaped unhurt.
Probable cause:
Based on the information from the recorded statements of witnesses and Captain of the aircraft, it clearly indicates that the aircraft was attempting to land on Runway 04 with a tail-wind blowing at 270° 15kts gusting up to 25kts on the first approach, contrary to what was reported by the Captain to the investigators. The demonstrated cross wind landing on the DHC6-310 is 25kts and tailwind landing is 10kts. The aircraft was unsettled and unstable until it passed abeam the terminal building which was not the normal touch down point under normal landing condition. The flap setting on the first approach with the tail-wind condition was at 10°, which is not in accordance with company’s procedures. A tail wind landing condition that will satisfy the criteria for the DHC6-310 is not more than 10kts tail-wind and a flap setting of not more than 20°. One of the stabilized approach criterias for visual conditions (VMC) into Kudat is landing configuration must be completed by 500ft Above Ground Level (AGL) for the DHC6-310 where else if the above conditions could not be met, a go-around should be initiated. Hence, the Crew should have initiated a go-around earlier before the aircraft reached 500ft AGL on the first approach. The aircraft should be in the correct landing configuration at or below the stabilized approach altitude of 500ft AGL, since the aircraft was not stable due to the tail wind and gusting weather. The procedure carried out on the approach for Runway 04 was not consistent with MASwings’ Standard Operating Procedure (SOP) for a tailwind condition. Nonetheless, the first approach for Runway 04 though was uneventful. On the second approach from Runway 22, the wind condition was still not favorable for landing, and gusting. The aircraft was believed to be slightly low on the initial approach and was still unstable. The flap setting for the second approach for Runway 22 was at full flap (37°). As the wind was gusting, a flap setting to full-down should be avoided for the landing as stated in company’s DHC6-310 SOP. With the full-flap configuration, the aircraft had difficulty to settle down on the runway thus dragging the aircraft until abeam the tower which is way beyond the normal touch down zone.
At the point where the aircraft was approaching to land it was reported that the aircraft was hit by a sudden gust, several factors, including the following, have been looked into:
a) Why was the aircraft unable to climb after initiating the go-around?
The full flap setting would require a zero degree pitch attitude to ensure the aircraft speed is maintained. With go-around power set, the zero degree pitch would ensure a climb without speed loss. A pitch above zero degree can cause the aircraft speed to decrease and induce a stall condition resulting in the aircraft being unable to climb.
b) Was the go-around technique executed correctly, taking into consideration that the wind was blowing from 270° and gusting?
The Captain had said that "I applied maximum power and expected the aircraft to climb. At this point, the aircraft was still in left-wing high situation. I noticed the aircraft did make a climb but it was a shallow climb. I did not retract the flaps to 20°, as at that time, in my mind, the aircraft was still low."
c) Under normal conditions, the rule of thumb for initiating a go-around procedure is to apply maximum power, set attitude to climb, confirm airspeed increasing and reduce the flap setting. This procedure was found not to be properly synchronized between MASwings Manuals and DHC6-310 Series 300 SOP.
d) Were the pilots in control of the aircraft?
Based on the Captain’s statement and other associated factors, the pilots were not in total control of the aircraft.

Crash of a Cessna 340A in Hampton Roads: 4 killed

Date & Time: Oct 10, 2013 at 1209 LT
Type of aircraft:
Operator:
Registration:
N4TK
Flight Type:
Survivors:
No
Schedule:
Fort Lauderdale – Hampton Roads
MSN:
340A-0777
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
The instrument-rated pilot was on a cross-country flight. According to air traffic control records, an air traffic controller provided the pilot vectors to an intersection to fly a GPS approach. Federal Aviation Administration radar data showed that the airplane tracked off course of the assigned intersection by 6 nautical miles and descended 800 ft below its assigned altitude before correcting toward the initial approach fix. The airplane then crossed the final approach fix 400 ft below the minimum crossing altitude and then continued to descend to the minimum descent altitude, at which point, the pilot performed a missed approach. The missed approach procedure would have required the airplane to make a climbing right turn to 2,500 ft mean sea level (msl) while navigating southwest back to the intersection; however, radar data showed that the airplane flew southeast and ascended and descended several times before leveling off at 2,800 ft msl. The airplane then entered a right 360-degree turn and almost completed another circle before it descended into terrain. Examination of the wreckage revealed no evidence of any preimpact mechanical malfunctions or failures. During the altitude and heading deviations just before impact, the pilot reported to an air traffic controller that adverse weather was causing the airplane to lose "tremendous" amounts of altitude; however, weather radar did not indicate any convective activity or heavy rain at the airplane's location. The recorded weather at the destination airport about the time of the accident included a cloud ceiling of 400 ft above ground level and visibility of 3 miles. Although the pilot reported over 4,000 total hours on his most recent medical application, the investigation could not corroborate those reported hours or document any recent or overall actual instrument experience. In addition, it could not be determined whether the pilot had experience using the onboard GPS system, which had been installed on the airplane about 6 months before the accident; however, the accident flight track is indicative of the pilot not using the GPS effectively, possibly due to a lack of proficiency or familiarity with the equipment. The restricted visibility and precipitation and maneuvering during the missed approach would have been conducive to the development of spatial disorientation, and the variable flightpath off the intended course was consistent with the pilot losing airplane control due to spatial disorientation. Toxicological tests detected ethanol and other volatiles in the pilot's muscle indicative of postmortem production.
Probable cause:
The pilot's failure to maintain airplane control due to spatial disorientation in low-visibility conditions while maneuvering during a missed approach. Contributing to the accident was the pilot's ineffective use of the onboard GPS equipment.
Final Report:

Crash of a Saab 340B in Udon Thani

Date & Time: Oct 6, 2013 at 0845 LT
Type of aircraft:
Operator:
Registration:
HS-GBG
Flight Phase:
Survivors:
Yes
Schedule:
Chiang Mai - Udon Thani
MSN:
453
YOM:
1998
Flight number:
DD8610
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
25
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Following an uneventful flight from Chiang Mai, the crew completed the landing on runway 30 at Udon Thani Airport. The aircraft vacated runway and was taxiing when control was lost. The airplane veered to the right, entered a soft grassy area, lost its nose gear and came to rest. All 28 occupants evacuated safely and the aircraft was damaged beyond repair.
Probable cause:
Failure of the hydraulic system, causing the malfunction of the nosewheel steering system and the brakes.

Crash of an Embraer EMB-120ER Brasília in Lagos: 16 killed

Date & Time: Oct 3, 2013 at 0932 LT
Type of aircraft:
Operator:
Registration:
5N-BJY
Flight Phase:
Survivors:
Yes
Schedule:
Lagos - Akure
MSN:
120-174
YOM:
1990
Flight number:
SCD361
Country:
Region:
Crew on board:
7
Crew fatalities:
Pax on board:
13
Pax fatalities:
Other fatalities:
Total fatalities:
16
Captain / Total flying hours:
20068
Captain / Total hours on type:
1309.00
Copilot / Total flying hours:
4660
Copilot / Total hours on type:
3207
Aircraft flight hours:
27362
Aircraft flight cycles:
34609
Circumstances:
The crew discussed some concerns about the aircraft prior to departure but at this time we are not prepared to elaborate on those concerns as there remains a lot of work to complete on the CVR analysis in order to determine the specific nature of the crew’s concerns. Associated 361 was cleared for take-off on runway one eight left at Lagos international airport. The wind was calm and weather is not considered a factor in this accident. Approximately 4 seconds after engine power was advanced to commence the take-off roll, the crew received an automated warning from the onboard computer voice which consisted of three chimes followed by “Take-off Flaps…Take-off Flaps”. This is a configuration warning that suggests that the flaps were not in the correct position for take-off and there is some evidence that the crew may have chosen not to use flaps for the take-off. The warning did not appear to come as any surprise to the crew and they continued normally with the take-off. This warning continues throughout the take-off roll. As we are in the process of verifying the accuracy of the flight data, we have not yet been able to confirm the actual flap setting however we expect to determine this in the fullness of time. It was determined from the CVR that the pilot flying was the Captain and the pilot monitoring and assisting was the First Officer. The ‘set power‘ call was made by the Captain and the ‘power is set’ call was confirmed by the First Officer as expected in normal operations. Approximately 3 seconds after the ‘power is set’ call, the First Officer noted that the aircraft was moving slowly. Approximately 7 seconds after the ‘power is set’ call, the internal Aircraft Voice warning system could be heard stating ‘Take off Flaps, Auto Feather’. Auto feather refers to the pitch of the propeller blades. In the feather position, the propeller does not produce any thrust. The FDR contains several engine related parameters which the AIB is studying. At this time, we can state that the Right engine appears to be producing considerably less thrust than the Left engine. The left engine appeared to be working normally. The aircraft automated voice continued to repeat ‘Take-off Flaps, Auto Feather’. The physical examination of the wreckage revealed that the right engine propeller was in the feather position and the engine fire handle was pulled/activated. The standard ‘eighty knots’ call was made by the First Officer. The first evidence that the crew indicated that there was a problem with the take-off roll was immediately following the ‘eighty knots’ call. The First Officer asked if the take- off should be aborted approximately 12 seconds after the ‘eighty knots’ callout. Our investigation team estimates the airspeed to be approximately 95 knots. Airspeed was one of the parameters that, while working in the cockpit, appeared not to be working on the Flight Data Recorder. We were able to estimate the speed based on the radar data that we synchronized to the FDR and CVR but it is very approximate because of this. In response to the First Officer’s question to abort, the Captain indicated that they should continue and they continued the take-off roll. The crew did not make a ‘V1’ call or a Vr’ call. V1 is the speed at which a decision to abort or continue a take-off is made. Vr is the speed at which it is planned to rotate the aircraft. Normally the non-flying pilot calls both the V1 and the Vr speeds. When Vr is called the flying pilot pulls back on the control column and the aircraft is rotated (pitched up) to climb away from the runway. During the rotation, the First Officer stated ‘gently’, which we believe reflects concern that the aircraft is not performing normally and therefore needs to be rotated very gently so as not to aerodynamically stall the aircraft. The First Officer indicated that the aircraft was not climbing and advised the Captain who was flying not to stall the aircraft. Higher climb angles can cause an aerodynamic stall. If the aircraft is not producing enough overall thrust, it is difficult or impossible to climb without the risk of an aerodynamic stall. Immediately after lift-off, the aircraft slowly veered off the runway heading to the right and was not climbing properly. This aircraft behavior appears to have resulted in the Air Traffic Controller asking Flight 361 if operation was normal. Flight 361 never responded. Less than 10 seconds after rotation of the aircraft to climb away from the runway, the stall warning sounded in the cockpit and continued to the end of the recording. The flight data shows characteristics consistent with an aerodynamic stall. 31 seconds after the stall warning was heard, the aircraft impacted the ground in a nose down near 90° right bank.
Probable cause:
The accident was the consequence of the decision of the crew to continue the take-off despite the abnormal No. 2 Propeller rpm indication and a low altitude stall as a result of low thrust at start of roll for take-off from No. 2 Engine caused by an undetermined malfunction of the propeller control unit.
The following contributing factors were identified:
- The aircraft was rotated before attaining V1.
- The decision to continue the take-off with flap configuration warning and auto- feather warning at low speed.
- Poor professional conduct of the flight crew.
- Inadequate application of Crew Resource Management (CRM) principles.
- Poor company culture.
- Inadequate regulatory oversight.
Final Report:

Crash of a Cessna 525A CitationJet CJ2 in Santa Monica: 4 killed

Date & Time: Sep 29, 2013 at 1820 LT
Type of aircraft:
Operator:
Registration:
N194SJ
Flight Type:
Survivors:
No
Schedule:
Hailey - Santa Monica
MSN:
525A-0194
YOM:
2003
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
3463
Captain / Total hours on type:
1236.00
Aircraft flight hours:
1932
Circumstances:
The private pilot was returning to his home airport; the approach was normal, and the airplane landed within the runway touchdown zone markings and on the runway centerline. About midfield, the airplane started to drift to the right side of the runway, and during the landing roll, the nose pitched up suddenly and dropped back down. The airplane veered off the runway and impacted the 1,000-ft runway distance remaining sign and continued to travel in a righthand turn until it impacted a hangar. The airplane came to rest inside the hangar, and the damage to the structure caused the roof to collapse onto the airplane. A postaccident fire quickly ensued. The subsequent wreckage examination did not reveal any mechanical anomalies with the airplane's engines, flight controls, steering, or braking system. A video study was conducted using security surveillance video from a fixed-base operator located midfield, and the study established that the airplane was not decelerating as it passed through midfield. Deceleration was detected after the airplane had veered off the runway and onto the parking apron in front of the rows of hangars it eventually impacted. Additionally, video images could not definitively establish that the flaps were deployed during the landing roll. However, the flaps were deployed as the airplane veered off the runway and into the hangar, but it could not be determined to what degree. To obtain maximum braking performance, the flaps should be placed in the ”ground flap” position immediately after touchdown. The wreckage examination determined that the flaps were in the ”ground flap” position at the time the airplane impacted the hangar. Numerous personal electronic devices that had been onboard the airplane provided images of the passengers and unrestrained pets, including a large dog, with access to the cockpit during the accident flight. Although the unrestrained animals had the potential to create a distraction during the landing roll, there was insufficient information to determine their role in the accident sequence or what caused the delay in the pilot’s application of the brakes.
Probable cause:
The pilot’s failure to adequately decrease the airplane’s ground speed or maintain directional control during the landing roll, which resulted in a runway excursion and collision with an airport sign and structure and a subsequent postcrash fire.
Final Report:

Crash of a Cessna 421C Golden Eagle III in Lyon-Bron: 4 killed

Date & Time: Sep 24, 2013 at 1045 LT
Operator:
Registration:
N556MB
Flight Phase:
Survivors:
No
Schedule:
Lyon - Aix-les-Milles
MSN:
421C-00468
YOM:
1978
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
410
Captain / Total hours on type:
12.00
Copilot / Total flying hours:
579
Copilot / Total hours on type:
3
Aircraft flight hours:
3661
Circumstances:
After takeoff from runway 34 at Lyon-Bron Airport, while in initial climb at a height of 200 feet, the twin engine airplane deviated to the left, rolled to the left and then veered to the left with a low rate of climb. Shortly after passing the end of the runway, the airplane lost height then struck the ground and caught fire. The airplane was destroyed by a post crash fire and all four occupants were killed. For unknown reasons, the pilot-in-command was seating in the right seat.
Probable cause:
The accident probably occurred as a result of an asymmetrical flight starting from the rotation that the pilot was not able to control. As technical examinations and observations from the wreckage could not give any conclusive malfunction of the engines or systems, the initial cause is most likely an improper adjustment of the steering trim before takeoff. The poor experience of the pilot on this high powered and complex aircraft as well as the low height reached did not allow the pilot to understand and manage the situation quickly and avoid the loss of control.
Final Report:

Crash of a Beechcraft C90A King Air in Idaho Falls

Date & Time: Sep 19, 2013 at 1553 LT
Type of aircraft:
Operator:
Registration:
N191TP
Survivors:
Yes
Schedule:
Pocatello – Idaho Falls
MSN:
LJ-1223
YOM:
1989
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3975
Captain / Total hours on type:
2500.00
Aircraft flight hours:
4468
Circumstances:
The airplane was equipped with two main fuel tanks (132 usable gallons each) and two nacelle fuel tanks (60 usable gallons each). In normal operation, fuel from each nacelle tank is supplied to its respective engine, and fuel is automatically transferred from each main tank to its respective nacelle tank. While at the airplane's home airport, the pilot noted that the cockpit fuel quantity gauges indicated that the nacelle tanks were full, and he believed that the main tanks had fuel sufficient for 30 minutes of flight. The pilot did not verify by any other means the actual fuel quantity in any of the tanks. Thirty gallons of fuel were added to each main tank; they were not topped off. The airplane, with two passengers, then flew to an interim stop about 45 miles away, where a third passenger boarded. The airplane then flew to its destination, another 165 miles away. The pilot reported that, at the destination airport, he noted that the cockpit fuel quantity gauges indicated that the nacelle tanks were full; he surmised that the main fuel tanks were not empty but did not note the actual quantity of fuel. Forty gallons of fuel were added to each main tank. Again, the main tanks were not topped off, and the pilot did not verify by any other means the actual fuel quantity in any of the tanks. The return flight to the interim stop was uneventful. The third passenger deplaned there, and the airplane departed for its home airport. While on final approach to the home airport, both engines stopped developing power, and the pilot conducted a forced landing to a field about 1.2 miles short of the runway. The pilot later reported that, at the time of the power loss, the fuel quantity gauges indicated that there was still fuel remaining in the airplane. Postaccident examination of the airplane revealed that all four fuel tanks were devoid of fuel. The examination did not reveal any preimpact mechanical anomalies, including fuel leaks, that would have precluded continued flight. The airplane manufacturer conducted fuel-consumption calculations for each of the two city pairs. Because the pilot did not provide any information regarding flight routes, altitudes, speeds, or times for any of the flight segments, the manufacturer's calculations were based on direct routing in zero-wind conditions, nominal airplane and engine performance, and assumed cruise altitudes and speeds. Although the results are valid for these input parameters, variations in any of the input parameters can significantly affect the calculated fuel requirements. As a result, although the manufacturer's calculations indicated that the round trip would have burned less fuel than the total available fuel quantity that was derived from the pilot-provided information, the lack of any definitive information regarding the actual flight parameters limited the utility of the calculated value and the comparison. The manufacturer's calculations indicated that the accident flight leg (from the interim airport to the home airport) would have consumed about 28.5 gallons total. Given that the airplane was devoid of fuel at the accident site, the pilot likely departed the interim airport with significantly less than the manufacturer's minimum allowable departure fuel quantity of about 39.5 gallons per side. The lack of any observed preimpact mechanical problems with the airplane, combined with the lack of objective or independently substantiated fuel quantity information, indicates that the airplane's fuel exhaustion was due to the pilot's inadequate and improper pre- and inflight fuel planning and procedures.
Probable cause:
The pilot's inadequate preflight fuel planning, which resulted in departure with insufficient fuel to complete the flight, and consequent inflight power loss due to fuel exhaustion.
Final Report:

Crash of a PZL-Mielec AN-2R in Kamako

Date & Time: Sep 13, 2013 at 1150 LT
Type of aircraft:
Operator:
Registration:
9Q-CFT
Survivors:
Yes
Schedule:
Tshikapa - Kamako
MSN:
1G223-14
YOM:
1987
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
16798
Captain / Total hours on type:
16000.00
Aircraft flight hours:
6981
Circumstances:
Following an uneventful flight from Tshikapa, the pilot initiated the approach to Kamako Airfield in relative good conditions. On final, the wind component suddenly changed. The aircraft lost height and impacted ground 16 metres short of runway 12. Upon impact, the undercarriage were partially torn off and the aircraft slid before coming to rest 37 metres past the runway threshold. All six occupants, one pilot and five passengers, escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
It was determined that the loss of control that occurred on short final was the result of the combination of a human error and weather component. The pilot was surprised by the abrupt change in weather conditions on short final to Kamako runway 12. He elected to initiate a go-around procedure and increased engine power but unfortunately, low level windshear caused the aircraft to lose height and to struck the ground as its speed was insufficient. In consequence, the increase power was too low to allow the pilot to maintain the approach profile. The torsion of the blades confirmed that the engine was at full power for a go-around procedure at impact. The absence of a windsock at Kamako Airfield was considered as a contributing factor as this would help the pilot to recognize the wind component and to decide to land or to go-around in due time.
Final Report: