Crash of a Swearingen SA226TC Metro II in Emerald

Date & Time: Apr 2, 1981
Type of aircraft:
Operator:
Registration:
VH-BPL
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
TC-272
YOM:
1978
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
At liftoff, the pilot lost control of the airplane that crashed on runway. The pilot, sole on board, was injured and the aircraft was damaged beyond repair.

Crash of a Cessna 402A near Mount Hagen: 8 killed

Date & Time: Apr 1, 1981
Type of aircraft:
Operator:
Registration:
P2-GKJ
Survivors:
No
Site:
Schedule:
Port Moresby – Goroka – Mount Hagen
MSN:
402A-0081
YOM:
1969
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
8
Circumstances:
While approaching Mount Hagen Airport in poor weather conditions, the twin engine airplane struck the slope of a wooded mountain. The aircraft was totally destroyed and all eight occupants were killed.
Probable cause:
Controlled flight into terrain.

Crash of a Fletcher FU-24-950 in Otangiwai: 1 killed

Date & Time: Mar 2, 1981 at 1025 LT
Type of aircraft:
Operator:
Registration:
ZK-DUI
Flight Phase:
Survivors:
No
Schedule:
Otangiwai - Otangiwai
MSN:
195
YOM:
1971
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
10898
Circumstances:
An aerial topdressing operation was being carried out from an airstrip near Otangiwai. The sowing area was on an adjacent farm property. The pilot commenced sowing over the higher ground in the area, but as the morning progressed turbulence became significant in the lee of the hills and the highly experienced pilot ( 10,898 flying hours ) decided to turn his attention to the lower part of the farm. Accordingly a sortie was carried out over the northeastern corner of the property. At 10:20 the pilot took off to make another series of sowing runs over the same area. The Fletcher did not come back from this sortie and at about 11:00 the wreckage of ZK-DUI was found. Fire had not occurred.The pilot was dead. The crash site was on a level river flat.The aircraft had dived into the ground at an angle of at least 60 degrees to the horizontal and probably near vertically. The propeller was separated from the engine and buried 1 metre in the soil. Compression damage had severed the fuselage at the middle of the cockpit and the remainder of the aircraft had rebounded and came to rest on the main wheels some 8 metres from the forward fuselage. The rear fuselage was folded in half behind the wing. No fertilizer was in the hopper and there was none in the vicinity of the wreck.The left outer wing panel was found about 100 metres from the rest of the plane. Its leading edge section was missing. Cable marks showed that the LE section had been sheared off from the main spar by a wire cable. The investigation found that the aircraft had collided in flight with a single 11,000 volt conductor, or wire, at roughly the center of the 500 metre span between two poles. The collision was at a height of about 220 feet AGL and about 600 metres from the crash site. The wire was strung across the valley as part of a 4-kilometre-long electrical supply line installed by the local power authority only about five weeks before.
Probable cause:
The accident investigator concluded that this accident was probably caused by a loss of control of the aircraft after it was substantially damaged in a collision with a power conductor.

Crash of a Piper PA-31-350 Navajo Chieftain in Portland: 1 killed

Date & Time: Jan 26, 1981 at 1538 LT
Registration:
VH-POC
Flight Phase:
Survivors:
Yes
Schedule:
Portland - Melbourne
MSN:
31-7952087
YOM:
1979
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
815
Captain / Total hours on type:
83.00
Circumstances:
The operator had undertaken to carry out a ship's crew exchange programme that consisted of transporting 16 persons and their baggage from Portland to Essendon and the same number back to Portland. Similar programmes had been carried out previously and it was known that the passengers usually carried considerable baggage. However, only two Piper PA-31-350 aircraft, VH-POC and VH-RNH, were assigned to the task. Prior to departure Essendon, both pilots attended the Briefing Office and prepared flight plans, intended to operate under the Instrument Flight Rules and the pilots calculated it would be necessary to load 208 minutes fuel for the first return flight to Portland. This included an additional 30 minutes fuel for holding, as was required because of forecast thunderstorm activity, with associated reduced visibility in rain, in the Essendon area. Both pilots elected to have their aircraft refuelled to capacity which, they indicated on their flight plans, would give them a total of 280 minutes endurance; 72 minutes more than required. The aircraft proceeded to Portland without known incident, arriving at about 14:00 hours. After a break for refreshments, the pilots returned to their aircraft at about 1500 hours and carried out pre-flight checks. The passengers arrived at the aerodrome in a number of vehicles. Initially the pilots began to weigh the baggage and record the weights on a manifest. The passengers were in a light-hearted mood, however, and with an atmosphere of some confusion, not all of the baggage was weighed, the manifest was not completed and no individual weights were marked on the bags.The baggage was then transported by trolleys to the aircraft and shared between them without consideration of weight. The baggage in the rear baggage area of the cabin of VH-POC was not restrained to prevent movement. The pilots decided that, by inspection, the average baggage weight per passenger was 20 kg. The accepted standard weight of 77 kg per adult passenger was also assumed. Each pilot then completed a load sheet for his aircraft, on the basis of carrying eight passengers. The sheet for VH-POC indicated that the aircraft fuel load was 290 kg. The total weight calculated for VH-POC was 3,080 kg. This was less than the maximum allowable all-up-weight of 3,178 kg. However, an incorrect aircraft operating weight had been used and an arithmetical error had occurred in the calculation. Correcting for these, the aircraft weight should have been recorded as 3,256 kg. When ready to embark, the passengers were only directed towards the two aircraft. No effort was made to split the party into two even groups and in the event, nine passengers boarded VH-POC. On boarding VH-POC, the pilot did not correct the passenger imbalance. He started both engines and proceeded to taxi for a take-off on Runway 22. Pre-take-off checks were carried out as the aircraft taxied. The weather conditions at the time were fine; visibility 15 km, temperature 22° Celsius, sea level barometric pressure 1007 millibars and surface wind from 210° to 220° magnetic, gusting from 25 to 35 knots. In such wind conditions, and because of the location near a coastal headland, there was significant turbulence present. The pilot of VH-POC had operated into Portland on numerous prior occasions and had experienced this common situation previously. The take-off run was commenced and the pilot reported that full power was obtained from both engines. He stated that at 95 kts the aircraft was rotated and, when a positive rate of climb had been established, the landing gear was retracted. Then, at a height of 60 to 70 feet, just after he had reduced power to the climb setting, the left engine suddenly lost power. Ground witnesses who observed the take-off reported that the aircraft appeared slow to accelerate. Once airborne, it maintained a low climb profile and, at one stage, slewed to the right. Irregular engine noise was heard but it was not identified to a particular engine. The pilot reported that he confirmed a left engine failure by closing the left throttle. On fully re-opening the throttle, however, he noted a slight power response and hence he elected not to shut down the engine and feather the left propeller. Several of the passengers were aware of an abnormal situation but none was aware of the nature of the problem nor could confirm which engine was malfunctioning. They reported that the landing gear audio warning was sounding throughout most of the flight, which indicated a throttle was at or near the closed position. The pilot reported that the aircraft began to lose height and, as a forced landing was imminent, he turned to the right to avoid the sea. Control had been difficult in the gusty conditions but he had managed to reduce speed, lower the landing gear and guide the aircraft to a landing in a reasonably suitable area. The aircraft touched down on undulating-, sandy scrub-covered terrain. The landing gear and engines were torn out and the aircraft came to rest after travelling only some 26 metres. The fuselage broke open near the rear door during the ground slide. Some passengers were able to evacuate the cabin without assistance and they rendered help to the pilot and other passengers. A small fire, which had ignited in the vicinity of the left engine as the aircraft came to rest, then suddenly spread and engulfed the fuselage before the final passenger could be extricated. Subsequent examination of the wreckage was hampered by the extensive fire damage. No pre-existing fault was found in those components that were recovered. An inspection of the left propeller found that it had been feathered at ground impact. It was not possible to establish precisely the aircraft's weight and centre of gravity at the time of the accident as the contents of the nose and engine nacelles baggage compartments were destroyed. The available evidence, however, indicated that the aircraft weighed at least 3400 kg and its centre of gravity was probably beyond the aft limit. Piper PA31-350 performance data indicated that, for a new aircraft, the maximum attainable single-engine rate of climb at the limit weight of 3,178 kg was 220 feet per minute. At a weight of 3,400 kg this would be reduced by about 40 percent to 134 feet per minute. At the higher weight, detracting factors such as aircraft age, turbulence and less than optimum airspeed would have precluded the aircraft from achieving a positive rate of climb. The pilot was briefly interviewed in hospital on 27.1.81. At that time he also submitted a written notification of the accident. Subsequently, he has declined, through industrial counsel, to either attend for an interview under procedures of the Air Safety Investigation Branch or to supply answers to written questions. Hence it has not been possible to fully resolve a number of safety aspects of the accident, such as aircraft loading, the nature of the power loss and subsequent aircraft handling considerations.
Probable cause:
The probable cause of the accident was that the aircraft experienced a loss of power from one engine under conditions which precluded a safe continuation of flight. The two most significant conditions were aircraft overloading and turbulence. The nature and cause of the power loss have not been determined.
Final Report:

Crash of a Bristol 170 Freighter 31E in Blenheim

Date & Time: Jan 14, 1981
Type of aircraft:
Operator:
Registration:
ZK-CAM
Flight Type:
Survivors:
Yes
MSN:
13155
YOM:
1953
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Upon landing at Blenheim-Woodbourne Airport, the right main gear collapsed. The airplane slid for few dozen yards before coming to rest. All four occupants escaped uninjured while the aircraft was written off.
Probable cause:
Fatigue crack in landing gear centre fitting.

Crash of a Fletcher FU-24 in Yass

Date & Time: Dec 31, 1980
Type of aircraft:
Operator:
Registration:
VH-EOA
Flight Phase:
Survivors:
Yes
MSN:
43
YOM:
1957
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed in unknown circumstances in Yass while engaged in a crop spraying mission. The pilot, sole on board, was injured.

Crash of a Partenavia P.68B in Bankstown

Date & Time: Dec 23, 1980
Type of aircraft:
Operator:
Registration:
VH-IYO
Flight Phase:
Flight Type:
Survivors:
Yes
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Shortly after takeoff from Bankstown Airport, while climbing, the twin engine airplane stalled and crashed in a camping lot. The pilot, sole on board, was injured. There were no injuries on ground.

Crash of a Britten-Norman BN-2A Trislander Mk.III-2 near Tumut: 2 killed

Date & Time: Dec 16, 1980
Type of aircraft:
Registration:
VH-EGU
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Bankstown - Melbourne
MSN:
1030
YOM:
1976
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
While flying over the Snowy Mountains on a cargo flight from Bankstown to Melbourne, the pilot reported icing conditions. Shortly later, the three engine airplane went out of control and crashed in a wooded area. The aircraft was destroyed and both occupants were killed. It was later reported that a cold front was coming across the area with low temperatures and icing conditions.
Probable cause:
It is believed that the loss of control was the consequence of an excessive accumulation of ice on airframe as well as on carburetors.

Crash of a Pilatus PC-6/B1-H2 Turbo Porter near Oakey

Date & Time: Nov 28, 1980
Operator:
Registration:
A14-681
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
681
YOM:
1968
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Aircraft flight hours:
5840
Circumstances:
While flying at low height, the single engine airplane struck power cables and crashed in an open field, bursting into flames. All occupants escaped with minor injuries while the aircraft was destroyed by fire.

Crash of a Boeing 727-92C on Yap Island

Date & Time: Nov 21, 1980 at 0952 LT
Type of aircraft:
Operator:
Registration:
N18479
Survivors:
Yes
Schedule:
Saipan – Agana – Yap – Palau
MSN:
19174
YOM:
1966
Flight number:
CO614
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
67
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
14000
Captain / Total hours on type:
700.00
Copilot / Total flying hours:
7000
Copilot / Total hours on type:
5500
Aircraft flight hours:
30878
Aircraft flight cycles:
20788
Circumstances:
Air Micronesia Flight 614 departed Saipan at 07:30 for a flight to Palau with intermediate stops in Guam and Yap, Western Caroline Islands. The aircraft departed Guam at 08:30 and climbed to FL350. An en route descent to Yap was made from the north through broken to scattered clouds and the captain, who was flying the aircraft, turned onto a downwind leg at the northeast portion of the airport. The downwind leg was flown at an altitude of 600 feet above the runway 07 elevation while the crew checked to see if the runway was clear, to see if the fire truck was in place, and to see the direction of the windsock. The flaps were set at 30° on the base leg. Abeam the approach end of runway 07, the captain began a right 90° and a left turn manoeuvre to align the aircraft with the final approach to runway 07. During a portion of the downwind leg, the captain relinquished control of the aircraft to the first officer while the captain took pictures of the airport. He then resumed control and passed the camera to the second officer and asked him to take pictures of the runway. As the aircraft passed through 90deg from the runway heading, it had descended to about 300 feet above the runway elevation of 52 feet msl. When the aircraft was aligned with the runway heading, it was about 480 feet above runway elevation at a point 1.5 miles from the approach end of the runway. At 09:52 the aircraft touched down 13 feet short of runway 07. The right main landing gear immediately separated from the aircraft. The aircraft gradually veered off the runway and came to rest in the jungle about 1,700 feet beyond the initial touchdown. A severe ground fire erupted immediately along the right side of the aircraft as it came to rest. All occupants had evacuated within about 1 minute after the aircraft came to rest.
Probable cause:
The Captain's premature reduction of thrust in combination with flying a shallow approach slope angle to an improper touchdown aim point. These actions resulted in a high rate of descent and a touchdown on upward sloping terrain short of the runway threshold, which generated loads that exceeded the design strength and failed the right-hand landing gear. Contributing to the accident were the Captain's lack of recent experience in the B-727 aircraft and a transfer of his DC-10 aircraft landing habits and techniques to the operation of the B-727 aircraft.
Final Report: