Crash of a De Havilland DHC-2 Beaver off Lyall Haarbour: 6 killed

Date & Time: Nov 28, 2009 at 1603 LT
Type of aircraft:
Operator:
Registration:
C-GTMC
Flight Phase:
Survivors:
Yes
Schedule:
Vancouver - Mayne Island - Pender Island - Lyall Harbour - Vancouver
MSN:
1171
YOM:
1958
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
2800
Captain / Total hours on type:
2350.00
Circumstances:
The Seair Seaplanes Beaver was departing Lyall Harbour, Saturna Island, for the water aerodrome at the Vancouver International Airport, British Columbia. After an unsuccessful attempt at taking off downwind, the pilot took off into the wind towards Lyall Harbour. At approximately 1603 Pacific Standard Time, the aircraft became airborne, but remained below the surrounding terrain. The aircraft turned left, then descended and collided with the water. Persons nearby responded immediately; however, by the time they arrived at the aircraft, the cabin was below the surface of the water. There were 8 persons on board; the pilot and an adult passenger survived and suffered serious injuries. No signal from the emergency locator transmitter was heard.
Probable cause:
Findings as to Causes and Contributing Factors:
1. The combined effects of the atmospheric conditions and bank angle increased the load factor, causing an aerodynamic stall.
2. Due to the absence of a functioning stall warning system, in addition to the benign stalling characteristics of the Beaver, the pilot was not warned of the impending stall.
3. Because the aircraft was loaded in a manner that exceeded the aft CG limit, full stall recovery was compromised.
4. The altitude from which recovery was attempted was insufficient to arrest descent, causing the aircraft to strike the water.
5. Impact damage jammed 2 of the 4 doors, restricting egress from the sinking aircraft.
6. The pilot’s seat failed and he was unrestrained, contributing to the seriousness of his injuries and limiting his ability to assist passengers.
Findings as to Risk:
1. There is a risk that pilots will inadvertently stall aircraft if the stall warning system is unserviceable or if the audio warnings have been modified to reduce noise levels.
2. Pilots who do not undergo underwater egress training are at greater risk of not escaping submerged aircraft.
3. The lack of alternate emergency exits, such as jettisonable windows, increases the risk that passengers and pilots will be unable to escape a submerged aircraft due to structural damage to primary exits following an impact with the water.
4. If passengers are not provided with explicit safety briefings on how to egress the aircraft when submerged, there is increased risk that they will be unable to escape following an impact with the water.
5. Passengers and pilots not wearing some type of flotation device prior to an impact with the water are at increased risk of drowning once they have escaped the aircraft.
Final Report:

Crash of a McDonnell Douglas MD-11F in Shanghai: 3 killed

Date & Time: Nov 28, 2009 at 0814 LT
Type of aircraft:
Operator:
Registration:
Z-BAV
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Shanghai - Bishkek
MSN:
48408/457
YOM:
1990
Flight number:
SMJ324
Country:
Region:
Crew on board:
7
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
The three engine aircraft departed Shanghai-Pudong Airport on a cargo flight to Bishkek, carrying various goods and seven crew members. During the takeoff roll from runway 35L, the pilot-in-command initiated the rotation but the aircraft did not lift off properly with had a negative vario. It overran the runway and eventually crashed in an open field. Three crew were killed while four others were injured. The aircraft was totally destroyed.
Probable cause:
The crew did not properly operate the thrust levers so that the engines did not reach take off thrust. The aircraft had not reached Vr at the end of the runway and could not get airborne. According to the design criteria of the MD11 the crew needs to push at least two thrust levers to beyond 60 degrees, which will trigger autothrust to leave "CLAMP" mode and adjust the thrust to reach the target setting for takeoff, the servo motors would push the thrust levers forward in that case. During the accident departure the pilot in the left seat did not advance the thrust levers to more than 60 degrees, hence the server motors did not work although autothrust was engaged but remained in CLAMP mode and thus did not adjust the thrust to reach takeoff settings. The crew members perceived something was wrong. Audibly the engine sound was weak, visibibly the speed of the aircraft was low, tactically the pressure on the back of the seat was weaker than normal. Somebody within the crew, possibly on the observer seats, suggested the aircraft may be a bit heavy. The T/O THRUST page never appeared (it appears if autothrust is engaged and changes from CLAMP to Thrust Limit setting. Under normal circumstances with autothrust being engaged a click sound will occur as soon as the thrust levers reach the takeoff thrust position. A hand held on the thrust levers will feel the lever moving forward, however, the crew entirely lost situational awareness. None of the anomalies described in this paragraph prompted the crews members' attention. When the aircraft approached the end of the runway several options were available: reject takeoff and close the throttles, continue takeoff and push the throttle to the forward mechanical stop, continue takeoff and immediately rotate. The observer called "rotate", the captain rotated the aircraft. This shows the crew recognized the abnormal situation but did not identify the error (thrust levers not in takeoff position) in a hurry but reacted instinctively only. As the aircraft had not yet reached Vr, the aircraft could not get airborne when rotated. As verified in simulator verification the decision to rotate was the wrong decision. The simulator verification showed, that had the crew pushed the thrust levers into maximum thrust when they recognized the abnormal situation, they would have safely taken the aircraft airborne 670 meters before the end of the runway. The verification also proved, that had the crew rejected takeoff at that point, the aircraft would have stopped before the end of the runway. The crew did not follow standard operating procedures for managing thrust on takeoff. The crew operations manual stipulates that the left seat pilot advances the thrust levers to EPR 1.1 or 70% N1 (depending on engine type), informs the right seat pilot to connect autothrust. The pilot flying subsequently pushes the thrust levers forward and verifies they are moving forward on servos, the pilot monitoring verifies autothrust is working as expected and reaches takeoff thrust settings. In this case the left seat pilot not only did not continue to push the thrust levers forward, but also called out "thrust set" without reason as he did not verify the takeoff thrust setting had been achieved. It is not possible to subdivide the various violations of procedures and regulations. The crew had worked 16 hours during the previous sector. In addition, one crew member needed to travel for 11 hours from Europe to reach the point of departure of the previous sector (Nairobi Kenya), two crew members need to travel for 19 hours from America to the point of departure of the previous sector. These factors caused fatigue to all crew members. The co-pilot was 61 years of age, pathological examination showed he was suffering from hypertension and cardiovascular atherosclerosis. His physical strength and basic health may have affected the tolerance towards fatigue. All crew members underwent changes across multiple time zones in three days. Although being in the period of awakeness in their biological rhythm cycle, the cycle was already in a trough period causing increased fatigue. The captain had flown the Airbus A340 for 300 hours in the last 6 months, which has an entirely different autothrust handling, e.g. the thrust levers do not move with power changes in automatic thrust, which may have caused the captain to ignore the MD-11 thrust levers. The co-pilot in the right hand seat had been MD-11 captain for about 7 years but had not flown the MD-11 for a year. Both were operating their first flight for the occurrence company. The two pilots on the observer seats had both 0 flight hours in the last 6 months. The co-pilot (right hand seat) was pilot flying for the accident sector. The captain thus was responsible for the thrust management and thrust lever movement according to company manual. A surviving observer told the investigation in post accident interviews that the captain was filling out forms and failed to monitor the aircraft and first officer's actions during this critical phase of flight. There are significant design weaknesses in the MD-11 throttle, the self checks for errors as well as degree of automation is not high.
Source: Aviation Herald/Simon Hradecky

Crash of a Lockheed KC-130J Hercules in Pisa: 5 killed

Date & Time: Nov 23, 2009 at 1410 LT
Type of aircraft:
Operator:
Registration:
MM62176
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Pisa - Pisa
MSN:
5497
YOM:
2000
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
Shortly after takeoff from Pisa-San Giusto-Galileo Galilei Airport, while climbing, the four engine aircraft went out of control and crashed on a railway road located 3 km southwest of the airfield. The aircraft was destroyed by impact forced and a post crash fire and all five occupants from the 46th Squadron were killed.

Crash of a Cessna 208B Grand Caravan in Windhoek: 3 killed

Date & Time: Nov 15, 2009 at 0658 LT
Type of aircraft:
Operator:
Registration:
ZS-OTU
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Windhoek – Ondjiva – Lubango – Luanda
MSN:
208B-0513
YOM:
1996
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
671
Captain / Total hours on type:
206.00
Aircraft flight hours:
12469
Circumstances:
On 15 November 2009, at about 0458Z, and aircraft a Cessna Caravan 208B, with a pilot and three passengers on board, took off from Eros Airport for a flight to Ondjiva, Lubango and Luanda. On board the aircraft were a substantial amount of cargo, which included building materials, meat, paints, bottles of wine etc. which was placed between and on top of the seats as well as in the cargo-pod. The cargo inside the cabin area was not secured. Shortly after takeoff from runway 19, the aircraft turned to the right and then pitched nose up. According to the passenger who survived, the aircraft entered into a left spin shortly after the nose pitched up and second later impacted with terrain, coming to rest facing the direction it took off from. The pilot and two passengers were fatally injured during the accident. One of the passengers survived the accident and was admitted to a local hospital with s spinal injury. The pilot-in-command was a holder of a commercial pilot licence. His medical certificate was valid with restrictions (to wear corrective lenses). Fine weather was reported during the time of the accident with surface wind of 180° at 8 knots.
Probable cause:
The investigations revealed that during this operation the aircraft's take-off weight was exceeded by 629 pounds. The aircraft failed to maintain flying speed and stalled shortly after takeoff, rendering ground impact inevitable.
The following contributing factors were identified:
- This was the pilot's first flight from Eros Airport therefore being unfamiliar with the airport and the environmental phenomena's associated with it (especially taking off from runway 19),
- The pilot made one fundamental error in his weight calculation that he used the incorrect aircraft empty weight,
- The cargo that was in the cabin was packed between and underneath and on top of the seats and was not secured,
- The aircraft took off from runway 19, which was an upslope runway,
- Taking off from runway 19 the terrain kept rising with mountains straight ahead as well as to the left and right,
- The pilot retracted the flaps shortly after rotation, which resulted in an attitude change and performance (aircraft lost altitude), which should be regarded as a significant contributory factor to this accident,
- The pilot was observed to turn to the right shortly after takeoff, which increased the drag on the aircraft as well as the stall speed,
- Harsh anti-erosion rubber paint that was sprayed onto the leading edge of the wings resulted in an increased stall speed,
- Inadequate oversight by the regulatory authority should be regarded as a significant contributory factor to this accident.
Final Report:

Ground accident of an Ilyushin II-76MD in Ivanovo

Date & Time: Nov 7, 2009
Type of aircraft:
Operator:
Registration:
RA-86894
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
00134 32977
YOM:
1981
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Aircraft flight hours:
6200
Circumstances:
The crew lined up on runway and was cleared for takeoff. Power was added on all four engine and the crew started the takeoff roll when the engine n°3 detached from its pylon, fall on the ground and rolled for about 150 metres before coming to rest. The crew stopped the airplane and evacuated safely. The aircraft was damaged beyond repair.
Probable cause:
The engine n°3 detached during the takeoff roll for unknown reasons.

Crash of a Grumman G-111 Albatross in Fort Pierce

Date & Time: Nov 5, 2009 at 1534 LT
Type of aircraft:
Registration:
N120FB
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Fort Pierce - Okeechobee
MSN:
G-331
YOM:
1953
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
9095
Captain / Total hours on type:
14.00
Copilot / Total flying hours:
11500
Copilot / Total hours on type:
1100
Aircraft flight hours:
3747
Circumstances:
The pilot stated that during the landing gear retraction he heard a loud bang, followed by three to four smaller bangs. The first officer confirmed that the left engine was the affected engine and immediately began feathering the propeller. Once the propeller had been feathered, the captain confirmed the action by looking outside and noticing the propeller in the feathered position. The captain further reported that the right engine was producing the maximum power available and was indicating 55 inches of manifold pressure. Unable to achieve airspeed of greater than 95 to 96 knots indicated, the captain attempted to return to the airport for an emergency landing; however, he was unable to maintain altitude and attempted to land on an airport perimeter road, impacting the airport fence and a sand berm in the process. A cursory examination of the engine and system components revealed no evidence of a preimpact mechanical malfunction.
Probable cause:
A total loss of left engine power and subsequent failure of the airplane to maintain airspeed and altitude on the remaining engine for undetermined reasons.
Final Report:

Crash of a Xian MA60 in Harare

Date & Time: Nov 3, 2009 at 1936 LT
Type of aircraft:
Operator:
Registration:
Z-WPJ
Flight Phase:
Survivors:
Yes
Schedule:
Harare - Bulawayo
MSN:
03 01
YOM:
2005
Flight number:
UM239
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
34
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
During the takeoff roll at Harare Airport, the aircraft was bout to lift off when it collided with five warthogs, causing the left main gear to be torn off. Out of control, the aircraft veered off runway to the left and came to rest. All 38 occupants evacuated safely while the aircraft was damaged beyond repair.
Probable cause:
Loss of control during takeoff following a collision with five warthogs.

Crash of an Ilyushin II-76MD in Mirny: 11 killed

Date & Time: Nov 1, 2009 at 0849 LT
Type of aircraft:
Registration:
RF-76801
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Mirny – Irkutsk – Chita
MSN:
00934 95866
YOM:
1989
Country:
Region:
Crew on board:
7
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
11
Circumstances:
The four engine aircraft departed Mirny on a positioning flight to Chita with an intermediate stop in Irkutsk, carrying four passengers and a crew of seven on behalf of the Russian Ministry of the Interior. Shortly after takeoff by night, the aircraft rolled to the right to an angle of 90° then crashed at a speed of 364 km/h some 1,893 metres past the runway end. The aircraft was totally destroyed and all 11 occupants were killed. The accident occurred 59 seconds after takeoff.
Probable cause:
The day before the accident, the aircraft arrived in Mirny following a cargo flight, delivering various goods. After landing, the crew activated the electrical locking system for the rudder and the ailerons, and the 'lock on' light came on in the cockpit panel. In the morning of the accident, prior to takeoff, the crew followed the pre-takeoff checklist and deactivated the electrical locking system, but the 'lock on' light remained illuminated. Considering this as a false alarm, the captain decided to take off and proceeded with a manuel control of the ailerons. The left aileron moved normally while the right aileron got locked because of the locking mechanism. During the takeoff roll, because the four engine were not in full power mode, there was no sound alarm about the aileron locked mechanism. The aircraft deviated to the right and after lift off, it rolled to the right to angle of 8°. The pilot-in-command elected to counteract the banking but this maneuver was limited due to the right aileron locked mechanism. The aircraft continued to roll to the right to an angle of 90° until control was lost.

Crash of a Boeing 707-330C in Sharjah: 6 killed

Date & Time: Oct 21, 2009 at 1531 LT
Type of aircraft:
Operator:
Registration:
ST-AKW
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Sharjah - Khartoum
MSN:
20123/788
YOM:
1969
Flight number:
AZZ2241
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
19943
Copilot / Total flying hours:
6649
Copilot / Total hours on type:
900
Aircraft flight hours:
77484
Aircraft flight cycles:
26888
Circumstances:
The Aircraft was operating a flight from Sharjah International Airport, UAE to Khartoum International Airport, Sudan, with a total of six persons on board: three flight crew members (captain, co-pilot, and flight engineer), a ground engineer, and two load masters. All of the crew members sustained fatal injuries due to the high impact forces. Sometime after of liftoff, the core cowls of No. 4 engine separated and collapsed onto the departure runway, consequently No. 4 Engine Pressure Ratio (“EPR”) manifold flex line ruptured leading to erroneous reading on the EPR indicator. The crew interpreted the EPR reading as a failure of No. 4 engine; accordingly they declared engine loss and requested the tower to return to the Airport. The Aircraft went into a right turn, banked and continuously rolled to the right at a high rate, sunk, and impacted the ground with an approximately 90° right wing down attitude.
Probable cause:
The Investigation identified the following Causes:
(a) the departure of the No. 4 engine core cowls;
(b) the consequent disconnection of No. 4 engine EPR Pt7 flex line;
(c) the probable inappropriate crew response to the perceived No. 4 engine power loss;
(d) the Aircraft entering into a stall after the published maximum bank angle was exceeded; and
(e) the Aircraft Loss of Control (“LOC”) that was not recoverable.

Contributing Factors to the Accident were:
(a) the Aircraft was not properly maintained in accordance with the Structure Repair
Manual where the cowls had gone through multiple skin repairs that were not up to
aviation standards;
(b) the Operator’s maintenance system failure to correctly address the issues relating to the No. 4 engine cowls failure to latch issues;
(c) the failure of the inspection and maintenance systems of the maintenance organization, which performed the last C-Check, to address, and appropriately report, the damage of the No. 4 engine cowls latches prior to issuing a Certificate of Release to Service;
(d) the Operator’s failure to provide a reporting system by which line maintenance personnel report maintenance deficiencies and receive timely and appropriate guidance and correction actions;
(e) the Operator’s quality system failure to adequately inspect and then allow repairs that were of poor quality or were incorrectly performed to continue to remain on the Aircraft; and
(f) the SCAA safety oversight system deficiency to adequately identify the Operator’s chronic maintenance, operations and quality management deficiencies.
Final Report:

Crash of a Pilatus PC-12/47E in Weert: 2 killed

Date & Time: Oct 16, 2009 at 0824 LT
Type of aircraft:
Registration:
PH-RUL
Flight Phase:
Survivors:
No
Schedule:
Budel - Egelsbach
MSN:
1130
YOM:
2009
Flight number:
PHRUL
Location:
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
783
Captain / Total hours on type:
84.00
Aircraft flight hours:
95
Circumstances:
The aircraft took off from Budel-Kempen Airport runway 21 at 0822LT. After liftoff, pilot was instructed to make a left turn and was cleared to climb to 2,000 feet. While flying in clouds, the autopilot was disengaged. The aircraft rolled to the right then entered a steep descent and crashed in an open field located in Weert, east of the airport. The aircraft disintegrated on impact and both occupants were killed, among them Paul Evers, Director of Alko International.
Probable cause:
Technical or medical problems could not be ruled out according to Dutch Safety Board. However, it was considered likely that the pilot suffered from spatial disorientation.
Factors were:
- the fact that the autopilot disengaged;
- the high work load following loss of autopilot, during a single-pilot flight;
- the lack of training and experience on advanced aircraft like the PC-12 in manually flying the aircraft in IMC in a non-normal situation.
Final Report: