Crash of an IAI 1124A Westwind II in Huntsville: 3 killed

Date & Time: Jun 18, 2014 at 1424 LT
Type of aircraft:
Registration:
N793BG
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Huntsville - Huntsville
MSN:
392
YOM:
1983
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
20200
Captain / Total hours on type:
850.00
Copilot / Total flying hours:
28421
Copilot / Total hours on type:
1816
Aircraft flight hours:
7571
Circumstances:
A pilot proficiency examiner (PPE) was using the airplane to conduct a pilot-in-command (PIC) proficiency check for two company pilots. Before the accident flight, one of the two company pilots on board received a PIC proficiency check, which terminated with a full-stop landing and reverse thrust application; no discrepancies with either thrust reverser were discussed by either flight crewmember. The pilot being examined then left the cockpit, and the accident pilot positioned himself in the left front seat while the PPE remained in the right front seat. The flight crew then taxied to the approach end of the runway to begin another flight. Data from the enhanced ground proximity system (EGPWS) revealed that, the flight began the takeoff roll with the flaps retracted, the thrust reversers armed, and both engines stabilized at 96 percent N2. About 2 seconds later, the cockpit voice recorder (CVR) recorded the "V1" call while on the airplane was on the runway; acoustic analysis indicated that the N2 speed of one engine, likely the right, decreased; the N2 speed of the other engine remained constant. This decrease in N2 speed was consistent with the PPE retarding right engine thrust to flight idle with the intent of simulating an engine failure. The takeoff continued, and, while the airplane was in a wings-level climb at an airspeed of 148 knots about 18 ft radar altitude, the CVR recorded the pilot command that the landing gear be retracted. The landing gear remained extended, and, about 1 second after the command to retract the landing gear, or about 3 seconds after becoming airborne, while about 33 ft above the runway and at the highest recorded airspeed of 149 knots, the CVR recorded the beginning of a rattling sound, which was consistent with the deployment of the right thrust reverser, and it continued to the end of the recording. About 1.5 seconds after the rattling sound began, the CVR recorded the PPE asking, "…what happened," which indicates that the deployment was likely not annunciated in the cockpit. The right engine N2 speed continued to gradually decrease, and the airplane rolled slightly left, back to a wings-level position. The airplane continued climbing with the landing gear extended as pitch changes continued to occur. During this time, the flight crew exchanged comments about their lack of understanding about what was occurring. While flying 10 knots above V2 speed with the left engine N2 speed remaining steady and the right engine N2 speed decreasing at a slightly greater rate than previously, the airplane began a right roll with a corresponding steady decrease in airspeed from about 144 knots. About 9 seconds after the original call to retract the landing gear, the CVR recorded the PPE requesting that the landing gear be retracted, which occurred 1 second later. The airplane then continued in the right turn with the airspeed steadily decreasing, and about 11 seconds after the PPE asked "…what happened", the EGPWS sounded a bank angle alert. At that time, the airplane was in a right roll of about 30 degrees, and the airspeed was about 132 knots. The right roll continued to a maximum value of about 39 degrees, which was the last valid bank angle value recorded. The airplane impacted the ground off the right side of the runway in a nose- and right-winglow attitude. The landing gear and flaps were retracted, and there was no evidence of preimpact failure or malfunction of the flight controls for roll, pitch, and yaw; nor was there any evidence of a mechanical failure or malfunction of either engine. A definitive reason for the deployment of the right thrust reverser could not be determined. No previous instances of inadvertent in-flight thrust reverser deployment were documented by the operator of the accident airplane or by the airframe manufacturer for the accident airplane make and model. Certification flight testing of an airplane with the same thrust reverser system determined that the airplane remained controllable with the right thrust reverser deployed and throttle retarder system functioning. The flight testing also included application of a momentary, peak burst of right engine thrust, again with no controllability issues noted. It was also noted that with the installed throttle retarder system, in the event of inadvertent thrust reverser deployment, that the engine's thrust should have been reduced to idle within 4 to 8 seconds. Acoustic analysis of the accident flight indicated that the lowest recorded N2 rpm value was about 84 percent and that the reduction in rpm occurred over a period of about 8.5 seconds, after the right thrust reverser deployed. No determination could be made as to why the throttle retarder system did not reduce the right engine thrust to flight idle as designed. Additionally, no determination could be made as to why the flight crew was not able to maintain directional control of the airplane following deployment of the right thrust reverser. Although the PPE had severe coronary artery disease, which placed him at risk for an acute coronary event that would cause symptoms like chest pain, shortness of breath, or sudden unconsciousness, the CVR recorded no evidence of impairment. Neither the heart disease nor the medications he was taking to treat it would have impaired his judgement or physical functioning. Therefore, it is unlikely any medical condition or substance contributed to the PPE's actions. Additionally, there was no evidence that any medical condition would have impaired judgement or physical functioning of the pilot being examined.
Probable cause:
The flight crew's inability to maintain airplane control during initial climb following deployment of the right thrust reverser for reasons that could not be determined because postaccident examination of the airframe and engine thrust reverser system did not reveal any anomalies. Contributing to the accident was the excessive thrust from the right engine with the thrust reverser deployed for reasons that could not be determined during postaccident examinations and testing.
Final Report:

Crash of a Piper PA-46-500TP Malibu Meridian in White Plains: 1 killed

Date & Time: Jun 13, 2014 at 0808 LT
Registration:
N5335R
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
White Plains - Portland
MSN:
46-97100
YOM:
2001
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
5100
Captain / Total hours on type:
134.00
Aircraft flight hours:
1931
Circumstances:
The pilot arrived at the fixed-base operator on the morning of the accident and requested that his airplane be brought outside and prepared for an immediate departure; this occurred 1 hour 15 minutes before his scheduled departure time. Radar data showed that the airplane departed 23 minutes later. According to air traffic control data, shortly thereafter, the ground and departure controllers contacted the tower controller and asked if the airplane had departed yet; the tower controller responded, "I have no idea. We have zero visibility." Weather conditions about the time of the accident included a 200-ft overcast ceiling with about 1/4-mile visibility. Only five radar targets identified as the accident airplane were captured, and all of the targets were located over airport property. The first three radar targets began about midpoint of the 6,500-ft-long runway, and each of these targets was at an altitude of about 60 ft above ground level (agl). The final two targets showed the airplane in a shallow right turn, consistent with the published departure procedure track, at altitudes of 161 and 261 ft agl, respectively. The final radar target was about 1/2 mile from the accident site. Witnesses reported observing the airplane impact trees in a wings-level, slightly right-wing-down attitude at high speed. Examination of the wreckage revealed no preimpact mechanical malfunctions or anomalies of the airplane. The pilot's personal assistant reported that the pilot had an important meeting that required his attendance on the day of the accident flight. His early arrival to the airport and his request to have the airplane prepared for an immediate departure were actions consistent with self-induced pressure to complete the flight. Due to the poor weather conditions, which were expected to continue or worsen, he likely felt pressure to expedite his departure to ensure he was able to make it to his destination and to attend the meeting. This pressure may have further affected his ability to discern the risk associated with departing in low-visibility and low-ceiling conditions. As noted, the weather conditions were so poor that the local air traffic controller stated that he could not tell whether the airplane had departed. Such weather conditions are highly conducive to the development of spatial disorientation. Further, the altitude profile depicted by the radar data and the airplane's near wings-level attitude and high speed at impact were consistent with the pilot experiencing a form of spatial disorientation known as "somatogravic illusion," in which the pilot errantly perceives the airplane's acceleration as increasing pitch attitude, and efforts to hold the nose down or arrest the perception of increasing pitch attitude can exacerbate the situation. Such an illusion can be especially difficult to overcome because it typically occurs at low altitudes after takeoff, which provides little time for recognition and subsequent corrective inputs, particularly in very low-visibility conditions.
Probable cause:
The pilot's failure to maintain a positive climb rate after takeoff due to spatial disorientation (somatogravic illusion). Contributing to the accident was the pilot's self-induced pressure to depart and his decision to depart in low-ceiling and low-visibility conditions.
Final Report:

Crash of an Antonov AN-2 in Starosel'ye: 2 killed

Date & Time: Jun 7, 2014 at 1440 LT
Type of aircraft:
Operator:
Registration:
RF-02883
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Starosel'ye - Starosel'ye
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
Shortly after takeoff from Starosel'ye Airfield, while in initial climb, the aircraft impacted trees, stalled and crashed in a wooded area, bursting into flames. The aircraft was totally destroyed by a post crash fire and both occupants were killed. It was reported that the aircraft was not on the Russian Aviation Register and that the registration RF-02883 was unknown to the authority. Also, the pilot decided to takeoff from an airstrip that was closed to traffic and failed to announce his flight to ATC.

Crash of a Beechcraft B200 Super King Air in Bahía Solano

Date & Time: Jun 2, 2014 at 1700 LT
Operator:
Registration:
PNC-0225
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
BB-1644
YOM:
1998
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Shortly after takeoff from Bahía Solano-José Celestino Mutis Airport, while in initial climb, the crew encountered engine problems. The captain attempted an emergency landing in a prairie. The aircraft landed gear up and slid for few dozen metres before coming to rest. While all three occupants escaped with minor injuries, the aircraft was damaged beyond repair.

Crash of a Gulfstream GIV in Bedford: 7 killed

Date & Time: May 31, 2014 at 2140 LT
Type of aircraft:
Operator:
Registration:
N121JM
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Bedford – Atlantic City
MSN:
1399
YOM:
2000
Crew on board:
3
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
11250
Captain / Total hours on type:
1400.00
Copilot / Total flying hours:
18200
Copilot / Total hours on type:
2800
Aircraft flight hours:
4945
Aircraft flight cycles:
2745
Circumstances:
The aircraft crashed after it overran the end of runway 11 during a rejected takeoff at Laurence G. Hanscom Field (BED), Bedford, Massachusetts. The airplane rolled through the paved overrun area and across a grassy area, collided with approach lights and a localizer antenna, passed through the airport’s perimeter fence, and came to a stop in a ravine. The two pilots, a flight attendant, and four passengers died. The airplane was destroyed by impact forces and a postcrash fire. The corporate flight, which was destined for Atlantic City International Airport, Atlantic City, New Jersey, was conducted under the provisions of 14 Code of Federal Regulations (CFR) Part 91. An instrument flight rules flight plan was filed. Night visual meteorological conditions prevailed at the time of the accident. During the engine start process, the flight crew neglected to disengage the airplane’s gust lock system, which locks the elevator, ailerons, and rudder while the airplane is parked to protect them against wind gust loads. Further, before initiating takeoff, the pilots neglected to perform a flight control check that would have alerted them of the locked flight controls. A review of data from the airplane’s quick access recorder revealed that the pilots had neglected to perform complete flight control checks before 98% of their previous 175 takeoffs in the airplane, indicating that this oversight was habitual and not an anomaly. A mechanical interlock between the gust lock handle and the throttle levers restricts the movement of the throttle levers when the gust lock handle is in the ON position. According to Gulfstream, the interlock mechanism was intended to limit throttle lever movement to a throttle lever angle (TLA) of no greater than 6° during operation with the gust lock on. However, postaccident testing on nine in-service G-IV airplanes found that, with the gust lock handle in the ON position, the forward throttle lever movement that could be achieved on the G-IV was 3 to 4 times greater than the intended TLA of 6°. During takeoff, the pilot-in-command (PIC) manually advanced the throttle levers, but the engine pressure ratio (EPR) did not reach the expected level due to the throttles contacting the gust lock/throttle lever interlock. The PIC did not immediately reject the takeoff; instead, he engaged the autothrottle, and the throttle levers moved slightly forward, which allowed the engines to attain an EPR value that approached (but never reached) the target setting. As the takeoff roll continued, the second-in-command made the standard takeoff speed callouts as the airplane successively reached 80 knots, the takeoff safety speed, and the rotation speed. When the PIC attempted to rotate the airplane, he discovered that he could not move the control yoke and began calling out “(steer) lock is on.” At this point, the PIC clearly understood that the controls were locked but still did not immediately initiate a rejected takeoff. If the flight crew had initiated a rejected takeoff at the time of the PIC’s first “lock is on” comment or at any time up until about 11 seconds after this comment, the airplane could have been stopped on the paved surface. However, the flight crew delayed applying brakes for about 10 seconds and further delayed reducing power by 4 seconds; therefore, the rejected takeoff was not initiated until the accident was unavoidable. Among the victims was Lewis Katz, co-owner of the 'Philadelphia Inquirer'.
Probable cause:
The NTSB determines that the probable cause of this accident was the flight crewmembers’ failure to perform the flight control check before takeoff, their attempt to take off with the gust lock system engaged, and their delayed execution of a rejected takeoff after they became aware that the controls were locked. Contributing to the accident were the flight crew’s habitual noncompliance with checklists, Gulfstream Aerospace Corporation’s failure to ensure that the G-IV gust lock/throttle lever interlock system would prevent an attempted takeoff with the gust lock engaged, and the Federal Aviation Administration’s failure to detect this inadequacy during the G-IV’s certification.
Final Report:

Crash of an ATR42-500 in Coari

Date & Time: May 30, 2014 at 2055 LT
Type of aircraft:
Operator:
Registration:
PR-TKB
Flight Phase:
Survivors:
Yes
Schedule:
Coari - Manaus
MSN:
610
YOM:
2000
Location:
Country:
Crew on board:
4
Crew fatalities:
Pax on board:
45
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total hours on type:
2601.00
Copilot / Total flying hours:
5898
Copilot / Total hours on type:
548
Circumstances:
During the takeoff roll from Coari-Urucu Airport by night, the aircraft collided with a tapir that struck the right main gear. The crew continued the takeoff procedure and the flight to Manaus. After two hours and burning fuel, the aircraft landed at Manaus-Eduardo Gomes Airport. Upon touchdown, the right main gear collapsed and the aircraft veered to the right and came to rest. All 49 occupants evacuated safely while the aircraft was damaged beyond repair.
Probable cause:
Collision with a tapir during takeoff, causing severe damages to the right main gear.
The following findings were identified:
- The lack of isolation of the operational area allowed the land animal to enter the runway for landings and takeoffs, contributing to the accident.
- The crew did not notice the presence of the land animal on the runway early enough to abort the takeoff without extrapolating the runway limits and avoiding collision.
- The presence of the land animal (Tapirus terrestris) interfered with the operation and led to the collision of the right main landing gear.
Final Report:

Crash of a Rockwell Shrike Commander 500S in Fort Huachuca: 1 killed

Date & Time: May 17, 2014 at 1020 LT
Operator:
Registration:
N40TC
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Fort Huachuca - Fort Huachuca
MSN:
500-3091
YOM:
1976
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
13175
Captain / Total hours on type:
600.00
Copilot / Total flying hours:
16560
Copilot / Total hours on type:
4100
Aircraft flight hours:
21660
Circumstances:
The commercial pilot reported that the purpose of the flight was to perform a check/orientation flight with the airline transport pilot (ATP), who was new to the area; the ATP was the pilot flying. The airplane was started, and an engine run-up completed. The commercial pilot reported that, during the takeoff roll, all of the gauges were in the “green.” After reaching an airspeed of 80 knots, the airplane lifted off the ground. About 350 ft above ground level (agl), the pilots felt the airplane “jolt.” The commercial pilot stated that it felt like a loss of power had occurred and that the airplane was not responding. He immediately shut off the boost pumps, and the ATP initiated a slow left turn in an attempt to return to the airport to land. The airplane descended rapidly in a nose-low, right-wing-low attitude and impacted the ground. A witness reported that he watched the airplane take off and that it sounded normal until it reached the departure end of the runway, at which point he heard a distinct “pop pop,” followed by silence. The airplane then entered an approximate 45-degree left turn with no engine sound and descended at a high rate with the wings rolling level before the airplane went out of sight. Another witness made a similar statement. Based on the witnesses’ statements and photographs of the twisted airplane at the accident site, it is likely that a total loss of engine power occurred and that, during the subsequent turn back to the airport, the ATP did not maintain sufficient airspeed and exceeded the airplane’s critical angle-of-attack, which resulted in an aerodynamic stall and impact with terrain. Although a postaccident examination of the airframe and engines did reveal an inconsistency between the cockpit control positions and the positions of the fuel shutoff valves on the sump tank, this would not have precluded normal operation. No other anomalies were found that would have precluded normal operation.
Probable cause:
The pilot’s failure to maintain adequate airspeed and his exceedance of the airplane’s critical angle-of-attack after a total loss of engine power during the takeoff initial climb, which resulted in an aerodynamic stall and impact with terrain. The reason for the total loss of engine power could not be determined because an examination of the airframe and engines did not reveal any anomalies that would have precluded normal operation.
Final Report:

Crash of a Harbin Yunsunji Y-12-II in El Wak: 1 killed

Date & Time: May 12, 2014
Type of aircraft:
Operator:
Registration:
KAF124
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Mandera – El Wak – Garissa – Nairobi
MSN:
0095
YOM:
1997
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
10
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
Shortly after takeoff from El Wak Airfield, bound for Garissa, the twin engine aircraft stalled and crashed. The copilot was killed while 11 other occupants were injured. The aircraft was destroyed.

Crash of a PZL-Mielec AN-2T in Gryazi

Date & Time: May 9, 2014 at 1630 LT
Type of aircraft:
Operator:
Registration:
RF-00446
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Terbuny – Gryazi
MSN:
1G236-07
YOM:
1989
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft was returning to its base in Gryazi after taking part to a demonstration in Terbuny. After takeoff, while in initial climb, the engine lost power. The aircraft encountered difficulties to gain height, impacted power cables and crashed in an open field. All nine occupants evacuated safely and the aircraft was damaged beyond repair.
Probable cause:
Loss of engine power for unknown reasons.

Crash of a Quest Kodiak 100 in Doyo Baru: 2 killed

Date & Time: Apr 9, 2014 at 0940 LT
Type of aircraft:
Operator:
Registration:
PK-SDF
Flight Phase:
Survivors:
Yes
Schedule:
Doyo Baru – Ninia
MSN:
100-0049
YOM:
2011
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
25530
Captain / Total hours on type:
1752.00
Aircraft flight hours:
1752
Aircraft flight cycles:
2211
Circumstances:
A Kodiak-100 aircraft, registered PK-SDF, on 9 April 2014 was being operated by PT. Adventist Aviation Indonesia as non-schedule flight from Doyo Baru Airstrip with intended destination of Ninia Airstrip, Papua. On board in this flight were 7 persons consist of one pilot and six passengers. This flight was the fourth flights for the pilot who has performed flights from Doyo Baru (DOB) – Puldamat (PUL) at 2138-2228 UTC; Puldamat (PUL) –Soya (SOY) at 2243-2247 UTC; Soya (SOY) – Doyo Baru (DOB) at 2256-2344 UTC. The flight time to destination was estimated of 1 hour with cruising altitude of 10,000 feet and the fuel on board were sufficient for 4 hours flight time. Doyo Baru Airstrip located at approximately 10 NM North West of Sentani Airport (WAJJ). Air traffic movement to and from Doyo Baru Airstrip was controlled by Sentani Tower controller. At 0015 UTC, the pilot contacted to Sentani Tower controller, requested for start engine and clearance to fly to Ninia. The requests were approved and to report when ready for departure. At 0021 UTC, the pilot reported to the Sentani Tower controller ready for departure from Doyo Baru Airstrip. The Sentani Tower Controller instructed the pilot to hold to wait an aircraft took off from Sentani Airport. At 0024 UTC, the pilot received clearance for takeoff with additional traffic information and to report after airborne. At 0027 UTC, Sentani Tower controller has not received reports from the PK-SDF pilot and tried to call but was not responded. After several observations toward Doyo Baru area and did not see PK-SDF aircraft, The Sentani Tower controller reported to the Chief Section of Sentani Tower Air Navigation. At 0030 UTC, The Chief Section of Sentani Tower Air Navigation clarified the condition of PK-SDF aircraft to one of Indonesian Adventist Aviation pilot in Doyo Baru and obtained information that the aircraft had experienced in accident during takeoff at Doyo Baru. An engineer after received the information went to the accident site and saw appearance of white smoke came out from the side of the river which was known as the accident aircraft located. After arrived at the accident site the engineer saw the Adventist’s staffs and local people tried to extinguish the fire on the aircraft engine by throwing some water and used two fire extinguishers while some people moved the passengers from the wreckage. Two occupants including the pilot were fatally injured and five other passengers were seriously injured. All occupants were taken to Yowari Hospital (Rumah Sakit Umum Daerah – RSUD Yowari).
Probable cause:
Contributing Factors:
- The failure to airborne was due to the aircraft was not in correct takeoff configuration which required wing flap 20° while the flap was found at approximately 6° position during impact.
- The actions to recover the situation by selection of emergency power and flap were not proper for particular condition.
Final Report: