Crash of an Embraer EMB-545 Praetor 500 in Brunswick

Date & Time: Sep 21, 2023 at 1436 LT
Operator:
Registration:
N434FX
Survivors:
Yes
Schedule:
White Plains – Brunswick
MSN:
550-10073
YOM:
2020
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10900
Captain / Total hours on type:
1872.00
Copilot / Total flying hours:
16686
Copilot / Total hours on type:
306
Aircraft flight hours:
2863
Circumstances:
On September 21, 2023, about 1436 eastern daylight time, an Embraer SA EMB-525, N434FX, operated by Flexjet LLC, was substantially damaged when it was involved in an accident near St. Simons Island, Georgia. The pilot, copilot and six passengers were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91K fractional flight. The flight departed Westchester County Airport (HPN), White Plains, New York at 1239, destined for St. Simons Island Airport (SSI), St. Simons Island, Georgia. According to the pilot, the departure and en route phases of the flight were uneventful. During the arrival phase into SSI they elected to fly the RNAV (GPS) Runway 4 approach to allow them to be better aligned and setup for the landing. Checklists and callouts were conducted, and the approach was stable. After the 500 ft stable callout was made the airplane crossed over a small section of trees and rose slightly. The airplane then began to porpoise slightly when it was about 100 to 150 ft above mean sea level. The pilot tried to make corrections, but the airplane was not responding to his control inputs. The airplane then landed hard and slid along the runway, coming to rest in the grass off of runway 4. After the airplane came to rest, they evacuated the passengers safely and powered down the airplane. According to the copilot, the flight from HPN to SSI was uneventful until the final few seconds. When they were cleared for the approach, the pilot configured the airplane, slowed appropriately, and selected “Flaps 3” for the landing. The checklists were completed, and they had the runway in sight when they were 10 miles from the airport. No other traffic was identified as being in the airport traffic pattern and they prepared to land. The copilot made the “500’, Stabilized, 20 knot of headwind” callout at approximately 500 ft’. As the airplane crossed above the airport property, it began to pitch rapidly up and down. The copilot then looked over at the pilot’s hand on the control side sick and he could see him moving it back and forth excessively. He then said something along the lines of “Take it easy there,” and the pilot replied that the airplane was not responding. At that point the airplane was “maybe 50 ft” above the runway. The airplane touched down hard, prior to the runway threshold, on centerline, bounced and then touched down again. The airplane was listing to the right and skidding on the runway while slowly drifting to the right. The airplane slid off the runway and onto the grass where it hit a concrete sign base before it came to rest on the grass. Prior to opening the main cabin door, the copilot realized that both engines were still running. He then asked the pilot to shut down engines so that he could open the door to deplane the passengers. The copilot observed fuel gushing from the belly of the airplane when he exited. Examination of the accident site and airplane revealed that the airplane was substantially damaged. Both main landing gear were damaged, and the struts had punctured the top of the wings. During the impact sequence the airplane skidded down runway 4 for approximately 2,531 ft, then departed the right side of the runway, shearing off eight runway lights, one taxiway light, and destroying the taxiway A4 directional sign. The right main landing gear separated from the airplane and the leading edge of the right wing was damaged consistent with the impact with the taxiway sign. The airplane then went across taxiway A4, coming to rest between runway 4, taxiway A, and taxiway A4. The total distance from the airplane’s touchdown to where the airplane came to rest was approximately 3,083 ft. The reported wind at SSI about the time of the accident was from 050° at 13 knots, gusting to 23 knots. According to Federal Aviation Administration (FAA) and pilot records, the pilot held an airline transport pilot certificate, with a rating for airplane multi engine land, and commercial privileges for airplane single engine land and single engine sea. He also held type ratings on the BE-300, BE-400, CE-560XL, CE-650, CL-600, EMB-550, HS-125, and MU-300. His most recent FAA firstclass medical certificate was issued on June 13, 2023. He reported that he had accrued approximately 10,900 total flight hours, with 1,872 hours in the airplane make and model. According to FAA and pilot records, the copilot held an airline transport pilot certificate with a rating for airplane multi engine land, and commercial privileges for airplane single engine land. He also held type ratings on the A-310, A-320, B-757, B-767, DC-9, DC-10, EMB-550, and LR-JET. His most recent FAA first-class medical certificate was issued on June 13, 2023. He reported that he had accrued approximately 16,686 total flight hours, with 306 hours in the airplane make and model. According to FAA and maintenance records, the airplane was manufactured in 2020. The airplane’s most recent continuous airworthiness inspection was completed on April 11, 2023, at 2,863 total hours of operation.

Crash of a Swearingen SA226T Merlin IIIB in Farmingdale

Date & Time: Jun 20, 2016 at 1758 LT
Operator:
Registration:
N127WD
Flight Type:
Survivors:
Yes
Schedule:
White Plains - Farmingdale
MSN:
T-297
YOM:
1978
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
11450
Captain / Total hours on type:
410.00
Copilot / Total flying hours:
1300
Copilot / Total hours on type:
5
Aircraft flight hours:
4500
Circumstances:
According to the pilot in command (PIC), he was conducting an instructional flight for his "new SIC (second in command)," who was seated in the left seat. He reported that they had flown two previous legs in the retractable landing gear-equipped airplane. He recalled that, during the approach, they discussed the events of their previous flights and had complied with the airport control tower's request to "keep our speed up." During the approach, he called for full flaps and retarded the throttle to flight idle. The PIC asserted that there was no indication that the landing gear was not extended because he did not hear a landing gear warning horn; however, he was wearing a noise-cancelling headset. He added that the landing gear position lights were not visible because the SIC's knee obstructed his view of the lights. He recalled that, following the flare, he heard the propellers hit the runway and that he made the decision not to go around because of unknown damage sustained to the propellers. The airplane touched down and slid to a stop on the runway. The airplane sustained substantial damage to the fuselage bulkheads, longerons, and stringers. The SIC reported that the flight was a training flight in visual flight rules conditions. He noted that the airspace was busy and that, during the approach, he applied full flaps, but they failed to extend the landing gear. He added that he did not hear the landing gear warning horn; however, he was wearing a noise-cancelling headset. The Federal Aviation Administration Aviation Safety Inspector that examined the wreckage reported that, during recovery, the pilot extended the nose landing gear via the normal extension process. However, due to significant damage to the main landing gear (MLG) doors, the MLG was unable to be extended hydraulically or manually. He added that an operational check of the landing gear warning horn was not accomplished because the wreckage was unsafe to enter after it was removed from the runway. The landing gear warning horn was presented by an aural tone in the cockpit and was not configured to be heard through the pilots' noise-cancelling headsets. When asked, the PIC and the SIC both stated that they could not remember who read the airplane flight manual Before Landing checklist.
Probable cause:
The pilot-in-command's failure to extend the landing gear before landing and his failure to use the Before Landing checklist. Contributing to the accident was the pilots' failure to maintain a sterile cockpit during landing.
Final Report:

Crash of a Piper PA-46-500TP Malibu Meridian in White Plains: 1 killed

Date & Time: Jun 13, 2014 at 0808 LT
Registration:
N5335R
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
White Plains - Portland
MSN:
46-97100
YOM:
2001
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
5100
Captain / Total hours on type:
134.00
Aircraft flight hours:
1931
Circumstances:
The pilot arrived at the fixed-base operator on the morning of the accident and requested that his airplane be brought outside and prepared for an immediate departure; this occurred 1 hour 15 minutes before his scheduled departure time. Radar data showed that the airplane departed 23 minutes later. According to air traffic control data, shortly thereafter, the ground and departure controllers contacted the tower controller and asked if the airplane had departed yet; the tower controller responded, "I have no idea. We have zero visibility." Weather conditions about the time of the accident included a 200-ft overcast ceiling with about 1/4-mile visibility. Only five radar targets identified as the accident airplane were captured, and all of the targets were located over airport property. The first three radar targets began about midpoint of the 6,500-ft-long runway, and each of these targets was at an altitude of about 60 ft above ground level (agl). The final two targets showed the airplane in a shallow right turn, consistent with the published departure procedure track, at altitudes of 161 and 261 ft agl, respectively. The final radar target was about 1/2 mile from the accident site. Witnesses reported observing the airplane impact trees in a wings-level, slightly right-wing-down attitude at high speed. Examination of the wreckage revealed no preimpact mechanical malfunctions or anomalies of the airplane. The pilot's personal assistant reported that the pilot had an important meeting that required his attendance on the day of the accident flight. His early arrival to the airport and his request to have the airplane prepared for an immediate departure were actions consistent with self-induced pressure to complete the flight. Due to the poor weather conditions, which were expected to continue or worsen, he likely felt pressure to expedite his departure to ensure he was able to make it to his destination and to attend the meeting. This pressure may have further affected his ability to discern the risk associated with departing in low-visibility and low-ceiling conditions. As noted, the weather conditions were so poor that the local air traffic controller stated that he could not tell whether the airplane had departed. Such weather conditions are highly conducive to the development of spatial disorientation. Further, the altitude profile depicted by the radar data and the airplane's near wings-level attitude and high speed at impact were consistent with the pilot experiencing a form of spatial disorientation known as "somatogravic illusion," in which the pilot errantly perceives the airplane's acceleration as increasing pitch attitude, and efforts to hold the nose down or arrest the perception of increasing pitch attitude can exacerbate the situation. Such an illusion can be especially difficult to overcome because it typically occurs at low altitudes after takeoff, which provides little time for recognition and subsequent corrective inputs, particularly in very low-visibility conditions.
Probable cause:
The pilot's failure to maintain a positive climb rate after takeoff due to spatial disorientation (somatogravic illusion). Contributing to the accident was the pilot's self-induced pressure to depart and his decision to depart in low-ceiling and low-visibility conditions.
Final Report:

Crash of a Cessna 402B in Biddeford: 1 killed

Date & Time: Apr 10, 2011 at 1805 LT
Type of aircraft:
Operator:
Registration:
N402RC
Flight Type:
Survivors:
No
Site:
Schedule:
White Plains - Portland
MSN:
402B-1218
YOM:
1977
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4735
Captain / Total hours on type:
120.00
Aircraft flight hours:
6624
Circumstances:
The multi-engine airplane was being repositioned to its base airport, and the pilot had requested to change the destination, but gave no reason for the destination change. Radar data indicated that the airplane entered the left downwind leg of the traffic pattern, flew at pattern attitude, and then performed a right approximate 250-degree turn to enter the final leg of the approach. During the final leg of the approach, the airplane crashed short of the runway into a house located in a residential neighborhood near the airport. According to the airplane's pilot operating handbook, the minimum multi-engine approach speed was 95 knots indicated airspeed (KIAS), and the minimum controllable airspeed was 82 KIAS. According to radar data, the airplane's ground speed was about 69 knots with the probability of a direct crosswind. Post accident examination of the propellers indicated that both propellers were turning at a low power setting at impact. During a controlled test run of the right engine, a partial power loss was noted. After examination of the throttle and control assembly, two o-rings within the assembly were found to be damaged. The o-rings were replaced with comparable o-rings and the assembly was reinstalled. During the subsequent test run, the engine operated smoothly with no noted anomalies. Examination of the o-rings revealed that the damage was consistent with the o-rings being pinched between the corner of the top o-ring groove and the fuel inlet surface during installation. It is probable that the right engine had a partial loss of engine power while on final approach to the runway due to the damaged o-ring and that the pilot retarded the engine power to prevent the airplane from rolling to the right. The investigation found no mechanical malfunction of the left engine that would have prevented the airplane from maintaining the published airspeed.
Probable cause:
The pilot did not maintain minimum controllable airspeed while on final approach with a partial loss of power in the right engine, which resulted in a loss of control. Contributing to the accident was the partial loss of engine power in the right engine due to the improperly installed o-rings in the engine’s throttle and control assembly.
Final Report:

Crash of a Piper PA-61 Aerostar (Ted Smith 601) in West Dover: 1 killed

Date & Time: Dec 2, 2006 at 1245 LT
Registration:
N9797Q
Flight Type:
Survivors:
No
Schedule:
White Plains – West Dover
MSN:
61-0432-160
YOM:
1977
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
14000
Captain / Total hours on type:
2600.00
Aircraft flight hours:
2953
Circumstances:
On the day of the accident, the pilot was returning to his home airport, after dropping off friends at a different airport. No weather briefing or flight plan was filed with Flight Service for either flight. A witness and radar data depicted the accident airplane on a straight-in approach for runway 1, in a landing configuration, at a ground speed of approximately 120 knots. The last radar target was recorded about 1/4 mile from the runway threshold, at an altitude of approximately 150 feet agl. The wreckage was later found about 1/2 mile east of the runway threshold. Review of weather information revealed general VFR conditions along the route of flight, and at reporting stations near the accident site. Gusty winds, low-level wind shear, and moderate to severe turbulence also prevailed at the time of the accident. In addition, weather radar depicted scattered light snow showers in the vicinity of the accident site, and possibly a snow squall. Examination of the wreckage did not reveal any preimpact mechanical malfunctions. The pilot had a total flight experience of 14,000 hours, with 8,500 hours in multiengine airplanes, including 2,600 hours in the same make and model as the accident airplane. He also had 4,100 hours of instrument flight experience.
Probable cause:
A loss of control during approach for undetermined reasons, which resulted in a collision with trees.
Final Report:

Crash of a Saab 340A in Washington DC

Date & Time: Jun 8, 2005 at 2137 LT
Type of aircraft:
Operator:
Registration:
N40SZ
Survivors:
Yes
Schedule:
White Plains – Washington DC
MSN:
40
YOM:
1985
Flight number:
UA7564
Crew on board:
3
Crew fatalities:
Pax on board:
27
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4673
Captain / Total hours on type:
3476.00
Copilot / Total flying hours:
2050
Copilot / Total hours on type:
620
Aircraft flight hours:
41441
Circumstances:
During the approach, the flightcrew was unable to get the right main landing gear extended and locked. After several attempts, while conferring with the checklist and company personnel, the flightcrew performed an emergency landing with the unsafe landing gear indication. During the landing, the right main landing gear slowly collapsed, and the airplane came to rest off the right side of the runway. Examination of the right main landing gear revealed that the retract actuator fitting was secured with two fasteners, a smaller bolt, and a larger bolt. The nut and cotter key were not recovered with the smaller bolt, and 8 of the 12 threads on the smaller bolt were stripped consistent with an overstress pulling of the nut away from the bolt. The larger bolt was bent and separated near the head, consistent with a tension and overstress separation as a result of the smaller bolt failure. The overstress failures were consistent with the right main landing gear not being locked in the extended position when aircraft weight was applied; however, examination of the right main landing gear down lock system could not determine any pre-impact mechanical malfunctions. Further, the right main landing gear retract actuator was tomography scanned, and no anomalies were noted. The unit was then functionally tested at the manufacturer's facility, under the supervision of an FAA inspector. The unit tested successfully, with no anomalies noted.
Probable cause:
Failure of the right main landing gear to extend and lock for undetermined reasons, which resulted in the right main landing gear collapsing during touchdown.
Final Report:

Crash of a Cessna 414 Chancellor off Port Jefferson

Date & Time: May 26, 2003 at 1428 LT
Type of aircraft:
Operator:
Registration:
N1234
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Orlando – White Plains
MSN:
414-0525
YOM:
1974
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1250
Aircraft flight hours:
4259
Circumstances:
The commercial pilot/owner was on a cross-country flight from Orlando, Florida, to Salisbury, Maryland, on an instrument flight rules (IFR) flight plan. The pilot stated that all five fuel tanks were topped off and verified as full before departure. The fueler, in a written statement, reported that he added 100 gallons of fuel and that the fuel tank levels were topped off. In addition to the main tanks, the airplane was equipped with two large-capacity auxiliary tanks (31.5 gallons of useable fuel each) and a locker tank, and the airplane's total useable fuel capacity was 183 gallons. As the airplane approached Maryland, the pilot requested weather for White Plains, New York (HPN) and then changed his destination to HPN. As he approached the New York area at 21,000 feet, air traffic control (ATC) instructed the pilot to fly a published arrival procedure and to maintain an altitude of 16,000 feet. The pilot stated that, due to poor weather and air traffic congestion, he became concerned about possible delays and informed ATC that he had "minimal fuel." He did not declare an emergency. ATC then issued the pilot a descent clearance, and he reduced both throttles to idle. In preparation to level off at the new altitude, the pilot increased power on both throttles, and the right engine stopped producing power. The pilot was unable to maintain the assigned altitude and told the controller that he had "lost an engine, and needed vectors to the nearest runway." The left engine stopped producing power about 2 minutes later. The pilot ditched the airplane and exited the airplane before it sank. The airplane was not recovered. The pilot reported that there were no mechanical problems with the airplane before the flight.
Probable cause:
Loss of power to both engines for undetermined reasons.
Final Report:

Crash of a Dassault Falcon 10 in White Plains

Date & Time: Jun 30, 1997
Type of aircraft:
Registration:
N10YJ
Survivors:
Yes
MSN:
57
YOM:
1975
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Aircraft flight hours:
6784
Circumstances:
On approach to White Plains-Westchester County Airport, the crew noted a left main gear unsafe light. The gear was recycled and the crew agreed with ATC to perform a low pass to check the gear. Few minutes later, upon landing, the left main gear collapsed. All four occupants escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
No investigations were conducted on this event.

Crash of a Beechcraft A100 King Air in North Adams: 1 killed

Date & Time: Aug 4, 1994 at 1605 LT
Type of aircraft:
Registration:
N7GA
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
North Adams – White Plains
MSN:
B-119
YOM:
1972
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
10200
Captain / Total hours on type:
106.00
Aircraft flight hours:
10426
Circumstances:
The airplane had undergone routine maintenance for slow acceleration on the right engine. Maintenance records revealed the fuel controls were changed from the right engine to the left engine. The airplane was released back to the pilot for service, and he departed for his home station. Several witnesses saw the airplane after takeoff at a low altitude, and at a slow speed. The airplane turned left, and the left wing struck the ground. Two witnesses saw the airplane pass by them at a low altitude, and wrote, '...at this point we could see the left (port) engine propeller was turning very slowly. You could actually see the individual blades of the propeller turning.' A complete disassembly of both engines, revealed no discrepancies other than impact, and post impact fire damage. Disassembly of the left propeller indicated that the propeller blades were at or near feather at impact. The pilot had a total of 106 flight hours in Beech A100 aircraft, all in the 90 days prior to the accident, and 56 hours in the 30 days prior to the accident.
Probable cause:
The pilot's failure to maintain minimum control speed after an undetermined loss of engine power, which resulted in an inadvertent stall at too low of an altitude to allow recovery.
Final Report:

Crash of a Piper PA-60-700P Aerostar in White Plains

Date & Time: Jul 12, 1994 at 0916 LT
Registration:
N323CB
Flight Phase:
Survivors:
Yes
Schedule:
White Plains – Elkhart
MSN:
60-8365-007
YOM:
1983
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1619
Captain / Total hours on type:
1033.00
Aircraft flight hours:
775
Circumstances:
During an aborted takeoff, the airplane overran the 4,451 foot long runway, went down a hill, and struck a fence. According to the pilot, 'during the takeoff roll, the indicated airspeed needle climbed to approximately 60 knots, but then would go no further... My attempts to dislodge it by tapping on the face of the gauge were futile...I pulled back the throttles and applied full brakes...' The pilot reported that based on the existing conditions 'the airplane can accelerate from rest to rotation speed and back to rest in less than 3,500 feet.' The examination of the airplane revealed the pitot tube was internally obstructed with an insect and mud.
Probable cause:
The pilot's delay in aborting the takeoff. A factor was internal obstruction of the pitot tube.
Final Report: