Crash of an ATR72-212 in Altamira

Date & Time: Feb 21, 2011 at 1845 LT
Type of aircraft:
Operator:
Registration:
PR-TTI
Survivors:
Yes
Schedule:
Belém - Altamira
MSN:
454
YOM:
1995
Flight number:
TIB5204
Location:
Country:
Crew on board:
4
Crew fatalities:
Pax on board:
47
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6000
Captain / Total hours on type:
2600.00
Copilot / Total flying hours:
1210
Copilot / Total hours on type:
50
Aircraft flight hours:
32886
Circumstances:
The aircraft departed Belém-Val de Cans Airport on a schedule service to Altamira with 47 passengers and 4 crew members on board. The approach for landing in Altamira was completed in VFR mode and the aircraft was stabilized. The touchdown on the runway was smooth, with gradual deceleration, in which only the 'ground idle' was used. After the '70 knots' callout, a strong noise was heard, and the left main gear collapsed with the aircraft deviating to the left. The aircraft veered off runway and came to rest in a grassy area. Among the 51 occupants, one passenger suffered minor injuries.
Probable cause:
The following findings were identified:
- The LEFT MAIN LANDING GEAR ASSEMBLY (PN D23189000-19 and SN MN1700) collapsed, failing with 5,130 cycles after the last overhaul.
- A specific component (pin) of the assembly connecting the landing gear to the airframe, the AFT PIVOT PIN (P / N D61000, S / N 25), broke on account of fatigue, whose onset was facilitated by a machining process carried out in the pin section transition region.
- The ANAC-approved ATR72 Series Aircraft Maintenance Program of the TRIP Linhas Aéreas company read that the LEFT MAIN LANDING GEAR ASSEMBLY had to undergo overhaul every eight years or 18,000 cycles.
- On 27 February 2009, the PR-TTI landing gear was removed and, on 09 March 2009, was sent to be overhauled by the AV Indústria Aeronáutica Ltda. It had 31,684 cycles since new and 18,095 cycles since the last overhaul.
- AV Indústria Aeronáutica Ltda. was homologated for conducting such inspection, as specified in the List attached to the Addendum, Revision no. 11, dated 05 January 2009, and accepted by means of the Official Document no. 0173/2009-GGAC/SAR, issued by the Civil Aviation Authority.
- The AV Indústria Aeronáutica Ltda. company disassembled the legs of the landing gear, and outsourced some of the tasks for not possessing technical knowledge and/or appropriate machinery (necessary for the process of reconditioning the AFT PIVOT PIN (D61000 SN 25).
- Two of the three companies outsourced by AV Indústria Aeronáutica Ltda. were not homologated by the Civil Aviation Authority.
- The AV Indústria Aeronáutica Ltda. company conducted external audits of the three companies involved in the overhaul.
- The audits carried out by AV Indústria Aeronáutica Ltda. were not sufficient to identify that the contractors lacked qualified personnel, manuals and the machinery necessary to work with aeronautical products.
- The AV Indústria Aeronáutica Ltda. Technical Manager did not supervise the overhaul inspections and services performed by the contracted companies.
- The AFT PIVOT PIN (D61000 SN 25) is part of the assembly that connects the landing gear to the airframe.
- All revision tasks were described in the manuals of the manufacturer.
- The AFT PIVOT PIN (D61000 SN 25) failure-analysis report stated that the PRTTI aircraft left main landing gear collapsed on account of fatigue, whose onset was facilitated by a machining process carried out in the section transition region of the pin.
- The manufacturer's maintenance manual did not refer to any machining work in that region of the pin.
- In only one stage of the pin reconditioning process was it possible to observe that a machining task was required, namely, the Grinding of chromium.
- The lack of capacitation and training of the subcontractors’ professionals for handling aircraft material hindered the execution of an efficient maintenance work as prescribed by the manufacturer's manual, culminating in inadequate machining during the maintenance process.
- The lack of an effective process of supervision, both on the part of TRIP Linhas Aéreas and on the part of the other contractors and subcontractors allowed the existing maintenance services’ latent failures not to be checked and corrected, in a way capable of subsidizing, in an adequate and safe manner, the execution of the landing gear maintenance service.
- The process of supervision of the TRIP Linhas Aéreas and the AV Indústria Aeronáutica Ltda. companies by the Civil Aviation Authority, prescribed by specific legislation in force, was not enough to mitigate the latent conditions present in the accident in question.
- According to the technical opinion issued by the DCTA, the AFT PIVOT PIN (D61000 and SN 25) presented fracture surfaces with ± 45º inclination, as well as a flat area with multiple initiations, indicative of a fracture mechanism related to fatigue. In examinations of the external surface of the pin, in a region close to the fatigue fracture, cracks were observed that had initiated from scratches created by an inadequate maintenance machining process. In the region where the overload-related fracture occurred, it was also possible to identify that the machining process had modified the profile of the part in the section transition region, by producing a depression. Thus, it can be said that the AFT PIVOT PIN (D61000 and SN 25) of the PR-TTI left main gear broke on account of fatigue, whose onset was facilitated by an inadequate machining process that had been performed in the section transition region of the pin.
Final Report:

Crash of a Learjet 24 in Pachuca de Soto: 2 killed

Date & Time: Feb 18, 2011 at 1104 LT
Type of aircraft:
Registration:
XB-GHO
Flight Type:
Survivors:
No
Schedule:
Pachuca de Soto - Pachuca de Soto
MSN:
24-141
YOM:
1967
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The crew was completing a local training flight at Pachuca de Soto Airport. After landing, the aircraft went out of control, veered off runway and eventually collided with a building housing a military canine unit, bursting into flames. The aircraft was destroyed and both pilots were killed.

Ground accident of a Boeing 747-368 in Madinah

Date & Time: Feb 16, 2011
Type of aircraft:
Operator:
Registration:
HZ-AIS
Survivors:
Yes
Schedule:
Riyadh - Madinah
MSN:
23270/645
YOM:
1986
Flight number:
SV817
Country:
Region:
Crew on board:
17
Crew fatalities:
Pax on board:
260
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
After landing at Madinah-Mohammad Bin Abdulaziz Airport runway 17, the crew completed the braking procedure and vacated via taxiway B. For unknown reasons, the aircraft departed the concrete zone and entered a sandy area, causing the left main gear to dug in and both left engines n°1 and 2 to struck the ground. All 277 occupants evacuated safely while the aircraft was damaged beyond repair.

Crash of a Swearingen SA227BC Metro III in Cork: 6 killed

Date & Time: Feb 10, 2011 at 0950 LT
Type of aircraft:
Operator:
Registration:
EC-ITP
Survivors:
Yes
Schedule:
Belfast – Cork
MSN:
BC-789B
YOM:
1992
Flight number:
NM7100
Location:
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
10
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
1801
Captain / Total hours on type:
1600.00
Copilot / Total flying hours:
539
Copilot / Total hours on type:
289
Aircraft flight hours:
32653
Aircraft flight cycles:
34156
Circumstances:
The aircraft departed Belfast City Airport (EGAC) on an international scheduled passenger service to Cork Airport (EICK). Low Visibility Procedures (LVP) were in operation at the destination. The aircraft carried out two ILS1 approaches, each followed by a missed approach. The aircraft then entered a holding pattern following which a third ILS approach was made to Runway (RWY) 17. The approach was continued below Decision Height (200 ft) and a missed approach was initiated. Approaching the runway threshold, the aircraft rolled to the left followed by a rapid roll to the right during which the right wingtip contacted the runway surface. The aircraft continued to roll and impacted the runway in a fully inverted position. The aircraft departed the runway surface to the right and came to rest in soft ground. A significant quantity of mud entered the aircraft through a fracture in the roof, partially filling the cabin. Six persons (including the two Flight Crew members) were fatally injured, four were seriously injured and two received minor injuries. The propeller blades on both engines were severely damaged; three of the four propeller blades on the right-hand engine detached during the impact sequence. Fire occurred in both engines after impact. These fires were extinguished expeditiously by the Airport Fire Service.
Probable cause:
Loss of control during an attempted go-around initiated below Decision Height (200 feet) in Instrument Meteorological Conditions.
The following factors were considered as significant:
- The approach was continued in conditions of poor visibility below those required.
- The descent was continued below the Decision Height without adequate visual reference being acquired.
- Uncoordinated operation of the flight and engine controls when go-around was attempted
- The engine power-levers were retarded below the normal in-flight operational range, an action prohibited in flight.
- A power difference between the engines became significant when the engine power levers were retarded below the normal in-flight range.
- Tiredness and fatigue on the part of the Flight Crew members.
- Inadequate command training and checking.
- Inappropriate pairing of Flight Crew members, and
- Inadequate oversight of the remote Operation by the Operator and the State of the Operator.
Final Report:

Crash of a Pilatus PC-12/47 off Plettenberg Bay: 9 killed

Date & Time: Feb 8, 2011 at 1633 LT
Type of aircraft:
Registration:
ZS-GAA
Survivors:
No
Schedule:
Queenstown - Plettenberg Bay
MSN:
858
YOM:
2007
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total flying hours:
2662
Captain / Total hours on type:
582.00
Copilot / Total flying hours:
351
Copilot / Total hours on type:
112
Aircraft flight hours:
1096
Circumstances:
The aircraft, which was operated under the provisions of Part 91 of the Civil Aviation Regulations (CARs), departed from Queenstown Aerodrome (FAQT) at 1329Z on an instrument flight plan for Plettenberg Bay Aerodrome (FAPG). On board the aircraft were two (2) crew members and seven (7) passengers. The estimated time of arrival for the aircraft to land at FAPG was 1430Z, however the aircraft never arrived at its intended destination, nor did the crew cancel their search and rescue as per flight plan/air navigation requirements. At ±1600Z an official search for the missing aircraft commenced. The search was coordinated by the Aeronautical Rescue Co-ordination Centre (ARCC). The first phase of the search, which was land based, was conducted in the Robberg Nature Reserve area. Progress was slow due to poor visibility associated with dense mist and night time. A sea search was not possible following activation of the official search during the late afternoon and night time, but vessels from the National Sea Rescue Institute (NSRI) were able to launch at first light the next morning. Floating debris (light weight material) was picked up from the sea and along the western shoreline of the Robberg Nature Reserve where foot patrols were conducted. On 11 February 2011 the South African Navy joined the search for the missing wreckage by utilizing side scan sonar equipment to scan the sea bed for the wreckage. All the occupants on board the aircraft were fatally injured in the accident.
Probable cause:
The aircraft crashed into the sea following a possible in flight upset associated with a loss of control during IMC conditions.
The following contributory factors were identified:
- Deviation from standard operating procedures by the crew not flying the published cloud-break procedure for runway 30 at FAPG, but instead opted to attempt to remain visual with the ground/sea (comply with VMC requirements) by descending over the sea and approaching the aerodrome from the southeast (Robberg Nature Reserve side).
- Inclement weather conditions prevailed in the area, which was below the minima to comply with the approved cloud-break procedure for runway 30 at FAPG (minimum safety altitude of 844 feet according to cloud-break procedure) as published at the time of the accident.
- Judgement and decision making lacking by the crew. (The crew continued from the seaward side with the approach during IMC conditions and not diverting to an alternative aerodrome with proper approach facilities timeously although a cell phone call in this regard indicate such an intention).
- The possibility that the pilot-flying at the time became spatially disorientated during the right turn while encountering / entering IMC conditions in an attempt to divert to FAGG should be regarded as a significant contributory factor to this accident.
- This was the first time as far as it could be determined that the two crew members flew together.
Final Report:

Crash of a Beechcraft B90 King Air in Harrisburg

Date & Time: Feb 8, 2011
Type of aircraft:
Registration:
N90BU
Flight Type:
Survivors:
Yes
MSN:
LJ-425
YOM:
1969
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
After landing at Harrisburg Airport, the undercarriage collapsed and the aircraft came to rest on its belly. Both occupants escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
The exact cause of the accident remains unknown as no investigation was completed by the NTSB.

Crash of a Beechcraft B200 Super King Air in Goiânia: 6 killed

Date & Time: Jan 14, 2011 at 1810 LT
Registration:
PR-ART
Survivors:
No
Site:
Schedule:
Brasília – Goiânia
MSN:
BB-806
YOM:
1981
Location:
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
2500
Captain / Total hours on type:
550.00
Circumstances:
Following an uneventful flight from Brasília, the pilot started the descent to Goiânia-Santa Genoveva Airport in poor weather visibility with heavy rain falls and turbulences. On final approach, the twin engine aircraft descended below the glide until it impact the slope of Mt Santo Antônio located 10,7 km short of runway 32. The aircraft was destroyed by impact forces and a post crash fire and all six occupants were killed.
Probable cause:
The following findings were identified:
- Factors, such as obesity and sedentariness, associated with the high workload in the moments preceding the collision with the hill, may have contributed for the task demand to exceed the margins of safety, resulting in wrong decision-making by the pilot.
- Upon facing adverse meteorological conditions and being aware that aircraft which landed before him had reached better visibility in altitudes below 3,500 ft. on the final approach of the VOR procedure, the pilot may have increased his level of confidence in the situation, to the point of descending even further, without considering the risks involved.
- The weather conditions encountered in the final phase of the flight may have aggravated the level of tension in the aircraft cabin to the point of compromising the management of the situation by the pilot, who delegated responsibility for radiotelephony communication to a passenger.
- If one considers that the pilot may have decided to descend below the minimum safe altitude in order to achieve visual conditions, one may suppose that his decision, probably influenced by the experience of the preceding aircraft, was made without adequate evaluation of the risks involved, and without considering the option of flying IFR, in face of the local meteorological conditions. In addition, the pilot’s decision-making process may have been compromised by lack of information on Mount Santo Antonio in the approach chart.
- The primary radar images obtained by Anápolis Control (APP-AN) indicated the presence of thick nebulosity associated with heavy cloud build-ups on the final approach of the VOR procedure. Such meteorological conditions influenced the occurrence, which culminated in the collision of the aircraft with Mount Santo Antônio, independently of the hypotheses raised during the investigation.
- The final approach on the course 320º, instead of 325º, made the aircraft align with the hill with which it collided.
- Mount Santo Antonio, a control obstacle on the final approach in which the collision occurred, was not depicted in the runway 32 VOR procedure approach chart, in discordance with the prescriptions of the CIRTRAF 100-30, a fact that may have contributed to a possible decrease of the situational awareness.
Final Report:

Crash of a Boeing 727-286 in Orūmīyeh: 78 killed

Date & Time: Jan 9, 2011 at 1945 LT
Type of aircraft:
Operator:
Registration:
EP-IRP
Survivors:
Yes
Schedule:
Tehran - Orumiyeh
MSN:
20945/1048
YOM:
1974
Flight number:
IR277
Country:
Region:
Crew on board:
9
Crew fatalities:
Pax on board:
96
Pax fatalities:
Other fatalities:
Total fatalities:
78
Aircraft flight hours:
9019
Circumstances:
The aircraft departed Tehran-Mehrabad Airport at 1815LT with a delay of more than two hours due to poor weather conditions at destination. While descending to Orūmīyeh Airport by night, the crew encountered poor weather conditions with snow falls, visibility 800 metres and three ceilings at 1,500, 2,000 and 6,000 feet. After the crew was unable to intercept the ILS, the decision to initiate a go-around procedure was taken. Approaching the stall speed, the stick shaker activated and the aircraft probably encountered icing conditions. In a left bank angle estimated between 26 and 40°, the engine n°3 and 1 failed. At an altitude of 600 feet and at a speed of 96 knots, the flaps were retracted, causing the aircraft to stall and to impact the ground. The aircraft broke in three but there was no fire. 70 passengers and 8 crew members were killed while 27 other occupants were injured, some seriously.
Probable cause:
Bad weather conditions for the aircraft and inappropriate actions by cockpit crew to confront the situation is the main cause of the accident. The following contributing factors were identified:
- The old technology of aircraft systems,
- Absence of a suitable simulator for adverse weather conditions,
- Failure to correctly follow the operating manual by the flight crew,
- Inadequate cockpit resources management (CRM).

Crash of a Learjet 35A in Springfield

Date & Time: Jan 6, 2011 at 1100 LT
Type of aircraft:
Operator:
Registration:
N800GP
Survivors:
Yes
Schedule:
Chicago - Springfield
MSN:
35A-158
YOM:
1978
Flight number:
PWA800
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5932
Captain / Total hours on type:
827.00
Aircraft flight hours:
16506
Circumstances:
The flight encountered light rime icing during an instrument approach to the destination airport. The copilot was the pilot flying at the time of the accident. He reported that the airframe anti-icing system was turned off upon intercepting the instrument approach glide slope, which was shortly before the airplane descended below the cloud layer. He recalled observing light frost on the outboard wing and tip tank during the approach. The stick shaker activated on short final, and the airplane impacted left of the runway centerline before it ultimately departed the right side of the runway pavement and crossed a slight rise before coming to rest in the grass. The cockpit voice recorder transcript indicated that the pilots were operating in icing conditions without the wing anti- ice system activated for about 4 1/2 minutes prior to activation of the stick shaker. A postaccident examination of the airplane did not reveal any anomalies consistent with a preimpact failure of the flight control system or a loss of anti-ice system functionality. A performance study determined that the airplane’s airspeed during the final 30 seconds of the flight was about 114 knots and that the angle of attack ultimately met the stick shaker threshold. The expected stall speed for the airplane was about 93 knots. The airplane flight manual stated that anti-ice systems should be turned on prior to operation in icing conditions during normal operations. The manual warned that even small accumulations of ice on the wing leading edge can cause an aerodynamic stall prior to activation of the stick shaker and/or stick pusher.
Probable cause:
The pilot’s decision to conduct an instrument approach in icing conditions without the anti-ice system activated, contrary to the airplane flight manual guidance, which resulted in an inadvertent aerodynamic stall due to an in-flight accumulation of airframe icing.
Final Report:

Crash of a Beechcraft E18S in New Stuyahok

Date & Time: Jan 3, 2011 at 1350 LT
Type of aircraft:
Operator:
Registration:
N9001
Flight Type:
Survivors:
Yes
Schedule:
Kenai - New Stuyahok
MSN:
BA-460
YOM:
1959
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6539
Captain / Total hours on type:
464.00
Aircraft flight hours:
19571
Circumstances:
The pilot reported that the runway at the destination airport was ice-covered, and that upon touchdown the surface was slicker than he had anticipated. He aborted the landing by applying full power to take off. The airplane was unable to out-climb the rising terrain at the end of the runway, and it collided with terrain, sustaining substantial damage to the fuselage and both wings. The pilot indicated that there were no mechanical issues with the airplane that precluded its normal operation.
Probable cause:
The pilot's misjudgment of the runway surface condition, resulting in an aborted landing and collision with rising terrain during the ensuing takeoff attempt.
Final Report: