Crash of a Lockheed 10A Electra in Anchorage

Date & Time: Dec 31, 1960
Type of aircraft:
Operator:
Registration:
N842
Flight Type:
Survivors:
Yes
MSN:
1030
YOM:
1935
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed in unknown circumstances in Anchorage. The exact date remain unknown. There were no injuries but the aircraft was damaged beyond repair.

Crash of an Aero Commander 520 in Bilbao: 1 killed

Date & Time: Dec 21, 1960
Operator:
Registration:
N2631B
Flight Type:
Survivors:
No
Schedule:
Madrid – Paris
MSN:
520-143
YOM:
1954
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The pilot, sole on board, was completing a flight from Madrid to Paris. While in cruising altitude, he encountered technical problems with an engine and requested the permission to divert to Bilbao-Sondica Airport. On final approach, following an uneventful descent, the airplane stalled and crashed 500 meters short of runway threshold. The aircraft, owned by S. Sehranger, was destroyed and the pilot was killed.

Crash of a Lockheed 18-56 LodeStar near Grants: 4 killed

Date & Time: Mar 22, 1958 at 0240 LT
Type of aircraft:
Operator:
Registration:
N300E
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Burbank – Tulsa – New York
MSN:
2312
YOM:
1942
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
7680
Captain / Total hours on type:
386.00
Copilot / Total flying hours:
4500
Copilot / Total hours on type:
3500
Aircraft flight hours:
3910
Circumstances:
The flight had made routine position reports from its assigned altitude of 11,000 feet until passing over Winslow, Arizona. Shortly after the last routine report at 11,000 feet a higher altitude was requested of Air Traffic Control because of encountering icing conditions. The request was granted and the aircraft reported, five minutes later, being at 13,000 feet between cloud layers. The last report was over Zuni, New Mexico, estimating Grants at 0249, 19 minutes later. Ten minutes after this report a ground explosion at an elevation of 7,200 feet m. s. 1. was observed by another flight and by ground witnesses. The wreckage of N300E was found in the area of the witnessed explosion. The right engine master rod bearing had failed in flight and the right propeller was feathered; however, complete loss of control followed and the aircraft struck the ground in a very steep angle of descent. As far as can be determined, there was no failure of the aircraft structure or controls prior to ground impact. The aircraft had anti-icing equipment installed and the pilots were experienced in Lodestar operation. There is evidence of the aircraft being considerably over its maximum allowable weight at departure and it is believed that the comparatively sudden failure of an engine at 13,000 feet created a situation, made more critical by virtue of the then existing weight, in which the pilot was unable to maintain control of the aircraft. All four occupants were killed, among them the American film producer Mike Todd, husband of Elizabeth Taylor, who was flying with his scenarist Art Cohn. The twin engine airplane was christened 'The Liz'.
Probable cause:
The Board determines that the probable cause of this accident was the loss of control of an overloaded aircraft following the failure of an engine at a cruising altitude which was critical for single-engine operation. The loss of control was aggravated by surface ice accretion.
Final Report:

Crash of a Lockheed 18-56-24 LodeStar in Marlborough: 1 killed

Date & Time: Nov 5, 1954 at 1942 LT
Type of aircraft:
Operator:
Registration:
N9201H
Flight Type:
Survivors:
Yes
Schedule:
LaGuardia – Boston
MSN:
2353
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
8700
Captain / Total hours on type:
200.00
Copilot / Total flying hours:
1600
Copilot / Total hours on type:
600
Aircraft flight hours:
1500
Circumstances:
At approximately 1845, N9201H departed LaGuardia Airport, New York, on a VFR (Visual Flight Rules) flight to Logan Airport, Boston, Massachusetts. The crew consisted of Captain John K. MacKenzie and Copilot Whitney H. Welch. The passengers were Robert W. Mudge, Raymond J. Halloran, both airline pilots, and Mathew C. Abbott, an electrical engineer. Climbing to an altitude of 3,500 feet m. s. l. (mean sea level), the flight proceeded toward Boston. Approximately 12 miles southeast of Hertford, Connecticut, the right engine became very rough and backfired frequently. The captain was unable to correct this condition and later feathered the right propeller when in the vicinity of Willimantic, Connecticut. A wide right turn was made from a northeasterly to a northwesterly heading toward Bradley Field, Windsor Locks, Connecticut. Communication was established with Bradley Field and the flight was cleared for a straight-in approach to runway 33. The aircraft descended to 2,500 feet m. s. l. during the turn and thereafter continued descending on a northwest heading until it struck trees and crashed. Nearby residents quickly reached the scene, gave assistance and notified authorities. The Bradley Field 1930 weather was: Scattered clouds at 4,500 feet, visibility 15 miles plus, temperature 40 degrees, dewpoint 32, wind northwest 6 m. p. h. La Guardia weather at the time of departure was: Ceiling unlimited, visibility 15 miles plus. Conditions en route were clear with excellent visibility. The twin engine airplane was the property of Mr. John Fox.
Probable cause:
The Board determines that the probable cause of this accident was that after failure of the right engine, accepted single-engine procedure was not followed, which resulted in the aircraft losing altitude and striking the ground. The following findings were reported:
- Weather was not a factor in the accident,
- A structural failure occurred in the power section of the right engine that necessitated feathering of the right propeller,
- Failure to attain single-engine performance resulted in loss of altitude,
- Mechanical difficulties in the left engine reduced power but remaining available power was sufficient for single-engine performance.
Final Report:

Crash of a Lockheed C-60A-1-LO LodeStar in Teterboro

Date & Time: Jan 5, 1954
Type of aircraft:
Operator:
Registration:
N3138
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
18-2262
YOM:
1942
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
At lift off, the right engine failed. The aircraft stalled and crashed. There were no casualties but the airplane owned by Walker P. Inman was destroyed by a post crash fire.
Probable cause:
Failure of the right engine during take off.

Crash of a Lockheed 10A Electra off Milwaukee

Date & Time: Dec 24, 1952
Type of aircraft:
Operator:
Registration:
N14981
Flight Type:
MSN:
1044
YOM:
1936
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed into Lake Michigan while on approach to Milwaukee Airport. The aircraft was lost but no information about the occupant.

Crash of a Curtiss C-46A-40-CU Commando in Miami: 4 killed

Date & Time: Aug 4, 1952 at 0030 LT
Type of aircraft:
Operator:
Registration:
N79096
Flight Type:
Survivors:
No
Schedule:
Burbank – San Antonio – Miami
MSN:
27038
YOM:
1944
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
5823
Captain / Total hours on type:
1412.00
Circumstances:
The aircraft departed Burbank August 3 on a nonstop ferry flight to San Antonio, Texas. The aircraft, piloted by Douglas T. Dell, Chief Pilot of Resort Airlines, arrived at its destination at 2345 following an uneventful flight VFR direct. Two minor discrepancies were reported by the pilot on arrival at San Antonio; that the hydraulic system cycle every one minute and 20 seconds, and that the left engine dropped 100 RPM'S on the left magneto. These discrepancies were corrected y Slick Airways' maintenance crew at San Antonio, and at 1653, August 4, the aircraft departed for Miami, Florida, nonstop on a VFR flight plan to cruise at 10,000 feet. The crew on this flight consisted of Captain Robert E. Smith and Copilot John N. Goodman. Two non revenue passengers boarded the plane at San Antonio for the flight to Miami. The cabin of the aircraft contained no passenger seats. This equipment was to have been installed at Miami prior to placing the aircraft in service. The cockpit was equipped to accommodate a crew of three. One safety belt had been installed to accommodate one person riding in the cabin; however, no approved type seat was provided. The aircraft and engine log covering the flight from San Antonio to Miami, as well as a mutilated flight plan and log sheet recovered from the wreckage, indicated that the flight was made at an altitude of 10,000 feet. All entries in the flight plan and log sheet covering check points between San Antonio and Miami were completed up to and including Cross City, Florida, the last check point before reaching Miami. The last entry gave the estimated time of arrival at Miami as 2324. The estimated and actual time over the various cheek points along the route as reflected in the flight log indicated that the flight had progressed very nearly as estimated. On the recovered aircraft and engine log covering the San Antonio-Miami flight under heading entitled "Difficulties Noted During Flight," there was found this entry, "EXCESSIVE PLAY ON ELE." The log sheet had been signed by both the captain and the copilot. At approximately 2317 the Miami tower operator received a broken radio transmission from which he was unable to identify either the aircraft or the nature of the call. An attempt to establish contact was unsuccessful until the following message was received. "Miami tower - NAN 79096 requesting emergency landing." Two-way contact was established and at approximately 2318 the flight was cleared to land on Runway 27L (preferential runway for calm wind) and the pilot was advised that if this runway was not satisfactory any runway was available. In the next transmission, the pilot advised the tower that the elevator control linkage was broken and he would attempt to bring the aircraft in, using trim tabs only. His position was given as high over the west boundary of the airport at an altitude estimated by the tower operator as 3,000 feet. Since the use of Runway 9R would permit an approach to be made over very thinly populated areas, it was suggested to the pilot that if it was satisfactory with him, Runway 9R be used. The pilot advised the tower that the change of runways was satisfactory. The area was cleared of all traffic while the aircraft made a circuit of the field, letting down slowly with a wide approach to a long final. As the aircraft neared the approach end of the runway, it appeared to tower personnel to be lined up properly. The following is quoted from testimony of the tower operator: "As the aircraft neared the approach end of the runway and at an altitude of approximately 150 feet, the nose of the aircraft appeared to come up slightly, then crop about the same degree below the horizon. This was repeated several times, each time two maneuver becoming more violent, with the last pull-up very stoop. At an altitude of approximately 150 feet the aircraft appeared to fall off slightly on the left wing, the nose dropped, and the aircraft struck the ground almost vertically." The fire which followed the crash was quickly extinguished by the airport fire-fighting equipment, the crews of which had been altered and were in standby position prior to the crash. The aircraft was destroyed and all four occupants were killed.
Probable cause:
The Board finds that the probable cause of this accident was failure of the elevator control system in flight, resulting in loss of control of the aircraft during landing. The failure of the elevator control system was the result of poor workmanship and inadequate inspection during overhaul and modification. The following findings were pointed out:
- Weather was not considered a factor in this accident,
- Total flight time on the aircraft since overhaul and modification was approximately 13 hours 27 minutes,
- At 2318 the flight advised the Miami tower that the elevator control linkage was broken and elevators functioning by use of trim tabs only,
- The aircraft became uncontrollable and crashed during an attempted landing on Runway 09R,
- The push-pull tube was found disconnected from its point of attachment on the elevator bellerrank.
Final Report:

Crash of a Lockheed 18-56 LodeStar in Cedar Grove

Date & Time: Jan 28, 1952
Type of aircraft:
Operator:
Registration:
N94538
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
2095
YOM:
1941
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The pilot, sole on board, was completing a ferry flight from Kenya to the US with intermediate stops in Prestwick, Iceland and Canada. While approaching an airport located in the region of New York in snow falls, the airplane crash landed in a golf course and was damaged beyond repair. The pilot was unhurt.

Crash of a Douglas B-23 Dragon in Mount Shasta

Date & Time: Oct 20, 1951
Type of aircraft:
Operator:
Registration:
NC44890
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
2746
YOM:
1944
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed in flames in a dirt field located near Mount Shasta. All four occupants escaped uninjured while the aircraft was destroyed by a post crash fire. It was the property of Howard Hughes.

Crash of a Grumman G-73 Mallard in Columbus: 1 killed

Date & Time: Sep 30, 1950
Type of aircraft:
Operator:
Registration:
N74044
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
J-46
YOM:
1949
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
Crashed on takeoff at Columbus Southwest Airfield. The aircraft was destroyed by a post crash fire and the pilot died from burns. All three passengers were injured. Owned by John W. Galbreath, President of the Pittsburgh Pirates, the aircraft was carrying Joe Williams, New York sports columnist, Lester Scott, Director of the New York Knickerbockers of the National Basketball Association and Paul Jonas, Manager of the sports department of Mutual Broadcasting system. The aircraft was host to these three men at the Ohio State-Southern Methodist football game.