Crash of a Cessna 441 Conquest II in Renmark: 3 killed

Date & Time: May 30, 2017 at 1630 LT
Type of aircraft:
Operator:
Registration:
VH-XMJ
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Renmark - Adelaide
MSN:
441-0113
YOM:
1980
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
14751
Captain / Total hours on type:
987.00
Copilot / Total flying hours:
5000
Copilot / Total hours on type:
1000
Aircraft flight hours:
13845
Circumstances:
On 30 May 2017, a Cessna 441 Conquest II (Cessna 441), registered VH-XMJ (XMJ) and operated by AE Charter, trading as Rossair, departed Adelaide Airport, South Australia for a return flight via Renmark Airport, South Australia. On board the aircraft were:
• an inductee pilot undergoing a proficiency check, flying from the front left control seat
• the chief pilot conducting the proficiency check, and under assessment for the company training and checking role for Cessna 441 aircraft, seated in the front right control seat
• a Civil Aviation Safety Authority flying operations inspector (FOI), observing and assessing the flight from the first passenger seat directly behind the left hand pilot seat.
Each pilot was qualified to operate the aircraft. There were two purposes for the flight. The primary purpose was for the FOI to observe the chief pilot conducting an operational proficiency check (OPC), for the purposes of issuing him with a check pilot approval on the company’s Cessna 441 aircraft. The second purpose was for the inductee pilot, who had worked for Rossair previously, to complete an OPC as part of his return to line operations for the company. The three pilots reportedly started their pre-flight briefing at around 1300 Central Standard Time. There were two parts of the briefing – the FOI’s briefing to the chief pilot, and the chief pilot’s briefing to the inductee pilot. As the FOI was not occupying a control seat, he was monitoring and assessing the performance of the chief pilot in the conduct of the OPC. There were two distinct exercises listed for the flight (see the section titled Check flight sequences). Flight exercise 1 detailed that the inductee pilot was to conduct an instrument departure from Adelaide Airport, holding pattern and single engine RNAV2 approach, go around and landing at Renmark Airport. Flight exercise 2 included a normal take-off from Renmark Airport, simulated engine failure after take-off, and a two engine instrument approach on return to Adelaide. The aircraft departed from Adelaide at 1524, climbed to an altitude about 17,000 ft above mean sea level, and was cleared by air traffic control (ATC) to track to waypoint RENWB, which was the commencement of the Renmark runway 073 RNAV-Z GNSS approach. The pilot of XMJ was then cleared to descend, and notified ATC that they intended to carry out airwork in the Renmark area. The pilot further advised that they would call ATC again on the completion of the airwork, or at the latest by 1615. No further transmissions from XMJ were recorded on the area frequency and the aircraft left surveillance coverage as it descended towards waypoint RENWB. The common traffic advisory frequency used for air-to-air communications in the vicinity of Renmark Airport recorded several further transmissions from XMJ as the crew conducted practice holding patterns, and a practice runway 07 RNAV GNSS approach. Voice analysis confirmed that the inductee pilot made the radio transmissions, as expected for the check flight. At the completion of the approach, the aircraft circled for the opposite runway and landed on runway 25, before backtracking and lining up for departure. That sequence varied from the planned exercise in that no single-engine go-around was conducted prior to landing at Renmark. At 1614, the common traffic advisory frequency recorded a transmission from the pilot of XMJ stating that they would shortly depart Renmark using runway 25 to conduct further airwork in the circuit area of the runway. A witness at the airport reported that, prior to the take-off roll, the aircraft was briefly held stationary in the lined-up position with the engines operating at significant power. The take-off roll was described as normal however, and the witness looked away before the aircraft became airborne. The aircraft maintained the runway heading until reaching a height of between 300-400 ft above the ground (see the section titled Recorded flight data). At that point the aircraft began veering to the right of the extended runway centreline (Figures 1 and 15). The aircraft continued to climb to about 600 ft above the ground (700 ft altitude), and held this height for about 30 seconds, followed by a descent to about 500 ft (Figures 2 and 13). The information ceased 5 seconds later, which was about 60 seconds after take-off. A distress beacon broadcast was received by the Joint Rescue Coordination Centre and passed on to ATC at 1625. Following an air and ground search the aircraft was located by a ground party at 1856 about 4 km west of Renmark Airport. All on board were fatally injured and the aircraft was destroyed.
Probable cause:
Findings:
From the evidence available, the following findings are made with respect to the collision with terrain involving Cessna 441, registered VH-XMJ, that occurred 4 km west of Renmark Airport,
South Australia on 30 May 2017. These findings should not be read as apportioning blame or liability to any particular organisation or individual.
Contributing factors:
• Following a planned simulated engine failure after take-off, the aircraft did not achieve the expected single engine climb performance, or target airspeed, over the final 30 seconds of the flight.
• The exercise was not discontinued when the aircraft’s single engine performance and airspeed were not attained. That was probably because the degraded aircraft performance, or the
associated risk, were not recognised by the pilots occupying the control seats.
• It is likely that the method of simulating the engine failure and pilot control inputs, together or in isolation, led to reduced single engine aircraft performance and asymmetric loss of control.
• Not following the recommended procedure for simulating an engine failure in the Cessna 441 pilot’s operating handbook meant that there was insufficient height to recover following the loss of control.
Other factors that increased risk:
• The Rossair training and checking manual procedure for a simulated engine failure in a turboprop aircraft was inappropriate and, if followed, increased the risk of asymmetric control loss.
• The flying operations inspector was not in a control seat and did not share a communication systems with the crew. Consequently, he had reduced ability to actively monitor the flight and
communicate any identified performance degradation.
• The inductee pilot had limited recent experience in the Cessna 441, and the chief pilot had an extended time period between being training and being tested as a check pilot on this aircraft. While both pilots performed the same exercise during a practice flight the week before, it is probable that these two factors led to a degradation in the skills required to safely perform and monitor the simulated engine failure exercise.
• The chief pilot and other key operational managers within Rossair were experiencing high levels of workload and pressure during the months leading up to the accident.
• In the 5 years leading up to the accident, the Civil Aviation Safety Authority had conducted numerous regulatory service tasks for the air transport operator and had regular communication with the operator’s chief pilots and other personnel. However, it had not conducted a systemic or detailed audit during that period, and its focus on a largely informal and often undocumented approach to oversight increased the risk that organisational or systemic issues associated with the operator would not be effectively identified and addressed.
Other findings:
• A lack of recorded data from this aircraft reduced the available evidence about handling aspects and cockpit communications. This limited the extent to which potential factors contributing to the accident could be analysed.
Final Report:

Crash of an Antonov AN-26 in Balashov: 1 killed

Date & Time: May 30, 2017 at 0640 LT
Type of aircraft:
Operator:
Registration:
RF-36160
Flight Type:
Survivors:
Yes
Schedule:
Balashov - Balashov
MSN:
80 01
YOM:
1979
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The crew was performing a local training mission at Balashov Airport, in the region of Saratov. Following several touch-and-go manoeuvres, the crew initiated a new approach. On final, the airplane descended below the MDA and, at a speed of 240 km/h, rolled to the right to an angle of 24°, stalled and crashed in a field located 1,100 metres from the airfield, bursting into flames. Five occupants were injures while a pilot under supervision was killed. The airplane had the dual registration RF-36160 and 79 red.
Crew:
Cpt Y. Tereshin,
Maj S. Rodionov,
Ens Frolov,
P. Halaimov,
I. Makhmoudov,
M. Artemiev. †
Probable cause:
It was determined that during the approach, the instructor led the aircraft descending below MDA when he simulated an engine failure and positioned both power levers to idle. As a result of the failure of the propeller feathering system, the right engine stopped. After 14 seconds, the instructor mistakenly shut down the left engine that was running properly, causing the aircraft to lose speed, to stall and to crash.

Crash of an Antonov AN-26 near San Cristóbal: 8 killed

Date & Time: Apr 29, 2017
Type of aircraft:
Operator:
Registration:
CU-T1406
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Playa Baracoa - Playa Baracoa
MSN:
135 02
YOM:
1985
Flight number:
FAR1436
Country:
Crew on board:
8
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
8
Circumstances:
The airplane departed Playa Baracoa Airport at 0638LT on a training flight and continued to the southwest. En route, it impacted the slope of Mt Loma de la Pimienta located about six km north of San Cristóbal, province of Artemisa. The aircraft was destroyed and all eight crew members were killed. Owned by Aerogaviota, the airplane was operated by the Cuban Air Force (Fuerzas Armadas Revolucionarias) under flight code FAR1436.

Crash of a Pilatus U-28A at Cannon AFB: 3 killed

Date & Time: Mar 14, 2017 at 1835 LT
Type of aircraft:
Operator:
Registration:
08-0724
Flight Type:
Survivors:
No
Schedule:
Cannon - Cannon
MSN:
724
YOM:
2006
Flight number:
Demise 25
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
3400
Captain / Total hours on type:
3199.00
Copilot / Total flying hours:
448
Copilot / Total hours on type:
213
Circumstances:
On 14 Mar 17, at 1835 local time (L), a U-28A, tail number 0724, crashed one-quarter mile south of Clovis Municipal Airport (KCVN), New Mexico (NM). This aircraft was operated by the 318th Special Operations Squadron, 27th Special Operations Wing, Cannon Air Force Base (AFB), NM. The aircraft was destroyed and all three crewmembers died upon impact. The Mishap Aircraft (MA) departed Cannon AFB at 1512L for tactical training over Lubbock, Texas, followed by pilot proficiency training at KCVN. The Mishap Crew (MC) entered Lubbock airspace at 1545L, completed their tactical training, and departed Lubbock airspace at 1735L enroute to KCVN. The MC entered the KCVN traffic pattern at 1806L, where they conducted multiple approaches and landings prior to executing the mishap maneuver, a practice turnback Emergency Landing Pattern (ELP). The MC entered the practice turnback ELP with 0° flaps led to increased aircraft nose-down attitudes and higher descent rates required to maintain a safe angle of attack versus a comparative 15° flap approach. In addition, 0° flap stall speeds are higher than 15° flap stall speeds – 15 to 25 knots higher for the range of bank angles flown by the MC during the practice turnback ELP. The MC was also late to achieve the bank angle required to enable the MA to align with the extended centerline for the runway resulting in an overshoot condition. The MC attempted to arrest their excessive nose-down attitude, descent rate, and shallow bank angle by pulling back on the aircraft yoke and increasing bank angle. The g-load from the MC pull back, coupled with the MA's increased bank angle, slowed the MA airspeed below 0° flap stall speed and it departed controlled flight. Subsequent power increase and flight control inputs would not have enabled the aircraft to recover from the stall within remaining altitude. After entering the stall, the MC increased power; however, it was not enough to overcome the MA descent rate. At no point during the practice turnback ELP did the MA performance reflect a MC intent to abort the maneuver. The MA impacted the ground with a 13° nose-high, 7° left-wing low attitude. The aircraft was destroyed upon impact and all three occupants were killed.
Crew:
Cpt Andrew Becker, pilot,
1st Lt Frederick Dellecker, copilot,
Cpt Kenneth Dalga, combat systems officer.
Probable cause:
By a preponderance of the evidence, the Accident Investigation Board concluded the aircrew lost control of the aircraft when it entered a stall at low altitude during a turn back Emergency Landing Pattern procedure. There were no indications of mechanical malfunction. The board also surmised the crew delayed actions necessary to prevent the aircraft from entering the stall envelope and failed to accurately assess increasing risk throughout execution of the practice turn back Emergency Landing Pattern, thereby substantially contributing to the mishap.
Final Report:

Crash of a Beechcraft B60 Duke in Duette: 2 killed

Date & Time: Mar 4, 2017 at 1330 LT
Type of aircraft:
Registration:
N39AG
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Sarasota - Sarasota
MSN:
P-425
YOM:
1977
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1120
Captain / Total hours on type:
200.00
Copilot / Total flying hours:
20900
Copilot / Total hours on type:
165
Aircraft flight hours:
3271
Circumstances:
The private pilot, who had recently purchased the airplane, and the flight instructor were conducting an instructional flight in the multi-engine airplane to meet insurance requirements. Radar data for the accident flight, which occurred on the second day of 2 days of training, showed the airplane maneuvering between 1,000 ft and 1,200 ft above ground level (agl) just before the accident. The witness descriptions of the accident were consistent with the airplane transitioning from slow flight into a stall that developed into a spin from which the pilots were unable to recover before the airplane impacted terrain. Examination of the wreckage did not reveal evidence of any preexisting mechanical malfunctions or anomalies that would have precluded normal operation of the airplane. After the first day of training, the pilot told friends and fellow pilots that the instructor provided non-standard training that included stall practice that required emergency recoveries at low airspeed and low altitude. The instructor used techniques that were not in keeping with established flight training standards and were not what would be expected from an individual with his extensive background in general aviation flight instruction. Most critically, the instructor used two techniques that introduced unnecessary risk: increasing power before reducing the angle of attack during a stall recovery and introducing asymmetric power while recovering from a stall in a multi-engine airplane; both techniques are dangerous errors because they can lead to an airplane entering a spin. At one point during the first day of training, the airplane entered a full stall and spun before control was regained at very low altitude. The procedures performed contradicted standard practice and Federal Aviation Administration guidance; yet, despite the pilot's experience in multi-engine airplanes and in the accident airplane make and model, he chose to continue the second day of training with the instructor instead of seeking a replacement to complete the insurance check out. The spin encountered on the accident flight likely resulted from the stall recovery errors advocated by the instructor and practiced on the prior day's flight. Unlike the previous flight, the accident flight did not have sufficient altitude for recovery because of the low altitude it was operating at, which was below the safe altitude required for stall training (one which allows recovery no lower than 3,000 ft agl).
Probable cause:
The pilots' decision to perform flight training maneuvers at low airspeed at an altitude that was insufficient for stall recovery. Contributing to the accident was the flight instructor's inappropriate use of non-standard stall recovery techniques.
Final Report:

Crash of a Beechcraft B200T Super King Air at Butterworth AFB: 1 killed

Date & Time: Dec 21, 2016 at 1718 LT
Operator:
Registration:
M41-03
Flight Type:
Survivors:
Yes
Schedule:
Kuala Lumpur – Butterworth
MSN:
BT-37
YOM:
1993
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The crew was completing a training flight from Kuala Lumpur-Subang Airport when on final approach to Butterworth Airbase, the twin engine aircraft went out of control and crashed, coming to rest against the perimeter fence. The aircraft was partially destroyed by impact forces and one crew member was killed while three other occupants were injured. Weather conditions were considered as good at the time of the accident.

Crash of a Beechcraft 200 Super King Air in Iqaluit

Date & Time: Jul 17, 2016 at 1217 LT
Operator:
Registration:
C-FCGW
Flight Type:
Survivors:
Yes
Schedule:
Iqaluit - Iqaluit
MSN:
BB-207
YOM:
1977
Flight number:
BFF200
Location:
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
A Beech 200 Super King Air aircraft operated by Air Nunavut as flight 200, was on a training flight at Iqaluit, NU (CYFB) to upgrade a candidate to captain status. A VFR circuit was executed to simulate a flapless landing. While in the circuit, the crew experienced an actual communication failure on COM 1 while two other aircraft were inbound to Iqaluit. At the end of the downwind leg, a flap failure was simulated and the crew carried out the appropriate checklist. However, the landing checklist was not completed and the aircraft landed with the landing gear in the up position on runway 16. The aircraft skidded on the belly and came to a stop on the runway between taxiway A and G. The crew declared an emergency and evacuated the airplane with no injuries. The aircraft sustained damage to the belly pod and both propellers.

Crash of a Lockheed C-130H Hercules at Montijo AFB: 3 killed

Date & Time: Jul 11, 2016 at 1200 LT
Type of aircraft:
Operator:
Registration:
16804
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Montijo AFB - Montijo AFB
MSN:
4777
YOM:
1978
Country:
Region:
Crew on board:
7
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
The crew was completing a local training exercise at Montijo AFB, consisting of touch-and-go maneuvers. During the takeoff roll on runway 26, the four engine aircraft deviated from the centerline to the left then went out of control, veered off runway to the right and eventually crashed 1,460 meters past the runway threshold, bursting into flames. Four crew members were injured while three others were killed. The aircraft was destroyed by a post crash fire.

Crash of a Swearingen SA226T Merlin IIIB in Farmingdale

Date & Time: Jun 20, 2016 at 1758 LT
Operator:
Registration:
N127WD
Flight Type:
Survivors:
Yes
Schedule:
White Plains - Farmingdale
MSN:
T-297
YOM:
1978
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
11450
Captain / Total hours on type:
410.00
Copilot / Total flying hours:
1300
Copilot / Total hours on type:
5
Aircraft flight hours:
4500
Circumstances:
According to the pilot in command (PIC), he was conducting an instructional flight for his "new SIC (second in command)," who was seated in the left seat. He reported that they had flown two previous legs in the retractable landing gear-equipped airplane. He recalled that, during the approach, they discussed the events of their previous flights and had complied with the airport control tower's request to "keep our speed up." During the approach, he called for full flaps and retarded the throttle to flight idle. The PIC asserted that there was no indication that the landing gear was not extended because he did not hear a landing gear warning horn; however, he was wearing a noise-cancelling headset. He added that the landing gear position lights were not visible because the SIC's knee obstructed his view of the lights. He recalled that, following the flare, he heard the propellers hit the runway and that he made the decision not to go around because of unknown damage sustained to the propellers. The airplane touched down and slid to a stop on the runway. The airplane sustained substantial damage to the fuselage bulkheads, longerons, and stringers. The SIC reported that the flight was a training flight in visual flight rules conditions. He noted that the airspace was busy and that, during the approach, he applied full flaps, but they failed to extend the landing gear. He added that he did not hear the landing gear warning horn; however, he was wearing a noise-cancelling headset. The Federal Aviation Administration Aviation Safety Inspector that examined the wreckage reported that, during recovery, the pilot extended the nose landing gear via the normal extension process. However, due to significant damage to the main landing gear (MLG) doors, the MLG was unable to be extended hydraulically or manually. He added that an operational check of the landing gear warning horn was not accomplished because the wreckage was unsafe to enter after it was removed from the runway. The landing gear warning horn was presented by an aural tone in the cockpit and was not configured to be heard through the pilots' noise-cancelling headsets. When asked, the PIC and the SIC both stated that they could not remember who read the airplane flight manual Before Landing checklist.
Probable cause:
The pilot-in-command's failure to extend the landing gear before landing and his failure to use the Before Landing checklist. Contributing to the accident was the pilots' failure to maintain a sterile cockpit during landing.
Final Report:

Crash of a PZL-Mielec AN-2R in San Bernardino

Date & Time: May 6, 2016 at 1200 LT
Type of aircraft:
Operator:
Registration:
N2AN
Flight Type:
Survivors:
Yes
Schedule:
Upland - San Bernardino
MSN:
1G210-55
YOM:
1985
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3350
Captain / Total hours on type:
58.00
Aircraft flight hours:
2924
Circumstances:
The commercial pilot was entering the airport traffic pattern for landing during a familiarization flight. He reported that he turned on the carburetor heat, switched the fuel tank selector to the right fuel tank, and shortly thereafter, the engine experienced a total loss of power. The pilot attempted numerous times to restart the engine but was unsuccessful. After realizing that he would not be able to reach the runway, he decided to make a forced landing to a small field. During the landing approach, the airplane contacted a power line, nosed over, and came to rest inverted, resulting in substantial damage to the wings and fuselage. During the postaccident examination of the airplane, about 16 ounces of water were removed from the fuel system. Water was present in the lower gascolator, the fine fuel filter (upper gascolator), and subsequent fuel line to the carburetor inlet. A brass screen at the carburetor inlet and 2 carburetor fuel bowl thumb screens also contained corrosion, water, and rust. The approved aircraft inspection checklist called for washing the carburetor and main fuel filter every 50 hours and cleaning and/or replacing the fine fuel filter every 100 hours. The fine fuel filter is not easily accessible and not able to be drained during a preflight inspection. The mechanic who completed the most recent inspection stated that he did not drain or check the fine fuel filter. The last logbook entry that specifically stated the fuel filters were cleaned was about 4 years before the accident.
Probable cause:
The mechanic's failure to inspect the fine fuel filter gascolator as required during the most recent inspection, which resulted in a total loss of engine power due to fuel contamination.
Final Report: