Crash of a Cessna 402C off Halfmoon Bay: 5 killed

Date & Time: Aug 19, 1998 at 1643 LT
Type of aircraft:
Operator:
Registration:
ZK-VAC
Flight Phase:
Survivors:
Yes
Schedule:
Halfmoon Bay - Invercargill
MSN:
402C-0512
YOM:
1981
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
14564
Captain / Total hours on type:
27.00
Aircraft flight hours:
13472
Circumstances:
Surviving passengers reported that en route from Stewart Island to Invercargill there were symptoms of a righthand engine failure, which was corrected by the pilot's manipulation of floor-mounted fuel tank selectors. Shortly afterwards, both engines stopped. The pilot broadcast a Mayday and advised the passengers that they would be ditching. A successful ditching was carried out approximately 12 NM south of Invercargill. All occupants escaped from the aircraft, however, four persons exited without life jackets. The pilot entered the cabin but was unable to locate more before the aircraft sank. Rescuers reached the scene about an hour after the ditching only to find that all those without life jackets had perished, as had a young boy who was wearing one.
Probable cause:
A TAIC investigation found that there was no evidence of any component malfunction that could cause a double engine failure, although due to seawater damage the pre-impact condition of most fuel quantity system components could not be verified. Both fuel tank selectors were positioned to the lefthand tank, and it is probable that fuel starvation was the cause of the double engine failure. Company procedures for the Cessna 402 lacked a fuel quantity monitoring system to supplement fuel gauge indications. Dipping of the tanks was not a feasible option. Company pilots believed that the aircraft was fitted with low-fuel quantity warning lights, which was not the case. As three pilots believed the gauges indicated sufficient fuel was on board before the preceding round trip to the island, exhaustion may have followed an undetermined fuel indicating system malfunction. The failure of the company to require the use of operational flight logs, and other deficiencies in record keeping, were identified in the TAIC report. The much-publicised misunderstanding about the ditching location was not considered by the TAIC report to have affected the outcome of the rescue, but provides an example of the continued importance of using the phonetic alphabet in radiotelephony. A safety recommendation that operators use a fuel-quantity monitoring system to supplement fuel gauge indications was also made by the TAIC report.
Final Report:

Crash of a PZL-Mielec AN-2R in Yakutia

Date & Time: Aug 14, 1998
Type of aircraft:
Operator:
Registration:
RA-40681
Flight Phase:
MSN:
1G214-39
YOM:
1985
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed in unknown circumstances in a river bed somewhere in Yakutia. Occupant's fate unknown.

Crash of a Yakovlev Yak-40 in Jalal-Abad

Date & Time: Aug 14, 1998
Type of aircraft:
Operator:
Registration:
EX-87529
Survivors:
Yes
MSN:
9 52 11 41
YOM:
1975
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
After landing at Jalal-Abad Airport, the aircraft was unable to stop within the remaining distance. It overran, lost its undercarriage and came to rest. There were no casualties but the aircraft was damaged beyond repair.

Crash of a Boeing 747-4B5 in Seoul

Date & Time: Aug 5, 1998 at 2201 LT
Type of aircraft:
Operator:
Registration:
HL7496
Survivors:
Yes
Schedule:
Tokyo - Jeju - Seoul
MSN:
26400
YOM:
1996
Flight number:
KE8702
Country:
Region:
Crew on board:
16
Crew fatalities:
Pax on board:
379
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Originally, the flight was a direct one from Tokyo-Narita to Seoul but due to poor weather conditions at destination, the crew diverted to Jeju. The aircraft departed Jeju Airport at 2107LT on the final leg to Seoul-Gimpo Airport. At destination, weather conditions were still poor with heavy rain falls and wind from 220 gusting to 22 knots. After touchdown on runway 14R, the crew started the braking procedure but the aircraft deviated to the right and veered off runway. While contacting soft ground, the aircraft lost its undercarriage and came to rest. All 395 occupants evacuated, among them 20 were slightly injured. The aircraft was damaged beyond repair.
Probable cause:
It was determined that the loss of control after touchdown was the consequence of the captain's misuse of the thrust reverser during the landing roll and his confusion over crosswind conditions. Investigations revealed that after touchdown, the n°1 engine thrust reverser did not deploy because the n°1 engine power lever's position did not allow the reverser to be deployed. The following contributing factors were identified:
- Poor weather conditions,
- Cross wind component,
- Wet runway surface,
- Poor braking action.

Crash of a Beechcraft 1900D off Quiberon: 14 killed

Date & Time: Jul 30, 1998 at 1558 LT
Type of aircraft:
Operator:
Registration:
F-GSJM
Flight Phase:
Survivors:
No
Schedule:
Lyon - Lorient
MSN:
UE-238
YOM:
1996
Flight number:
PRB706
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
12
Pax fatalities:
Other fatalities:
Total fatalities:
14
Captain / Total flying hours:
3072
Captain / Total hours on type:
1356.00
Copilot / Total flying hours:
1016
Copilot / Total hours on type:
361
Aircraft flight hours:
3342
Circumstances:
Following an uneventful flight from Lyon-Satolas Airport, the crew was approaching Lorient-Lann-Bihoué Airport when he contacted ATC and requested a special clearance to cancel his IFR flight plan for a visual circuit over the Bay of Quiberon to show the 'Norway' ship (ex France) to the passengers. While cruising under VFR mode in excellent weather conditions at an altitude of 2,000 feet, the twin engine aircraft collided with a private Cessna 177 Cardinal registered F-GAJE and owned by the Aéro Club de Vannes. Following the collision, both aircraft entered an uncontrolled descent and crashed in the Bay of Quiberon about 1,500 metres from the ship and 10 km off Quiberon. All 14 people on board the Beech 1900D as well as the pilot of the Cessna 177 were killed.
Probable cause:
The collision was due to the absence of visual detection of the other aircraft by each of the two crews in an uncontrolled Class G Airspace where collision avoidance relies exclusively on external vigilance ("See and Avoid" rule). The decision to change the flight regime and trajectory placed the crew of the Beech 1900D in an improvised and unusual flight situation with a public transport aircraft. The following contributing factors have been identified:
- The pilots, on different frequencies, were unaware of their mutual presence,
- The pilots had their attention focused on the ship 'Norway',
- The organization of the activity in the cockpit of the Beech 1900D and its ergonomics did not allow effective monitoring, particularly towards the outside of the turn,
- The dead angles of the Cessna 177 probably masked the Beech 1900D from its pilot while both aircraft were approaching each other,
- The position of the sun may have hampered the pilot of the Cessna 177,
- The Cessna 177 transponder was off, thus the aircraft could not be viewed on the ATC radar based in Lorient. As a result, he was unable to provide traffic information to the crew of the Beech 1900D.
Final Report:

Crash of a Dornier DO228-201 in Cochin: 9 killed

Date & Time: Jul 30, 1998 at 1105 LT
Type of aircraft:
Operator:
Registration:
VT-EJW
Flight Phase:
Survivors:
No
Schedule:
Agathi – Cochin – Thiruvananthapuram
MSN:
8075
YOM:
1986
Flight number:
LRR503
Location:
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total flying hours:
5366
Captain / Total hours on type:
2271.00
Circumstances:
The aircraft was completing a flight from Agathi to Thiruvananthapuram with an intermediate stop in Cochin, carrying three passengers and three crew members. After takeoff from runway 17, at a height of about 400 feet, the aircraft pitched up steeply to a near vertical attitude and thereafter appeared to perform a manoeuvre similar to a stall turn to the right and crashed on the roof of the Component Repair Shop (CRS) building of the Naval Aircraft Yard. After impact the aircraft caught fire and was totally destroyed. All six occupants were killed as well as three people in the building. Six others received minor injuries.
Probable cause:
After take off the aircraft pitched up uncontrollably, stalled fell to its right and crashed. The uncontrollable pitch up was caused by sudden uncommanded downward movement of the Trimmable Horizontal Stabilizer leading edge. This was due to partial detachment of its 'actuator forward bearing support' fitting due non installation of required hi-lok fasteners. Poor aircraft maintenance practices at Short Haul Operations Department contributed to the accident.
Final Report:

Crash of an Embraer EMB-110P1 Bandeirante near Manacapuru: 12 killed

Date & Time: Jul 29, 1998 at 1300 LT
Registration:
PT-LGN
Flight Phase:
Survivors:
Yes
Schedule:
Manaus – Tefé
MSN:
110-343
YOM:
1982
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
24
Pax fatalities:
Other fatalities:
Total fatalities:
12
Captain / Total flying hours:
15000
Captain / Total hours on type:
8000.00
Copilot / Total flying hours:
2500
Copilot / Total hours on type:
2000
Circumstances:
The EMB-110 Bandeirante operated on a domestic flight from Manaus to Tefé, Brazil. Although the airplane was certificated for a maximum of 19 passengers, there were 25 passengers on board. Also, for financial reasons the crew decided to take more fuel than necessary for this flight. This resulted in the airplane departing with an excess of weight of 852 kg. About 20 minutes into the flight the oil pressure of the no. 2 engine dropped. The crew reduced engine power to 72% and continued to Tefé. When the flight was 185 km from Manaus at FL85 the oil pressure dropped to 40psi and the TGT increased. The copilot shut down the engine and the captain turned the airplane around, back to Manaus. At 13:15 the crew contacted Manaus ACC reporting that they were returning on one engine. The overloaded airplane flying on one engine, began to lose height. During the descent the speed was kept around 105 kts which occasionally caused activated stick shaker. To lose weight, the left overwing exit was opened and luggage of the passengers was jettisoned. The airplane did not make it to Manaus and an emergency landing on the Manacapuru River was made. The Bandeirante landed hard on the water, causing an opening in the fuselage. It sank quickly.
Probable cause:
The following factors were identified:
- It was not possible to examine the debris of the aircraft to determine the contribution of this factor to the failure of the left engine.
- It is possible that the failure to carry out a type B2 inspection and/or to carry out a type A1 inspection by an unqualified person may have contributed to the occurrence of a low oil pressure emergency, due to material deterioration or inadequate services. The impossibility of examining the aircraft could not determine this aspect.
- The owner of the air taxi company participated due to lack of adequate supervision in the planning of operations, at the technical, operational and administrative levels. This deficiency can be characterized, among other things, by the owner of the company that allowed the aircraft to fly with the type B2 inspection expired; by the excessive amount of fuel, when refueling in Manaus; by the unreasonable number of people on board, causing the aircraft to fly with excess weight, and still, by the receipt of pilots' salary to be conditioned to the accomplishment of the fateful flight.
- Errors were made by the aircraft crew due to the improper use of the resources available in the cabin, intended for the operation of the aircraft, due to non-compliance with operational rules.
- There was a mistake made by the crew due to the inadequate preparation for the flight, assuming numerous failures, such as: the non conference, by the pilots, of the cargo and passengers manifest; the lack of the realization of a briefing and still, to accept an aircraft for a flight, being the same with its inspection not carried out.
- An error was made by the crew due to inadequate evaluation of certain aspects of the flight. Such deficiency was evidenced when the first sign of failure of the lubrication system occurred, after twenty minutes of flight, and even so, they decided to proceed with the flight, when the most sensible and safe would be the return, immediately, to Manaus.
- The airline's support staff participated in the planning of weight and balance of the aircraft and the number of passengers on board, providing incorrect information to the aircraft's crew members. In addition, the mechanic who performed the A1 type inspection was not qualified for the function.
- There has been intentional non-compliance by the crew members with the operational rules established by the aircraft manufacturer.
- The Commander did not foresee what was predictable, for lack of caution, thus intentionally increasing the risk margin of the mission.
Final Report:

Crash of a Boeing 737-2J8C in Khartoum

Date & Time: Jul 19, 1998 at 1105 LT
Type of aircraft:
Operator:
Registration:
ST-AFL
Survivors:
Yes
Schedule:
Khartoum - Dongola
MSN:
21170
YOM:
1975
Flight number:
SD122
Country:
Region:
Crew on board:
9
Crew fatalities:
Pax on board:
91
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Shortly after takeoff from Khartoum-Haj Yussuf Airport, while climbing, the captain reported hydraulic problems and was cleared by ATC for an immediate return. After touchdown, several tires burst and the crew thought it was an engine malfunction so he deactivated the thrust reverser systems. Unable to stop within the remaining distance, the aircraft overran and collided with construction machines before coming to rest near a telecommunication relay. All 100 occupants evacuated safely while the aircraft was damaged beyond repair.

Crash of a Let L-410UVP-E in Dhaka

Date & Time: Jun 27, 1998
Type of aircraft:
Operator:
Registration:
S2-ADD
Survivors:
Yes
Schedule:
Ishwardi - Dhaka
MSN:
91 26 18
YOM:
1991
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
While approaching Dhaka-Tejgaon Airport at an altitude of 4,000 feet, the crew encountered technical problems with the right engine they shut down. Few seconds later, the crew was able to restart the right engine but as the temperature of the turbine increased, he shut down the engine again. This time, he was unable to feather the propeller. Due to excessive drag, the aircraft lost height and the captain attempted an emergency landing in an open field. On landing, the aircraft lost its undercarriage and came to rest. All seven occupants escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
Failure of the right engine for unknown reasons. Failure of the automatic propeller pitch control mechanism was a contributing factor.

Crash of a Swearingen SA226AC Metro II in Montreal: 11 killed

Date & Time: Jun 18, 1998 at 0728 LT
Type of aircraft:
Operator:
Registration:
C-GQAL
Survivors:
No
Schedule:
Montreal - Peterborough
MSN:
TC-233
YOM:
1977
Flight number:
PRO420
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
11
Captain / Total flying hours:
6515
Captain / Total hours on type:
4200.00
Copilot / Total flying hours:
2730
Copilot / Total hours on type:
93
Aircraft flight hours:
28931
Circumstances:
On the morning of 18 June 1998, Propair 420, a Fairchild-Swearingen Metro II (SA226-TC), C-GQAL, took off for an instrument flight rules flight from Dorval, Quebec, to Peterborough, Ontario. The aircraft took off from Runway 24 left (L) at 0701 eastern daylight time. During the ground acceleration phase, the aircraft was pulling to the left of the runway centreline, and the right rudder was required to maintain take-off alignment. Two minutes later, Propair 420 was cleared to climb to 16 000 feet above sea level (asl). At 0713, the crew advised the controller of a decrease in hydraulic pressure and requested to return to the departure airport, Dorval. The controller immediately gave clearance for a 180° turn and descent to 8000 feet asl. During this time, the crew indicated that, for the moment, there was no on-board emergency. The aircraft initiated its turn 70 seconds after receiving clearance. At 0713:36, something was wrong with the controls. Shortly afterward came the first perceived indication that engine trouble was developing, and the left wing overheat light illuminated about 40 seconds later. Within 30 seconds, without any apparent checklist activity, the light went out. At 0718:12, the left engine appeared to be on fire, and it was shut down. Less than one minute later, the captain took the controls. The flight controls were not responding normally: abnormal right aileron pressure was required to keep the aircraft on heading. At 0719:19, the crew advised air traffic control (ATC) that the left engine was shut down, and, in response to a second suggestion from ATC, the crew agreed to proceed to Mirabel instead of Dorval. Less than a minute and a half later, the crew informed ATC that flames were coming out of the 'engine nozzle'. Preparations were made for an emergency landing, and the emergency procedure for manually extending the landing gear was reviewed. At 0723:10, the crew informed ATC that the left engine was no longer on fire, but three and a half minutes later, they advised ATC that the fire had started again. During this time, the aircraft was getting harder to control in roll, and the aileron trim was set at the maximum. Around 0727, when the aircraft was on short final for Runway 24L, the landing gear lever was selected, but only two gear down indicator lights came on. Near the runway threshold, the left wing failed upwards. The aircraft then rotated more than 90° to the left around its longitudinal axis and crashed, inverted, on the runway. The aircraft immediately caught fire, slid 2500 feet, and came to rest on the left side the runway. When the aircraft crashed, firefighters were near the runway threshold and responded promptly. The fire was quickly brought under control, but all occupants were fatally injured.
Probable cause:
Findings as to Causes and Contributing Factors:
- The crew did not realize that the pull to the left and the extended take-off run were due to the left brakes' dragging, which led to overheating of the brake components.
- Dragging of the left brakes was most probably caused by an unidentified pressure locking factor upstream of the brakes on take-off. The dragging caused overheating and leakage, probably at one of the piston seals that retain the brake hydraulic fluid.
- When hydraulic fluid leaked onto the hot brake components, the fluid caught fire and initiated an intense fire in the left nacelle, leading to failure of the main hydraulic system.
- When the L WING OVHT light went out, the overheating problem appeared corrected; however, the fire continued to burn.
- The crew never realized that all of the problems were associated with a fire in the wheel well, and they did not realize how serious the situation was.
- The left wing was weakened by the wing/engine fire and failed, rendering the aircraft uncontrollable.
Findings as to Risk:
- Numerous previous instances of brake overheating or fire on SA226 and SA227 aircraft had the potential for equally tragic consequences. Not all crews flying this type of aircraft are aware of its history of numerous brake overheating or fire problems.
- The aircraft flight manual and the emergency procedures checklist provide no information on the possibility of brake overheating, precautions to prevent brake overheating, the symptoms that could indicate brake problems, or actions to take if overheated brakes are suspected.
- More stringent fire-blocking requirements would have retarded combustion of the seats, reducing the fire risk to the aircraft occupants.
- A mixture of the two types of hydraulic fluid lowered the temperature at which the fluid would ignite, that is, below the flashpoint of pure MIL-H-83282 fluid.
- The aircraft maintenance manual indicated that the two hydraulic fluids were compatible but did not mention that mixing them would reduce the fire resistance of the fluid.
Other Findings:
- The master cylinders were not all of the same part number, resulting in complex linkage and master cylinder adjustments, complicated overall brake system functioning, and difficult troubleshooting of the braking system. However, there was no indication that this circumstance caused residual brake pressure.
- The latest recommended master cylinders are required to be used only with specific brake assembly part numbers, thereby simplifying adjustments, functioning, and troubleshooting.
- Although the emergency checklist for overheating in the wing required extending the landing gear, the crew did not do this because the wing overheat light went out before the crew initiated the checklist.
- The effect of the fire in the wheel well made it difficult to move the ailerons, but the exact cause of the difficulty was not determined.
Final Report: