Crash of an Antonov AN-2T in Ust-Kuyga

Date & Time: Jul 28, 1972
Type of aircraft:
Operator:
Registration:
CCCP-32649
Flight Phase:
Survivors:
Yes
MSN:
1 18 473 03
YOM:
1952
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
En route from Deputatsky, the engine failed. The aircraft crash landed near Ust-Kuyga and was damaged beyond repair. There were no casualties.
Probable cause:
Engine failure.

Crash of a Noorduyn Norseman in Flin Flon: 1 killed

Date & Time: Jul 17, 1972
Type of aircraft:
Registration:
CF-ECE
Flight Phase:
Survivors:
Yes
MSN:
N29-36
YOM:
1947
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
1
Aircraft flight hours:
11800
Circumstances:
Shortly after takeoff from Flin Flon Airport, while climbing, the airplane stalled and crashed into a lake and sank. A passenger was killed while three other occupants were injured.
Probable cause:
The engine failed during initial climb after a fuel line broke, causing the fuel to leak in the engine and to catch fire while contacting high temperature parts.

Crash of a Douglas C-47B-30-DK in Tabuk

Date & Time: Jul 10, 1972
Operator:
Registration:
HZ-AAK
Survivors:
Yes
MSN:
16231/32979
YOM:
1945
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Suffered a landing accident at Tabuk Airport. There were no casualties.

Crash of a Convair CV-580 near Appleton: 5 killed

Date & Time: Jun 29, 1972 at 1037 LT
Type of aircraft:
Operator:
Registration:
N90858
Flight Phase:
Survivors:
No
Schedule:
Houghton – Ironwood – Green Bay – Oshkosh – Milwaukee – Chicago
MSN:
83
YOM:
1969
Flight number:
NC290
Crew on board:
3
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
15688
Captain / Total hours on type:
3079.00
Copilot / Total flying hours:
4462
Copilot / Total hours on type:
62
Aircraft flight hours:
45905
Circumstances:
The airplane was on its way from Green Bay to Oshkosh, flying at an altitude of 2,500 feet in relative good weather conditions when it collided with an Air Wisconsin De Havilland DHC-6 Twin Otter 200 registered N4043B. En route from Sheboygan to Appleton with six passengers and two pilots on board, the Twin Otter was descending to Appleton Airport. At the time of the accident, both airplanes were flying under VFR in an uncontrolled airspace. Following the collision, both aircraft crashed into Lake Winnebago, some five miles southeast of Appleton Airport. Debris were found floating on water, both airplanes were totally destroyed and all 13 occupants were killed.
Probable cause:
The failure of both flight crews to detect visually the other aircraft in sufficient time to initiate evasive action. the Board is unable to determine why each crew failed to see and avoid the other aircraft; however, the Board believes that the ability of both crews to detect the other aircraft in time to avoid a collision was reduced because of the atmospheric conditions and human visual limitations.
Final Report:

Crash of a De Havilland DHC-6 Twin Otter 200 near Appleton: 8 killed

Date & Time: Jun 29, 1972 at 1037 LT
Operator:
Registration:
N4043B
Survivors:
No
Schedule:
Chicago - Sheboygan - Appleton
MSN:
13
YOM:
1966
Flight number:
ZW671
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
8
Captain / Total flying hours:
6556
Captain / Total hours on type:
3412.00
Copilot / Total flying hours:
4309
Copilot / Total hours on type:
1685
Aircraft flight hours:
15664
Circumstances:
Following a uneventful flight from Sheboygan, the crew started the descent to Appleton Airport in relative good weather conditions when, at an altitude of 2,500 feet, the Twin Otter collided with a North Central Airlines Convair CV-580 registered N90858. En route from Green Bay to Oshkosh, the Convair was carrying two passengers and three crew members. At the time of the accident, both airplanes were flying under VFR in an uncontrolled airspace. Following the collision, both aircraft crashed into Lake Winnebago, some five miles southeast of Appleton Airport. Debris were found floating on water, both airplanes were totally destroyed and all 13 occupants were killed.
Probable cause:
The failure of both flight crews to detect visually the other aircraft in sufficient time to initiate evasive action. the Board is unable to determine why each crew failed to see and avoid the other aircraft; however, the Board believes that the ability of both crews to detect the other aircraft in time to avoid a collision was reduced because of the atmospheric conditions and human visual limitations.
Final Report:

Crash of a De Havilland DH.114 Heron 2B in Ponce: 5 killed

Date & Time: Jun 24, 1972 at 2317 LT
Type of aircraft:
Operator:
Registration:
N554PR
Survivors:
Yes
Schedule:
San Juan - Ponce
MSN:
14085
YOM:
1955
Flight number:
PQ191
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
18
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
8297
Captain / Total hours on type:
3017.00
Copilot / Total flying hours:
1434
Copilot / Total hours on type:
102
Aircraft flight hours:
11364
Circumstances:
On a night approach to Ponce-Mercedita Airport, the crew decided to make a go-around when control was lost. The airplane overrotated then crashed 2,200 feet past the runway 29 threshold and 260 feet to the south. Both pilots and three passengers were killed while all other occupants were injured. The aircraft was destroyed.
Probable cause:
The National Transportation Safety Board determines that the probable cause of the accident was the loss of directional control during a go-around from a landing attempt. Control was lost when the aircraft was overrotated at too low an airspeed to sustain flight. The crew’s reasons for rejecting the landing are not known.
Final Report:

Crash of a Hawker-Siddeley HS.121 Trident 1C in London: 118 killed

Date & Time: Jun 18, 1972 at 1711 LT
Operator:
Registration:
G-ARPI
Flight Phase:
Survivors:
No
Schedule:
London - Brussels
MSN:
2109
YOM:
1964
Flight number:
BE548
Region:
Crew on board:
9
Crew fatalities:
Pax on board:
109
Pax fatalities:
Other fatalities:
Total fatalities:
118
Captain / Total flying hours:
15000
Captain / Total hours on type:
4000.00
Copilot / Total flying hours:
1400
Copilot / Total hours on type:
750
Circumstances:
Following a normal takeoff roll on runway 28R, the aircraft rotated 42 seconds after brakes were released and lifted off 2 seconds later at 145 knots IAS. At 63 seconds the autopilot was engaged 355 feet above the runway at 170 knots IAS; the IAS speed lock was selected shortly thereafter. At 74 seconds the aircraft started a 20° banked turn to port towards the Epsom Non-Directional Beacon (NDB). At 83 seconds the captain reported 'Climbing as cleared'. He was then instructed to change frequency and contact London Air Traffic Control Centre. At 93 seconds the noise-abatement procedure was initiated. On the assumption that the captain was the handling pilot, this would involve the second officer selecting the flaps fully up and operating the thrust levers to reduce power to the pre-calculated figure. At 100 seconds the captain called 'Passing 1500' and at 103 seconds the aircraft was cleared to climb to Flight Level 60. This message was acknowledged by the captain at 108 seconds with the terse call 'up to 60'. This was the last message received from the flight. At second 114 when the airspeed was 162 knots and the altitude 1,772 feet, the droop lever was selected up putting the aircraft into the area of the stall as the droop started to move. At second 116 the stick-pusher stall recovery device operated, causing the autopilot automatically to disengage and the nose of the aircraft to pitch down and the stick-push to cease as the incidence decreased. Since the elevator trim would stay at its position on autopilot disengagement which at that speed with the droop up would be - the incidence then increased causing a second stick-push at second 124 and a third at second 127. At second 128 the stall recovery system was manually inhibited by pulling the lever. The aircraft then pitched up rapidly, losing speed and height, entering very soon afterwards the true aerodynamic stall and then a deep stall from which at that height no recovery was possible. Impact was at second 150 in a field next to the A30 motorway. The aircraft was totally destroyed and none of the 118 occupants survived the crash.
Probable cause:
The immediate causes of the accident were these:
- A failure by Captain Key to achieve and maintain adequate speed after noise-abatement procedures,
- Retraction of the droops at some 60 knots below the proper speed causing the aircraft to enter the stall regime and the stick-shaker and pusher to operate,
- Failure by the crew to monitor the speed errors and to observe the movement of the droop lever,
- Failure by the crew to diagnose the reason for the stick-shaker operation and the concomitant warnings,
- The dumping by the crew of the stall recovery system.
The underlying causes were these:
- The abnormal heart condition of Captain Key leading to lack of concentration and impaired judgment sufficient to account for his toleration of the speed errors and to his retraction of, or order to retract, the droops in mistake for the flaps,
- Some distraction, the nature of which is uncertain, possibly due to the presence of Captain Collins as a passenger on the flight deck, which caused S/O Ticehurst's attention to wander from his monitoring duties,
- Lack of training directed at the possibility of 'subtle' pilot incapacitation,
- Lack of experience of S/O Keighley,
- Lack of knowledge in the crew of the possibility or implication of a change of configuration stall,
- Lack of knowledge on the part of the crew that a stick-shaker and push might be experienced almost simultaneously and of the probable cause of such an event,
- Lack of any mechanism to prevent retraction of the droops at too low a speed after flap-retraction.
Final Report:

Crash of an Ilyushin II-62 in Cairo

Date & Time: Jun 16, 1972 at 1200 LT
Type of aircraft:
Operator:
Registration:
SU-ARN
Survivors:
Yes
MSN:
00801
YOM:
1970
Country:
Region:
Crew on board:
12
Crew fatalities:
Pax on board:
47
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
After landing on runway 36 at Cairo-Almaza Airport, the four engine airplane was unable to stop within the remaining distance, overran, lost its undercarriage and came to rest. All 59 occupants escaped uninjured while the aircraft was damaged beyond repair. It was determined that the crew was scheduled to land at Cairo International Airport runway 34 but following a poor flight preparation and several mistakes on approach, the crew descended to Almaza Airport instead of the international airport. At the time of the accident, the first portion of 650 meters of runway 34 at International Airport were closed to traffic due to repair. Thinking they were landing on the right airport, the crew landed at Almaza runway 36 700 meters past its threshold. In such conditions, the airplane was unable to stop within the remaining distance of runway 36 (1,890 meters), which is a relative short for such aircraft type.
Probable cause:
Crew error.

Crash of a Convair CV-880-22M-21 near Pleiku: 81 killed

Date & Time: Jun 15, 1972 at 1359 LT
Type of aircraft:
Operator:
Registration:
VR-HFZ
Flight Phase:
Survivors:
No
Schedule:
Singapore – Bangkok – Hong Kong
MSN:
22-00-53
YOM:
1961
Flight number:
CX700Z
Country:
Region:
Crew on board:
10
Crew fatalities:
Pax on board:
71
Pax fatalities:
Other fatalities:
Total fatalities:
81
Captain / Total flying hours:
14343
Captain / Total hours on type:
5261.00
Copilot / Total flying hours:
7649
Copilot / Total hours on type:
2687
Aircraft flight hours:
29434
Circumstances:
Flight CX700Z was a scheduled international flight from Singapore to Hong Kong with an en-route stop at Bangkok. It made a 55 minute stop at Bangkok during which 68 passengers and baggage were off loaded, and 35 passengers and baggage, in addition to 35 000 lbs of JP-1 fuel, were loaded. The aircraft took off from Bangkok at 0455 hours GMT bound for Hong Kong via airway Green 67 at FL290. The flight proceeded normally with the aircraft maintaining routine radio contact first with Bangkok ACC and from 0542 hours with Saigon ACC. The last message from the aircraft was received at 0554 hours by Saigon ACC giving the aircraft's position at 0553 hours over reporting point "PE5" at FL290, with an estimated time over "XVK" reporting point of 0606 hours. At 0620 hours, when no further messages had been received from the aircraft, Saigon ACC called it several times but received no reply. A request for information concerning the aircraft, made by Saigon ACC at 0640 hours to Hong Kong and then Taipei ACCs, produced negative results. The Distress Phase was initiated at 0715 hours and DETRESFA signalled to Tan Son Nhut RCC for appropriate action. The RCC advised Saigon ACC at 0755 hours that a Convair type aircraft had crashed about 30 NM southeast of Pleiku TACAN beacon. The aircraft was identified as VR-HFZ by two helicopter pilots who reached the accident site soon after the occurrence and while the wreckage was still burning. They recovered two bodies from the burning wreckage and flew them to Pleiku. The aircraft was totally destroyed and none of the 81 occupants survived the crash.
Probable cause:
The aircraft broke up in the air and caught fire following the detonation of a high explosive device within the passenger cabin.
Final Report:

Crash of a Douglas DC-8-53 in New Delhi: 86 killed

Date & Time: Jun 14, 1972 at 2018 LT
Type of aircraft:
Operator:
Registration:
JA8012
Survivors:
Yes
Schedule:
Tokyo – Bangkok – New Delhi – Tehran – Cairo – Rome – Frankfurt – London
MSN:
45680/213
YOM:
1964
Flight number:
JL471
Country:
Region:
Crew on board:
11
Crew fatalities:
Pax on board:
76
Pax fatalities:
Other fatalities:
Total fatalities:
86
Circumstances:
During a night approach to runway 28 at New Delhi-Palam Airport, the crew failed to realize his altitude was too low when the airplane struck several houses and crashed in flames on the west shore of the Yamuna River, some 22 km east of the airport. Ten crew members and 72 passengers as well as four people on the ground were killed. Five other occupants were injured. The aircraft was totally destroyed by impact forces and a post crash fire. At the time of the accident, the copilot was the pilot-in-command.
Probable cause:
Japanese investigators claimed a false glide path signal to be responsible for the descent into terrain. Indian investigators say the accident was caused by a total disregard of laid down procedures by the crew and abandoning all instrument indications without properly ensuring sighting of the runway.