Crash of a Swearingen SA226T Merlin IIIB in Rockport: 2 killed

Date & Time: Jan 19, 1982 at 1323 LT
Registration:
N336SA
Survivors:
No
Schedule:
Corpus Christi-Rockport
MSN:
T-336
YOM:
1980
Crew on board:
2
Crew fatalities:
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3800
Circumstances:
Prior to the FAF during a VOR/DME approach, the Merlin was cleared to change to the unicom frequency. The pilot of the Merlin contacted unicom and requested and airport advisory. The unicom operator replied that there was a pirep of 500 feet over the field with two miles visibility but 'zilch' over the water. Shortly after this contact the pilot of the AA-5A called on unicom turning final. The pilot of the AA-5A was given the same advisory as given to the Merlin and further advised that another aircraft was inbound for runway 14. The aircraft collided less than one mile northwest of the approach end of runway 14. AIM 157 recommends that VFR inbound flights broadcasting entering downwind and final. AIM 363 recommends that, when making an IFR approach to an airport not served by a tower or FSS and after ATC advises to change to advisory frequency, to broadcast intentions, including type approach, position and when over FAF inbound. All three occupants in both airplanes were killed.
Probable cause:
Midair collision during IFR circling due to inadequate visual lookout on part of both crew. The following findings were reported:
- Unavailable control tower,
- Unavailable radar approach/departure,
- Low ceiling,
- Fog,
- Inadequate air/ground communications from both crew.
Final Report:

Crash of a Canadair CL-44D4-1 in Miami

Date & Time: Jan 19, 1982 at 0830 LT
Type of aircraft:
Operator:
Registration:
HC-BHS
Flight Type:
Survivors:
Yes
Schedule:
Miami - Managua
MSN:
14
YOM:
1961
Crew on board:
4
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Aircraft flight hours:
42851
Circumstances:
After takeoff from Miami-Intl Airport, outbound to Managua on a cargo flight, the crew encountered technical problems with the undercarriage due to a hydraulic pressure fault. Decision was taken to return for a safe landing and the landing gears were lowered. The nose gear was down and locked but not both main gears which remained partially deployed and not locked. Upon touchdown, both main gear partially retracted and the airplane came to rest on the runway. All six occupants escaped uninjured while the aircraft was considered as damaged beyond repair.
Probable cause:
Undercarriage failure upon landing due to hydraulic pressure fault.

Crash of a Convair HC-131A Samaritan in Corpus Christi

Date & Time: Jan 18, 1982
Type of aircraft:
Operator:
Registration:
52-5786
Flight Type:
Survivors:
Yes
Schedule:
Corpus Christi - Corpus Christi
MSN:
53-6
YOM:
1954
Crew on board:
8
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was completing a local training flight at Corpus Christi Airport. Following an approach in reduced visibility due to foggy conditions, the airplane landed hard on runway 10R. Upon touchdown, the aircraft went out of control, veered off runway and came to rest. All eight crew members evacuated safely while the aircraft was damaged beyond repair.

Crash of a Convair CV-440 Metropolitan in Pearl Harbor

Date & Time: Jan 17, 1982 at 2245 LT
Operator:
Registration:
N21DR
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Honolulu - Kahului
MSN:
325
YOM:
1956
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3550
Captain / Total hours on type:
88.00
Aircraft flight hours:
40846
Circumstances:
After liftoff, the pilot called for the landing gear to be raised. As the plane was climbing through about 100 feet agl, the pilot noted a loss of power in the right engine and saw a fire light. Ground witnesses heard a muffled explosion and saw smoke and fire trailing from the right engine. The right engine was feathered and the pilot attempted to return to the airport, but was unable to maintain altitude. The plane was ditched near the entrance of Pearl Harbor. A tear down of the right engine revealed that the top ring lands of the n° 10 and n°14 pistons were broken and the top ring was missing from each of the pistons. Also, the rear counterbalance drive intermediate gear was worn and 11 gear teeth were missing. Additionally, the rear counterbalance drive gear was worn.
Probable cause:
Loss of engine power and mechanical failure during initial climb due to partial piston failure. The following findings were reported:
- Engine assembly, ring, partial failure,
- Fire, explosion,
- Dark night.
Final Report:

Crash of a Piper PA-31-310 Navajo in Port Mansfield: 1 killed

Date & Time: Jan 17, 1982 at 1500 LT
Type of aircraft:
Registration:
N9181Y
Flight Type:
Survivors:
No
MSN:
31-240
YOM:
1968
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3200
Circumstances:
The aircraft crashed and burned about half a mile from the approach end of runway 12. A witness reported that 'the plane just fell' while the pilot was making a sharp turn. An estimated 1,500 lbs of marijuana was on board.
Probable cause:
Loss of control on BFR approach pattern after the pilot failed to maintain flying speed. The following findings were reported:
- Stolen aircraft, unauthorized use,
- Inadvertent stall by the pilot.
Final Report:

Crash of a Piper PA-31T Cheyenne II in Delta

Date & Time: Jan 17, 1982 at 1435 LT
Type of aircraft:
Registration:
N91TW
Flight Type:
Survivors:
Yes
Schedule:
Delta - Las Vegas
MSN:
31-7820078
YOM:
1978
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4000
Captain / Total hours on type:
520.00
Aircraft flight hours:
340
Circumstances:
Approximately 1/2 mile from the airport after takeoff, the pilot noticed the left front baggage door partly open and made a left turn back toward the airstrip. After the turn, the baggage door came completely open, the left wing dropped immediately and the aircraft stalled. The pilot added full power and lowered the nose. When he raised the nose near the ground, the aircraft shuddered and crashed. Two rescue personnel, both certified pilots, arrived shortly after the accident and found the nose baggage door in the unlocked position with the bayonet pins retracted. A Piper representative stated that if the left side nose baggage door of a PA-31 opened in flight there would be the likelihood of an interruption to the smooth airflow through the prop, possibly reducing the thrust produced by the blades.
Probable cause:
Loss of control in flight while maneuvering to landing area after the pilot failed to maintain flying speed. The following findings were reported:
- Cargo door unlocked,
- Inadequate preflight preparation,
- Aircraft performances deteriorated,
- Inadvertent stall by the pilot.
Final Report:

Crash of a Boeing 737-222 in Washington DC: 78 killed

Date & Time: Jan 13, 1982 at 1601 LT
Type of aircraft:
Operator:
Registration:
N62AF
Flight Phase:
Survivors:
Yes
Schedule:
Washington DC - Tampa - Fort Lauderdale
MSN:
19556/130
YOM:
1969
Flight number:
QH090
Crew on board:
5
Crew fatalities:
Pax on board:
74
Pax fatalities:
Other fatalities:
Total fatalities:
78
Captain / Total flying hours:
8300
Captain / Total hours on type:
1852.00
Copilot / Total flying hours:
3353
Copilot / Total hours on type:
992
Aircraft flight hours:
23608
Aircraft flight cycles:
29549
Circumstances:
Air Florida Flight 90 was scheduled to leave Washington National Airport at 14:15 EST for a flight to Fort Lauderdale International Airport, FL (FLL), with an intermediate stop at the Tampa, FL (TPA). The aircraft had arrived at gate 12 as Flight 95 from Miami, FL, at 13:29. Because of snowfall, the airport was closed for snow removal from 13:38 to 14:53. At about 14:20 maintenance personnel began deicing the left side of the fuselage with deicing fluid Type II because the captain wanted to start the deicing just before the airport was scheduled to reopen (at 14:30) so that he could get in line for departure. Fluid had been applied to an area of about 10 feet when the captain terminated the operation because the airport was not going to reopen at 14:30. Between 14:45 and 14:50, the captain requested that the deicing operation be resumed. The left side of the aircraft was deiced first. No covers or plugs were installed over the engines or airframe openings during deicing operations. At 15:15, the aircraft was closed up and the jet way was retracted and the crew received push-back clearance at 15:23. A combination of ice, snow, and glycol on the ramp and a slight incline prevented the tug, which was not equipped with chains, from moving the aircraft. Then, contrary to flight manual guidance, the flight crew used reverse thrust in an attempt to move the aircraft from the ramp. This resulted in blowing snow which might have adhered to the aircraft. This didn't help either, so the tug was replaced and pushback was done at 15:35. The aircraft finally taxied to runway 36 at 15:38. Although contrary to flight manual guidance, the crew attempted to deice the aircraft by intentionally positioning the aircraft near the exhaust of the aircraft ahead in line (a New York Air DC-9). This may have contributed to the adherence of ice on the wing leading edges and to the blocking of the engine’s Pt2 probes. At 15:57:42, after the New York Air aircraft was cleared for takeoff, the captain and first officer proceeded to accomplish the pre-takeoff checklist, including verification of the takeoff engine pressure ratio (EPR) setting of 2.04 and indicated airspeed bug settings. Takeoff clearance was received at 15:58. Although the first officer expressed concern that something was 'not right' to the captain four times during the takeoff, the captain took no action to reject the takeoff. The aircraft accelerated at a lower-than-normal rate during takeoff, requiring 45 seconds and nearly 5,400 feet of runway, 15 seconds and nearly 2,000 feet more than normal, to reach lift-off speed. The aircraft initially achieved a climb, but failed to accelerate after lift-off. The aircraft’s stall warning stick shaker activated almost immediately after lift-off and continued until impact. The aircraft encountered stall buffet and descended to impact at a high angle of attack. At about 16.01, the aircraft struck the heavily congested northbound span of the 14th Street Bridge and plunged into the ice-covered Potomac River. It came to rest on the west end of the bridge 0.75 nmi from the departure end of runway 36. When the aircraft struck the bridge, it struck six occupied automobiles and a boom truck before tearing away a 41-foot section of the bridge wall and 97 feet of the bridge railings. Four persons in vehicles on the bridge were killed; four were injured, one seriously.
Probable cause:
The flight crew's failure to use engine anti-ice during ground operation and takeoff, their decision to take off with snow/ice on the airfoil surfaces of the aircraft, and the captain’s failure to reject the takeoff during the early stage when his attention was called to anomalous engine instrument readings. Contributing to the accident were the prolonged ground delay between deicing and the receipt of ATC takeoff clearance during which the airplane was exposed to continual precipitation, the known inherent pitch up characteristics of the B-737 aircraft when the leading edge is contaminated with even small amounts of snow or ice, and the limited experience of the flight crew in jet transport winter operations.
Final Report:

Crash of a Cessna 414 Chancellor in Aberdeen

Date & Time: Jan 12, 1982 at 1600 LT
Type of aircraft:
Registration:
N7706
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Oklahoma City - Miami
MSN:
414-0071
YOM:
1970
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1640
Captain / Total hours on type:
46.00
Circumstances:
The non-instrument rated pilot crashed about three hours after taking off with 4 1/2 hours of fuel on board. He crashed while attempting an off airport landing in a large field. The field was located less than half way to his destination. The sheriff reported minimum visibility with snow and freezing rain. The occupant received only minor injuries, but the plane was destroyed by impact and ground fire. An examination of the wreckage revealed no evidence of a pre-impact malfunction/failure of the engine or in flight fire. The pilot provided the following account: he was cruising above an overcast at 17,500 feet when the left engine began cutting out and forced him to descend through the clouds; he descended to VFR conditions at 1,200 feet agl over snow covered terrain and determined his location by viewing a water tower. He then elected to land in a field when he saw smoke and fire coming from the engine cowling. While landing, the left wing dropped and touched down first.
Probable cause:
Loss of engine power due to improper in-flight decision on part of the pilot. The following findings were reported:
- Clouds,
- Low ceiling,
- Rain,
- Icing conditions.
Final Report:

Crash of a Piper PA-31-310 Navajo in Ithaca: 2 killed

Date & Time: Jan 5, 1982 at 0749 LT
Type of aircraft:
Operator:
Registration:
N546BA
Survivors:
No
Schedule:
Utica – Ithaca – Washington DC
MSN:
31-709
YOM:
1971
Flight number:
EMP141
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3300
Captain / Total hours on type:
728.00
Copilot / Total flying hours:
2200
Copilot / Total hours on type:
380
Aircraft flight hours:
5906
Circumstances:
The airplane crashed while attempting an approach to Tompkins County Airport, Ithaca, New York, an en route stop from schedule flight 141 from Utica to Washington DC. The flight crew had contacted Elmira approach control and had received instructions for an instrument landing system (ILS) approach to runway 32 at Tompkins County Airport. About 07:40 EST, the copilot declared an emergency stating that the airplane had a landing flap problem; he later stated that only one flap was down. He also stated that they were not able to maintain altitude and that the airplane was descending. Elmira approach lost radar contact with the airplane about 07:41 EST; the last radio transmission from the flight was recorded about 07:45 EST. The airplane crashed in a wooded area near three suburban residences. The pilot and copilot, the only persons aboard, were killed. There were no injuries to personnel on the ground. The airplane was destroyed by impact and post impact fire.
Probable cause:
The probable cause of the accident was excessive wear of the left flap motor/flexible drive spline and certification of the airplane with a flap system that did not meet the requirements of Civil Air Regulation 3.339. The worn spline caused a split flap condition of 34 that resulted in marginal flight control authority. Moderate low altitude turbulence and transient low level wind shear may have contributed to the upset and loss of control.
Final Report:

Crash of a Cessna 414A Chancellor in Ashland: 8 killed

Date & Time: Jan 3, 1982 at 1704 LT
Type of aircraft:
Registration:
N2620L
Survivors:
No
Schedule:
Boca Raton - Ashland
MSN:
414A-0299
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
8
Captain / Total flying hours:
1809
Captain / Total hours on type:
250.00
Circumstances:
The pilot received two weather briefings, one on the evening before the flight, another at 1009 EST, within three hours of the takeoff time. IFR conditions were forecasted at the uncontrolled, destination airport. The pilot filed an IFR flight plan, but did not list an alternate airport. The aircraft departed Boca Raton at 1257 EST. The flight was uneventful en route and all communications were normal. During arrival, the pilot was cleared for a VOR 3 approach to runway 16. The minimum descent altitude (MDS) for the approach was 800 feet MSL (595 feet AGL) and the minimum visibility was one mile. Several witnesses at and near the airport saw or heard the aircraft. They described the aircraft as crossing the airport from the west side to the east. Those who saw it described it to be approximately 150 to 200 feet AGL, in and out of the clouds. Reportedly, the aircraft then circled and crossed the airport again. Subsequently, it struck an 80 feet tree, then impacted the ground in a steep descent. There was no evidence of failure or malfunction of the airframe or powerplant before impact. The aircraft was estimated to be 46 lbs over the max gross weight limit during impact. All eight occupants were killed.
Probable cause:
In flight collision with terrain during an uncontrolled descent due to improper IFR procedures. The following findings were reported:
- Dusk,
- Low ceiling,
- Fog,
- Rain,
- The pilot continue into known adverse weather,
- Trees,
- Overconfidence in personal ability on part of the pilot.
Final Report: