Crash of a Douglas DC-3C in Memphis

Date & Time: Nov 7, 1997 at 1956 LT
Type of aircraft:
Operator:
Registration:
N59316
Flight Type:
Survivors:
Yes
Schedule:
Gulfport - West Memphis
MSN:
18986
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7853
Captain / Total hours on type:
2603.00
Aircraft flight hours:
24516
Circumstances:
The PIC stated he was established on an instrument approach when the left engine fuel pressure dropped to zero and the engine quit. He moved the fuel selector to the right rear fuel tank and the engine started. He continued the approach for about 2 miles when the right engine quit followed by the left engine. He made a forced landing to a sandbar. Examination of the airplane revealed the fuel tanks were not ruptured and the fuel tanks were empty.
Probable cause:
The pilot-in-command's improper management of fuel resulting in a total loss of engine power on both engines during an instrument approach due to fuel exhaustion.
Final Report:

Crash of a Cessna 402B in Fort Lauderdale

Date & Time: Nov 2, 1997 at 1745 LT
Type of aircraft:
Operator:
Registration:
N69312
Survivors:
Yes
Schedule:
Andros Town - Fort Lauderdale
MSN:
402B-0430
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5017
Captain / Total hours on type:
2175.00
Aircraft flight hours:
7482
Circumstances:
The pilot was on approach for landing when the right main landing gear did not indicate that it was down. The pilot made a go-around and remained in left closed traffic performing emergency gear extension procedures with negative results. The pilot departed closed traffic and proceeded offshore to burn off fuel before attempting an emergency landing. A company airplane was dispatched to verify the landing gear position. The pilot started a straight in approach for landing five miles from the airport. The right engine started surging and quit. The left engine started surging one mile from the runway. He switched fuel tanks. The engine started and quit. He made a forced landing straight ahead and collided with runway approach lights about 1/4 mile from the end of the runway. The pilot stated he ran out of fuel.
Probable cause:
The pilot's improper management of fuel resulting in a total loss of engine power on both engines due to fuel exhaustion.
Final Report:

Crash of a Cessna 402B in Tampa: 3 killed

Date & Time: Oct 27, 1997 at 1510 LT
Type of aircraft:
Registration:
N69293
Flight Type:
Survivors:
Yes
Schedule:
Sarasota - Tampa
MSN:
402B-0415
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
3050
Aircraft flight hours:
3622
Circumstances:
The flight had departed runway 32, under IFR, from a local reliever airport 35 miles south of the destination, and was cleared to intercept the ILS approach for runway 36R. Instrument meteorological conditions existed with a low scattered cloud layer beneath the 900 foot broken clouds. Visibility was 8 miles. The flight never stabilized on the inbound course and glide slope. After acquiring the runway visually, about 3 miles from the airport, the airplane dove for the runway, subsequently touching down with the landing gear retracted. The left propeller incurred greater damage than the right propeller. The airplane began to go around, pitched up, then entered a steep left, descending turn that continued until impact with the ground.
Probable cause:
The pilot's failure to follow the landing checklist and extend the landing gear for landing, and his failure to maintain VMC during a go-around. Factors were: the pilot's diverted attention due to a non-stabilized instrument approach and his lack of recent instrument experience.
Final Report:

Crash of a Cessna 208B Grand Caravan in the Uncompahgre National Forest: 9 killed

Date & Time: Oct 8, 1997 at 0723 LT
Type of aircraft:
Operator:
Registration:
N12022
Flight Phase:
Survivors:
No
Site:
Schedule:
Montrose - Page
MSN:
208B-0432
YOM:
1995
Crew on board:
1
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total flying hours:
12900
Captain / Total hours on type:
1546.00
Aircraft flight hours:
2599
Aircraft flight cycles:
3680
Circumstances:
The airplane departed under visual flight rules (VFR) for a flight over mountainous terrain. It was tracked by radar from the departure area to the accident site. While climbing at the normal rate of climb to 15,400 feet, the airplane abruptly disappeared from radar. The wreckage was located among pine trees and exhibited evidence of a steep flight path angle and damage consistent with a stall/spin event. Investigation revealed no indication of airframe or flight control anomalies, and the powerplant and propeller damage was consistent with engine operation at moderate to high power. Evidence indicated that the airplane was free of airframe ice at impact. Postaccident calculations indicate that the airplane was near the maximum certificated gross weight and aft center of gravity limit. The pilot did not maintain instrument flying currency and reportedly avoided instrument meteorological conditions (IMC). Evidence indicated that the pilot did not use oxygen, as required (when flying above 12,000 feet). Ground observations and satellite and Doppler radar imagery indicated widespread cloudiness over the mountains west of Montrose on the day of the accident. Satellite data showed variable cloud tops higher than the airplane's flight altitude in the vicinity of the accident. The radar plot of the aircraft during the climb above 10,000 feet indicated course changes from the southwest to the northwest, back to the southwest and then a sharp turn to the right just prior to the rapid descent.
Probable cause:
the pilot's failure to maintain sufficient airspeed for undetermined reasons while maneuvering the airplane near the maximum gross weight and aft cg in or near instrument meteorological conditions, resulting in the loss of control and entry into a stall/spin. Factors contributing to the accident were the pilot's improper in-flight planning and decision-making and his failure to use proper stall/spin recovery techniques.
Final Report:

Crash of a Beechcraft G18S in Crosbyton

Date & Time: Oct 6, 1997 at 1830 LT
Type of aircraft:
Registration:
N9312Y
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Lubbock - Dallas
MSN:
BA-550
YOM:
1960
Flight number:
MXP1061
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3222
Captain / Total hours on type:
1328.00
Aircraft flight hours:
17974
Circumstances:
While in cruise flight at 9,000 feet MSL, the left engine began to 'run rough and lose power.' The pilot said he interpreted the problem as carburetor icing and applied carburetor heat. With the engine still running rough, the left propeller was feathered and the left engine shut down. Restart attempts were not successful. Unable to maintain altitude, the pilot requested to land at a nearby airport. After descending through IMC weather, the pilot realized that he would not make it to the airport, and executed a forced landing to rough/uneven terrain. Examination of the engines revealed that the alternate air doors were missing on the right and left engine. The hinges for the doors were attached to both carburetors and showed no evidence of distortion or impact damage. The doors were not found at the wreckage site. A missing alternate air door would allow ambient air to enter the carburetor, rendering the carburetor heating system ineffective. According to carburetor icing probability charts, the reported temperature and dew point values would be favorable to the formation of induction system icing.
Probable cause:
Inadequate maintenance which resulted in diminished carburetor heat effectiveness due to missing alternate air doors. Contributing were conducive carburetor icing weather conditions, low ceilings during the emergency descent, and the lack of suitable terrain for the forced landing.
Final Report:

Crash of a Beechcraft E18S in Lake Elmo

Date & Time: Oct 2, 1997 at 0605 LT
Type of aircraft:
Registration:
N916TM
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Lake Elmo - Minneapolis
MSN:
BA-337
YOM:
1958
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4450
Captain / Total hours on type:
350.00
Aircraft flight hours:
10530
Circumstances:
The pilot reported that the airplane lifted off at 70 knots. After accelerating in ground effect the airplane became 'unstable in the roll axis' so he added power. He reported that the left wing tip contacted the runway approximately 3/4 the way down the runway. The pilot then added additional power at which point the left wing contacted the grass off the left side of the departure end of the runway. The pilot then reduced the power to idle and landed the airplane in the grass collapsing the landing gear. The pilot reported that the engines sounded normal throughout the accident sequence. Investigation revealed another Beech 18 had taken off on the same runway, but in the opposite direction of N916TM less than one minute prior to the accident.
Probable cause:
The pilot's failure identify the unsafe condition (vortex turbulence) which existed due to departing airplane and his subsequent inability to control the airplane once encountering the turbulence.
Final Report:

Ground accident of a Boeing 727-51C in Denver

Date & Time: Oct 1, 1997 at 0436 LT
Type of aircraft:
Operator:
Registration:
N414EX
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Denver – San Francisco
MSN:
18899/256
YOM:
1966
Flight number:
RYN607
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
15020
Captain / Total hours on type:
7305.00
Aircraft flight hours:
47098
Aircraft flight cycles:
45215
Circumstances:
As the cargo jet was taxiing for takeoff in a non movement area, it was struck by an airport employee shuttle bus. The airplane captain was seriously injured. Visual meteorological conditions prevailed, and the collision occurred during predawn hours. The bus driver said he stopped at the stop sign, turned on the 4-way flasher lights, and looked both ways. He saw one inbound aircraft to the right that had stopped. He did not see the airplane approaching from the left as he started across the cargo ramp. The airplane crew stated they did not see the bus until seconds before impact. Airplane skid marks, measuring 22 and 24 feet in length, were noted on the taxiway. No bus skid marks were noted on the roadway.
Probable cause:
Failure of the bus driver to yield the right of way to oncoming traffic due to his inadequate visual lookout. Factors were visibility restrictions, inadequate driver training by management, and the flight crew's inadequate visual lookout due to their attention being diverted by performing the pre takeoff checklist.
Final Report:

Crash of a De Havilland DHC-2 Beaver off Ketchikan: 1 killed

Date & Time: Sep 29, 1997 at 1747 LT
Type of aircraft:
Operator:
Registration:
N4787C
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Ketchikan - Ketchikan
MSN:
1330
YOM:
1959
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2071
Captain / Total hours on type:
1200.00
Aircraft flight hours:
24267
Circumstances:
The float equipped airplane was observed taking off in light winds and calm water, and obtaining a steep climb and nose high attitude. Witnesses described hearing no reduction of engine noise from takeoff power to climb power. The airplane entered a steep left bank about 200 feet above the water, then rolled rapidly to the right and impacted at a steep angle into the water. The airplane had been modified with a Short Take Off and Landing (STOL) kit. Certification flight tests had determined that this modification eliminated aerodynamic warning of impending stalls, and therefore required an audible stall warning. Test results also required the addition of both a ventral fin, and horizontal stabilizer finlets, to meet directional stability certification. These tests determined that the least stable condition was in the takeoff flap configuration, during climb. The Supplemental Type Certificate (STC) for the modification required the ventral fin, and an audible stall warning system be installed. The manufacturer provided a marketing video, produced prior to the STC approval, which stated the stall warning system was not required in the U.S. The company indicated this tape was used for training, and was a basis for pilots routinely disabling the stall warning horn by pulling the circuit breaker. At the time of the accident, the airplane did not have the ventral fin installed, a takeoff flaps setting was selected, and the audible stall warning circuit breaker was in the pulled (disabled) position. The local FAA Flight Standards Office had inspected the accident airplane 14 times in the previous 29 months, and made no mention of the ventral fin not being installed.
Probable cause:
The pilot's excessive climb and turning maneuver at low altitude, the pilot's inadvertent stall, and the intentional operation of the airplane with the required stall warning system disabled. Factors associated with this accident were the pilot's overconfidence in the modified airplane's ability, the uninstalled ventral fin, inadequate compliance with the STC by the company, unclear information by the manufacturer, and inadequate surveillance by the FAA.
Final Report:

Crash of a Cessna 207A Skywagon neat Twin Hills: 1 killed

Date & Time: Sep 26, 1997 at 1306 LT
Operator:
Registration:
N9984M
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Manokotak - Togiak
MSN:
207-0774
YOM:
1984
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
7470
Captain / Total hours on type:
1000.00
Aircraft flight hours:
14089
Circumstances:
The flight departed with 180 pounds of cargo after deplaning a passenger. Three company pilots overheard the accident pilot report that he was 13 minutes from his destination. The overdue aircraft was located by company airplanes about 700 feet MSL, on the east (downwind) side of an 890 feet msl pass. The airplane impacted on a 330 degree heading and perpendicular to the axis of the canyon/pass (oriented east-west), in a flat attitude, with no ground scars leading to the wreckage. No anomalies were found with the airplane, and all blades on the propeller exhibited torsional twisting and leading edge gouging. A westerly wind of seven to nine knots existed and numerous pilots reported the mountain passes were not obscured by clouds. Photographs from the pilot's camera depicted views of the accident canyon, with the pass and accident site above the altitude from which the photographs were taken. These photographs contained the date of the accident. Numerous depressant and stimulant, over-the-counter cold and asthma medications were found in the pilot's flight bag. Toxicological tests detected several over-the counter medications used for cold and asthma symptoms with illness effect of distraction or sensory disturbance. As a result of the condition for which the drugs were ingested may have also played a role in the accident.
Probable cause:
Improper in-flight planning/decision by the pilot, and his failure to maintain sufficient altitude over mountainous terrain. Factors related to the accident were downdraft conditions, mountainous/hilly terrain, and the use of over-the-counter medications.
Final Report:

Crash of a Rockwell Aero Commander 500A in Ketchikan: 2 killed

Date & Time: Sep 6, 1997 at 1300 LT
Registration:
N543AN
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Wrangell – Everett
MSN:
500-908-17
YOM:
1960
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
2577
Captain / Total hours on type:
81.00
Aircraft flight hours:
6679
Circumstances:
The aircraft had an in-flight breakup when the left wing and tail section separated. Post accident inspection revealed a right engine main fuel supply line progressive rupture, only trace amounts of fuel in the fuel lines, and no rotational damage to the right engine. Pre accident, long term, fuel leak evidence surrounded the ruptured line. The right propeller was not feathered. The left wing D-tube rib at station 127 exhibited compressive buckling. Left wing fractures were upward, and horizontal stabilizer deformation was downward. During an actual loss of engine power in the airplane 17 months before this accident, the pilot had feathered the incorrect propeller. Both a mechanic, and an FAA safety counselor, who were familiar with the pilot, described him as able to be disoriented, and reliant on GPS for navigation. He had stated five months before the accident that he did not feel his instrument flying skills were proficient, and desired training. On the day of the accident, weather was visual meteorological conditions, with layered clouds above 2,200 feet mean sea level. The pilot stated to the FAA weather briefer that he wanted to make the flight under visual conditions. The flight route and altitude was unknown.
Probable cause:
The rupture of the right engine fuel supply line as a result of inadequate inspection by the pilot/mechanic, and the pilot's excessive pull up which resulted in exceeding the design stress limits of the airplane. Factors were the improper emergency procedures and failure to feather the propeller.
Final Report: