Crash of a Cessna 414A Chancellor near Wonthaggi

Date & Time: Oct 27, 1989 at 0833 LT
Type of aircraft:
Operator:
Registration:
VH-SDV
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Melbourne – Port Welshpool
MSN:
414A-0261
YOM:
1979
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The pilot reported that whilst enroute from Essendon to Wonthaggi he descended to the lowest safe altitude of 3600 feet above sea level, lowered the landing gear, reduced power and airspeed to counter the effect of turbulence and entered a holding pattern to the south south west of the Wonthaggi navigation aid. During the holding pattern the aircraft descended until it collided with trees that were 865 feet above sea level. The weather at the time included gale force winds, rain and low cloud. There were no thunderstorms or microbursts in the area, however, other aircraft reported a very low cloud base and severe turbulence. A few minutes prior to the accident ground witnesses, south south west of the accident site, reported an aircraft matching the description of VH-SDV, flying below a low, misty, ragged cloud base. There was no record of another aircraft in the area at the time. Information was available which indicated that the aircraft had descended below 3600 feet during the approach to Wonthaggi. The passengers reported that the pilot gave no indication of any problem or danger. Until the impact, they believed the aircraft was descending normally for a landing at Port Welshpool.
Probable cause:
No aircraft defects were found which may have been factors in the accident. The investigation indicates that the pilot attempted to fly under the low cloud base, in order to reach the Port Welshpool destination where weather conditions were earlier reported to have been partially sunny. Port Welshpool is not serviced by an approved navigation aid. The pilot attempted to descend below the cloud base, hoping to achieve visual flight conditions to continue to his destination.
Final Report:

Crash of a De Havilland DHC-2 Beaver in Orroroo: 1 killed

Date & Time: Sep 20, 1989 at 1222 LT
Type of aircraft:
Operator:
Registration:
VH-IDD
Flight Phase:
Survivors:
No
Schedule:
Orroroo - Orroroo
MSN:
1532
YOM:
1963
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The aircraft had been delayed in servicing and repair and had only been released six weeks prior to the accident. This delay had caused the operator/pilot to fall behind in his commitments and, according to some witnesses, caused him to worry about the situation. On the day of the accident, the pilot had just completed spraying a 243 hectare paddock and had landed to reload. After take-off for the new task, the pilot was seen to make an aerial inspection of the paddock before entering the first swath run. At the end of this run, the aircraft collided with a Single Wire Earth Return (SWER) powerline and crashed. It was later shown that the aircraft was in a bank to the right of about 18 degrees. The SWER line ran across one end of the paddock at an angle and on the crop side of a windmill just inside the fence which bordered the road. The line contacted the right maingear and outboard sprayboom attachment struts on the right wing. The wire broke after impact but the aircraft hit the ground heavily on the right main gear. The gear detached from the aircraft, the propeller struck the ground and the aircraft slewed around as it came to rest after some 27 metres of ground travel. The front half of the aircraft was destroyed by fire which broke out almost immediately the aircraft stopped. The pilot, sole on board, was killed.
Probable cause:
Two main hypothesis were proposed. One was that the pilot was distracted from a less than demanding task by business worries. The other was that the pilot had perceived that the SWER line was on the right of the windmill and outside the fence and therefore did not present an obstacle to his procedure turn. Neither hypothesis could be substantiated. An additional concern was the fact that the pilot had died from impact injuries in an accident that, prima facie, was survivable. Concern focused on whether the pilot had secured his harness properly and/or whether the inertia reel had failed. Detailed engineering inspection of the inertia reel by the Bureau and the manufacturer could not positively determine the mode of operation of the inertia reel. However, the post mortem report showed that the nature of injuries to the pilot, while sufficient to cause death prior to the fire, were such as to indicate that the inertia reel had probably not failed. The pilot did not see the powerline in time to avoid a collision.
Final Report:

Crash of a Piper PA-31-310 Navajo in Carnarvon

Date & Time: Aug 18, 1989 at 1856 LT
Type of aircraft:
Operator:
Registration:
VH-DEG
Flight Type:
Survivors:
Yes
Schedule:
Geraldton – Carnarvon
MSN:
31-7812098
YOM:
1978
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
At approximately 1809, (23 minutes before last light) during final approach to landing at Carnarvon, the pilot noticed that the landing gear had not extended correctly. The aircraft remained in the circuit area whilst the pilot attempted to lower the landing gear using both manual and emergency methods. He also sought assistance from the company's, Perth based, duty pilot and Carnarvon based engineers. After exhausting all possible methods of lowering the gear the pilot decided to land with the landing gear and flaps retracted. The pilot rejected a landing on the sealed runways because he was apprehensive that it would cause unnecessary damage to the aircraft and could result in a fire. He considered landing in a riverbed (rejected by the Senior Operational Controller), alongside one of the sealed runways (the surface was unsuitable) and on one of the dirt strips. The pilot was offered a flare path on dirt runway 27 however, he declined and indicated that he would try to land using the available light. At 1856 (last light was at 1832) the pilot attempted a landing on runway 27. On late final approach the aircraft collided with a one and a half metre high levy bank, 270 metres short and 115 metres to the right of the threshold. The pilot was trapped in the wreckage for some time after the aircraft came to a stop. While the passenger was slightly injured, the pilot was seriously wounded.
Probable cause:
The landing gear problem arose when the left main landing gear would not lower. Examination of the aircraft revealed that both hinges fitted to the inboard landing gear door had fractured. The forward hinge had fractured as a result of fatigue and the rear hinge as a result of overload. The fatigue crack initiation had occurred at a sharp edged, prominent forging flash on the inner radius of the hinge and had grown over approximately 4000 load cycles. A similar fatigue problem had been identified on an earlier version of the hinge (part number 46653-00), however, regular inspections for fatigue cracking were discontinued when hinges with part number 47529-32 (as fitted to VH-DEG) were introduced in 1980. Similar fatigue cracking was found in the forward door hinge of another PA31 during the investigation. The fractured hinges jammed the left main landing gear mechanism and neither the normal or emergency extension systems could extend the gear. The pilot was apprehensive about wheels up landings. Much of his decision making was aimed at reducing the risk of fire and minimising the damage the aircraft would sustain during the landing. eg. Selection of a dirt runway instead of the sealed strip, landing with flaps retracted etc. During the pilot's attempts to rectify the landing gear problem, and up until the time of his touchdown, he was subjected to considerable radio transmission traffic involving questions, directions and suggestions which distracted him from his primary tasks. The pilot indicated on at least two occasions that he was ready to land, however, each time advice and questions from the ground personnel involved overrode his intentions. When the pilot was asked if he wanted a flare path on runway 27 there was still some natural light available and he was intending to land. However, by the time he was able to make his final approach it was dark and he was unable to see the ground. Studies have shown that aircrew subjected to high levels of stress can suffer skill fatigue and cognitive task saturation, which in turn can lead to a breakdown in the decision making process. It was apparent from the pilot's radio transmissions and the quality of the decisions made in the latter part of the flight that his information processing and decision making abilities had been degraded by the stress of continuous radio transmissions and continuous, and sometimes conflicting, instructions. As a result, what should have been a relatively simple wheels up landing in daylight was turned into an extremely difficult wheels up landing at night. With the landing gear retracted the aircraft's taxi and landing lights were not available to the pilot.
The following factors were considered relevant to the development of the accident:
1. Manufacturing defect. A forging flash created a stress concentration which led to fatigue cracking.
2. Inadequate inspection procedures. Previous inspection procedures introduced to disclose similar cracking were withdrawn on the introduction of later part numbered hinges.
3. Apprehension of the pilot. The pilot was apprehensive about apparently significant dangers of landing an aircraft, wheels up, on a sealed runway.
4. Inordinate interference in aircraft operations by ground based advisors. The ground advisors input overrode the pilot's decision on a number of occasions with the result that a simple exercise became very complicated.
5. Cognitive task saturation and skill fatigue. The amount of information, advice and suggestions being passed via the radio communications system overloaded the pilot decision making abilities.
6. Improper in-flight decisions. As a result of task saturation the final decision made by the pilot to attempt a night landing on an unlighted strip was incorrect.
7. The pilot did not see and therefore was unable to avoid the levy bank.
Final Report:

Crash of a Beechcraft 65-B80 Queen Air in Tolmie: 1 killed

Date & Time: Jul 6, 1989 at 0341 LT
Type of aircraft:
Operator:
Registration:
VH-XAE
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Sydney - Melbourne
MSN:
LD-305
YOM:
1966
Location:
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
At 0341 hours EST on 6 July 1989, Beechcraft 80 Queen Air aircraft registered VH-XAE collided with high voltage power lines and descended rapidly, contacting the ground three kilometres north-east of Tolmie. The pilot, who was the only occupant, received fatal injuries. There was no fire. The aircraft was on a flight from Sydney to Melbourne cruising at 8000 feet. Persons in the accident area heard an aircraft flying very low over their houses, then observed a flash of light and heard the sound of ground impact. A ground search was commenced but due to falling snow and very poor visibility the wreckage was not found until about 0745 hours in daylight. The elevation of the ground at the accident site was approximately 2,700 feet above sea level.
Probable cause:
The exact cause of the accident could not be determined.
Final Report:

Crash of a De Havilland DHC-2 Beaver off Cape Richards

Date & Time: Jul 5, 1989 at 1645 LT
Type of aircraft:
Registration:
VH-OCW
Flight Phase:
Survivors:
Yes
Schedule:
Cap Richards-Townsville
MSN:
436
YOM:
1953
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft was scheduled to conduct three round trips between Townsville and Cape Richards, with a stop at Orpheus Island on some legs, during the day. The pilot involved in the accident flew the first and third trips and another pilot flew the second. After the first trip the pilot reported that he pumped the floats out and considered that the quantity of water removed was normal. On the third trip he picked up a "standby" passenger at Orpheus Island. On arrival at Cape Richards the scheduled six passengers were loaded. A witness employed by the resort to handle the aircraft and passengers on the island reported that the floats appeared to be sitting in the water such that the water was above the normal water line on the floats. Examination of the aircraft loading indicated that the aircraft was overweight and the centre of gravity was just inside the rear limit. The pilot reported taxiing at 1613 hours with eight persons on board. At 1624 hours he reported that he was returning to unload one passenger. In that time two takeoff attempts into the north-east were made. The wind in the bay where the attempts were made was a light northerly. The pilot again reported taxiing at 1634 hours with seven persons on board. A further two takeoff attempts were made. On the final attempt the pilot did not taxi as far into the bay as on previous occasions. The takeoff was continued well out beyond the shelter of the island into an area where the wind was easterly at about 10 knots, and the swell was 1 to 1.5 metres. The pilot reported that the aircraft had attained an indicated airspeed of 55 knots, and he intended to fly it off the water at 57 knots. The right float had lifted from the water and it hit a wave which pushed the right wing up. The pilot was unable to lift the left wing which hit the water, causing the aircraft to cart-wheel.
Probable cause:
The following factors were considered relevant to the development of the accident:
1. The pilot selected the incorrect takeoff direction for the wind conditions prevailing.
2. The pilot continued the takeoff into an area of unsuitable swell. This accident was not the subject of an on-scene investigation.
Final Report:

Crash of a Britten-Norman BN-2A-26 Islander off Derby

Date & Time: May 22, 1989 at 1350 LT
Type of aircraft:
Registration:
VH-BSN
Flight Phase:
Survivors:
Yes
Schedule:
Cockatoo Island - Derby
MSN:
3005
YOM:
1982
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The pilot had planned the direct track for the flight from Cockatoo Island to Derby at 5,500 feet above sea level. When the pilot gave his DEPARTURE call he amended his cruising level to below 5,000 feet. No further calls were received from the aircraft. The Cockatoo Island workboat was 56 kilometres north-north-west of Derby, and approximately 20 kilometres west of the direct track between Cockatoo Island and Derby. The crew of the boat observed an aircraft approaching at very low level. The aircraft passed over the boat approximately 5-7 metres above the deck, and entered a right hand turn. During the turn the right wing tip struck the water causing the aircraft to cartwheel and crash about 400 metres from the boat. The fuselage broke open on impact and the occupants were subsequently rescued by the crew of the boat.
Probable cause:
The pilot declined to provide any information which might have clarified the circumstances of the accident, however, available information indicates that he carried out an unauthorized low pass over the boat. During the turn following the low pass, he misjudged the aircraft's height and the right wing tip struck the water.
The following factors were considered relevant to the development of the accident:
- The pilot was neither trained nor authorized to conduct operations at low level,
- The pilot exercised poor judgement by operating at an unnecessarily low height,
- The pilot misjudged his height above the water.
Final Report:

Crash of a Piper PA-61 Aerostar (Ted Smith 601) off Wollongong: 1 killed

Date & Time: Apr 2, 1989 at 1030 LT
Operator:
Registration:
VH-NOE
Flight Type:
Survivors:
No
Schedule:
Sydney - Wollongong
MSN:
61-0849-8162154
YOM:
1981
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The pilot was to conduct a charter with passengers from Sydney to Wollongong, Nowra, Canberra and return to Sydney, departing Sydney at about 10.00am. Earlier that morning he positioned the aircraft at Sydney and had it refuelled. When the passengers arrived he explained that the weather in the various destinations was very poor and that there was a possibility they may not be able to land. However, he was prepared to give it a try. As the passengers were pressed for time, they could not afford to take a chance with the weather and so they decided to drive. They told the pilot that if he could land at Wollongong later that day they would continue the flight with him. However, they impressed on him that there was no pressure for him to depart immediately as they would not be in Wollongong for several hours. After driving for a short time, the passengers decided that the weather did not appear as if it would improve, and believed that it would be better to complete the journey by car. They contacted the charter company by phone to cancel the charter, but the pilot had already departed. The flight to Wollongong appears to have proceeded normally where the pilot reported commencing an NDB approach, and would call again at a specified time. This was the last message received from the pilot. Witnesses on the ground at Wollongong, and on a yacht 20 nautical miles to the east of Wollongong reported hearing an aircraft flying at approximately 1000 to 2000 feet in the low cloud and rain. There were no other known aircraft in the area. Later that day a helicopter discovered wreckage debris in the sea, which was confirmed as being from the aircraft. The search was discontinued due to very poor weather and visibility, and cancelled two weeks later when further efforts failed to locate any trace of the aircraft.
Probable cause:
The reason why the aircraft flew into the sea could not be determined.
Final Report:

Crash of a Mitsubishi MU-2B-60 Marquise in Sturt Meadows Station: 10 killed

Date & Time: Dec 16, 1988 at 1015 LT
Type of aircraft:
Registration:
VH-BBA
Flight Phase:
Survivors:
No
Schedule:
Perth – Bellevue Mine – Kalgoorlie – Leinster – Nevoria Mine
MSN:
782
YOM:
1980
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
20
Captain / Total flying hours:
6249
Captain / Total hours on type:
134.00
Aircraft flight hours:
2827
Circumstances:
The aircraft had been chartered for a return flight from Perth to Bellevue Mine, Kalgoorlie and Nevoria Mine. The aircraft departed Perth on 15 December and arrived at Bellevue Mine after an uneventful flight. The following morning the pilot telephoned Kalgoorlie Flight Service Unit (FSU) and obtained brief details of expected winds for the flight to Kalgoorlie, as well as a forecast of the weather for the aircraft's arrival. He then submitted details of the flight to the flight service officer (FSO), at the same time commenting that there was some adverse weather in the Bellevue Mine area. The flight plan indicated that the pilot intended to climb to flight level (FL) 195 after take-off, with a time interval of 27 min to pass Leonora and a further 22 min to reach Kalgoorlie. The flight plan was amended after take-off to include a brief stop at Leinster. At 0940 hours the aircraft departed for Leinster, 5 km from Bellevue Mine. (This short flight was conducted to pick up passenger baggage.) At 0957 hours the pilot reported to the Kalgoorlie FSU that the aircraft had departed Leinster at 0955 hours and was climbing to FL 195. At 1008 hours he requested traffic information for a climb to FL 210 and, after being advised that there was no traffic, replied that he was climbing to that level. He also remarked that there were some big clouds in the area. No further communications were received from the aircraft. At approximately 1015 hours the aircraft crashed on Sturt Meadows Station. The crash site was approximately 1200 ft above sea level. All 10 occupants were killed.
Probable cause:
It is probable that the pilot did not have an adequate understanding of the operations of the MU-2B-60 aircraft at high altitude. The meteorological conditions were conducive to the formation of ice on aircraft flying in cloud above the freezing level. It is probable that loss of control occurred above the freezing level on climb to an amended altitude of FL 210.
Final Report:

Crash of a De Havilland DHC-2 Beaver in Lake Monduran: 3 killed

Date & Time: Dec 5, 1988 at 1200 LT
Type of aircraft:
Operator:
Registration:
VH-BSL
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Bundaberg - Bundaberg
MSN:
1618
YOM:
1966
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
The aircraft reported departing Bundaberg for Monduran Dam on a no SAR flight at 1135 hrs EST with three persons on board and an endurance of 270 minutes. The purpose of the flight was to complete the endorsement of the pilot under check and to assess the suitability of an area of water on the coast to where the passenger, who was the regular pilot of the aircraft, was to fly the aircraft the following day. The pilot in command had flown 27 hours in the previous three months, of which 9 were on type. The pilot under check had flown only one hour in the last three months. This flight had been in VH-BSL. At approximately 1200 hrs, the aircraft was observed in the Lake Monduran area. It flew two left hand circuits, landing into wind towards the dam wall each time. After the second takeoff, it turned left and was seen heading north from the lake. Nothing further was heard or seen of the aircraft. Following an extensive search, the wreckage was located six days later lying inverted in 15 metres of water approximately 2 km WNW of the dam wall in the area of the junction of the main east-west channel and a northsouth channel of the lake. Both floats had separated from the aircraft and the right float was severely torn for about half its length. There was substantial water impact damage to the windshield frame/cockpit roof area and to the upper leading edge surfaces of both wings.
Probable cause:
No fault was found with the aircraft or its systems which might have contributed to the accident. It could not be determined who was manipulating the controls of the aircraft at the time of the accident. Evidence was obtained that it was the habit of the check pilot to have pilots undergoing endorsement or check to fly two circuits landing into wind and then to carry out crosswind landings. The check pilot and the pilot under check had previously operated at the dam and alighted on to both the east/west and the north/south channels. Having been observed to fly two into wind circuits and then head north and not be sighted again, it is possible that the aircraft then commenced crosswind operations onto the north/south arm of the lake, landing in a southerly direction with a crosswind from the left. Information from the Bureau of Meteorology indicated that the surface wind in the area at the time of the accident was 090` magnetic at 15 knots. This information was confirmed by witnesses at the dam wall who observed white caps on the surface of the dam. The north/south channel of the lake was bounded on its east side by steep hills rising to 70 metres above water level. The effect of this high ground was to partially blanket the north/south channel from the easterly wind. The position of the wreckage was in the area where the wind shadow effect would have ended and where the wind would have blown at full strength along the main east/west channel of the lake. The crosswind limitation for the aircraft as stated in the flight manual was 8.7 knots. Commenting in early 1988 on an enquiry regarding the raising of this limit, the aircraft manufacturer emphasised the 8.7 knot limit and advised that any test work to raise the limit should proceed cautiously starting at or below the current (8.7 knot) limit. If the aircraft was conducting crosswind operations in the north/south channel, and suddenly encountered a 15 knot crosswind on exiting the wind shadow area, the control difficulties confronting the pilot could have been significant. The aircraft wreckage was intact except for the floats which had been torn off by water impact forces. The right float was severely damaged while the left was intact. The forward tip of the right float had been severed by the propeller. The remaining forward section had then been forced upwards and outboard and had broken off. This weakened the float support structure, causing it to fail, and allowing the remaining section of the right float to strike the right side of the fuselage just aft of the cabin. Damage of this type an magnitude was most probably caused by the nose of the right float digging into the surface of the lake at relatively high speed. For this to occur, the aircraft was banked to the right at float impact - a possible consequence of encountering a strong crosswind from the left. There was no evidence that the aircraft had hit a submerged object. The factors associated with the development of this accident could not be determined.
Final Report:

Crash of a Piper PA-31-310 Navajo off Stanwell Park: 3 killed

Date & Time: Nov 1, 1988 at 1740 LT
Type of aircraft:
Registration:
VH-DAP
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Nowra - Nowra
MSN:
31-364
YOM:
1968
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
The aircraft had been modified by the installation of an air driven winch for the purpose of towing gunnery targets and was operating in conjunction with a warship for scheduled sea/air gunnery practise. Weather conditions in the area were reported as overcast at 4000 feet, wind 060 degrees / 15-20 knots and visibility of 15-20 kilometres. At about 1717 hours the aircraft was instructed to commence carrying out gunnery tracking runs at an altitude of 1000 feet with the sleeve target not deployed. Between 1720 and 1735 hours the aircraft carried out two such runs from the west and east. The aircraft then tracked to the south, away from the ship, to a distance of about 10 kilometres. At about 1738 the aircraft was instructed to turn inbound for a run from astern. At about 1739 hours the pilot reported engine problems and about one minute later advised "I've got problems, Mayday, I'm going in". Crewmen stationed near the stern of the ship, reported seeing the aircraft dive into the sea. The warship was immediately turned back towards the crash position. Other warships and aircraft were also ordered to the crash position. The only wreckage sighted was at the crash datum and was believed to have been a section of wing. This wreckage was located about two metres below the surface and sank before it could be recovered. The approximate depth of water at the crash position is 450 fathoms. No trace of the aircraft or its occupants has been discovered to date.
Probable cause:
The subsequent investigation established that the flight crew were properly qualified to conduct the flight, and that the aircraft was appropriately certified and maintained. The flight was conducted in accordance with the conditions of the operating contract. At the time of the occurrence the aircraft had not deployed the sleeve target and no firing was being carried out. No evidence was found to suggest an in-flight structural failure or fire. The installation of the target towing equipment was not considered to have been a factor in the development of the accident. There was a loss of control of the aircraft following an apparent engine malfunction. The precise reasons for the accident have not been established.
The following factors were considered relevant to the development of the accident:
1. Apparent engine failure or malfunction.
2. Control of the aircraft was lost for reasons which have not been determined.
Final Report: