Crash of a Rockwell Aero Commander 500 in Laredo: 7 killed

Date & Time: Sep 23, 1978 at 2340 LT
Registration:
N6244B
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Fort Worth - San Antonio - Laredo
MSN:
500-652-13
YOM:
1958
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
310
Captain / Total hours on type:
142.00
Circumstances:
While approaching Laredo area by night, the pilot encountered marginal weather conditions with low ceiling and limited visibility. He completed several turns when the airplane entered a dive and crashed. The airplane was totally destroyed upon impact and all seven occupants were killed.
Probable cause:
Uncontrolled descent after the pilot initiated flight in adverse weather conditions. The following contributing factors were reported:
- The pilot became lost/disoriented,
- Spatial disorientation,
- Low ceiling,
- Haze,
- Dark night,
- VFR flight not recommended,
- During last 11 minutes of flight, heading changed thru 630°.
Final Report:

Crash of a Swearingen SA226TC Metro II in Austin

Date & Time: Aug 13, 1978 at 1643 LT
Type of aircraft:
Operator:
Registration:
N300TL
Survivors:
Yes
Schedule:
San Antonio - Austin
MSN:
TC-238E
YOM:
1977
Crew on board:
2
Crew fatalities:
Pax on board:
16
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4985
Captain / Total hours on type:
815.00
Circumstances:
On final approach to Austin-Robert Mueller Airport, the left engine failed. The crew continued the approach but forgot to lower the landing gear. The airplane belly landed and slid for dozen yards before coming to rest. Two occupants, among them the copilot, were seriously injured while 16 other people escaped with minor injuries. The aircraft was written off.
Probable cause:
Failure of the left engine on final approach due to inadequate preflight preparation on part of the flying crew. The following contributing factors were reported:
- Mismanagement of fuel,
- Fuel starvation,
- Failed to assure the gear was down and locked,
- Improper emergency procedures,
- Failed to follow approved procedures,
- Aircraft refueled in right wing with 125 gallons before 18 minutes flight,
- Crossflow valve found off.
Final Report:

Crash of a Swearingen SA226T Merlin IIIA in San Antonio: 2 killed

Date & Time: Feb 3, 1977 at 0054 LT
Registration:
N34SM
Survivors:
No
Schedule:
Seattle – San Antonio
MSN:
T-263
YOM:
1976
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
18812
Captain / Total hours on type:
283.00
Circumstances:
While approaching San Antonio Airport by night, the crew encountered poor weather conditions with low ceiling, rain and fog. Too low, the airplane struck trees and crashed in flames few miles short of runway 12R. It was destroyed by a post crash fire and both pilots were killed.
Probable cause:
Collision with trees on initial approach due to improper IFR operation. The following contributing factors were reported:
- Low ceiling (200 feet),
- Rain,
- Fog,
- Cleared for ILS approach runway 12R, navigation receiver turned to frequency for ILS approach to runway 03R.
Final Report:

Crash of a Cessna 421A Golden Eagle I in Tulsa

Date & Time: Jan 11, 1974 at 1754 LT
Type of aircraft:
Operator:
Registration:
N4005L
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Tulsa - San Antonio
MSN:
421A-0005
YOM:
1967
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2305
Captain / Total hours on type:
121.00
Circumstances:
During the takeoff roll at Tulsa Airport on an runway covered by slush, the pilot started the rotation prematurely. The airplane climbed a few feet then stalled and crashed back onto the runway. Out of control, it veered off runway and came to rest. Both occupants were slightly injured and the aircraft was damaged beyond repair.
Probable cause:
Engine malfunction during takeoff run and initial climb. The following factors were reported:
- Inadequate preflight preparation,
- Premature liftoff,
- Failed to obtain flying speed,
- Disregard of good operating practice,
- Improper emergency procedures,
- Ice/slush on runway,
- Partial loss of power on one engine,
- Engines check ok prior to takeoff,
- No full power runup due to ice on runway,
- Rotated below VNC,
- Observers heard engine backfire.
Final Report:

Crash of a Beechcraft 65-B80 Queen Air in Kent: 4 killed

Date & Time: Dec 29, 1972 at 1645 LT
Type of aircraft:
Operator:
Registration:
N9867
Flight Type:
Survivors:
No
Schedule:
San Antonio - Kent
MSN:
LD-114
YOM:
1963
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
28000
Captain / Total hours on type:
80.00
Circumstances:
The pilot was completing a last turn to reach the approach path when the twin engine airplane stalled and crashed in flames. The airplane was destroyed and all four occupants have been killed.
Probable cause:
The pilot failed to maintain flying speed, causing the aircraft to stall. The aircraft was apparently turning from base leg to final approach and was in a clean configuration.
Final Report:

Crash of a Douglas DC-6A in San Antonio: 3 killed

Date & Time: Jan 31, 1967 at 0320 LT
Type of aircraft:
Operator:
Registration:
N640NA
Flight Type:
Survivors:
No
MSN:
45475
YOM:
1958
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
16179
Captain / Total hours on type:
348.00
Circumstances:
The crew was completing a cargo flight to Kelly AFB, San Antonio, Texas, on a subcontract for the US Air Force. While descending to Kelly AFB, the crew decided to divert to San Antonio-Intl Airport for unknown reason. While on a night approach, the pilot-in-command failed to realize his altitude was too low when the airplane struck trees, stalled and crashed in a cleef. The aircraft was destroyed and all three crew members were killed. At the time of the accident, the airplane was 1,100 feet below the glide.
Probable cause:
The cause of the accident was not determined.
Final Report:

Crash of a Curtiss C-46F-1-CU Commando in Katy: 2 killed

Date & Time: Jan 22, 1961 at 1609 LT
Type of aircraft:
Operator:
Registration:
N1308V
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
San Antonio – Mobile
MSN:
22583
YOM:
1945
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
En route from San Antonio to Mobile at an altitude of 2,500 feet, the crew informed ATC that the left engine caught fire. He elected to divert to the nearest airport but few minutes later, the left wing detached and the airplane crashed in flames in a field located in Katy, about 27 miles west of Houston. The aircraft was destroyed and both pilots were killed.
Probable cause:
It was determined that the 8th cylinder on the left engine failed in flight, causing hydraulic leak. The oil spread in the engine nacelle and caught fire while contacting high temperature equipment. As the fire could not be contained, it spread to the left wing which detached shortly later.

Crash of a Curtiss C-46A-40-CU Commando in Miami: 4 killed

Date & Time: Aug 4, 1952 at 0030 LT
Type of aircraft:
Operator:
Registration:
N79096
Flight Type:
Survivors:
No
Schedule:
Burbank – San Antonio – Miami
MSN:
27038
YOM:
1944
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
5823
Captain / Total hours on type:
1412.00
Circumstances:
The aircraft departed Burbank August 3 on a nonstop ferry flight to San Antonio, Texas. The aircraft, piloted by Douglas T. Dell, Chief Pilot of Resort Airlines, arrived at its destination at 2345 following an uneventful flight VFR direct. Two minor discrepancies were reported by the pilot on arrival at San Antonio; that the hydraulic system cycle every one minute and 20 seconds, and that the left engine dropped 100 RPM'S on the left magneto. These discrepancies were corrected y Slick Airways' maintenance crew at San Antonio, and at 1653, August 4, the aircraft departed for Miami, Florida, nonstop on a VFR flight plan to cruise at 10,000 feet. The crew on this flight consisted of Captain Robert E. Smith and Copilot John N. Goodman. Two non revenue passengers boarded the plane at San Antonio for the flight to Miami. The cabin of the aircraft contained no passenger seats. This equipment was to have been installed at Miami prior to placing the aircraft in service. The cockpit was equipped to accommodate a crew of three. One safety belt had been installed to accommodate one person riding in the cabin; however, no approved type seat was provided. The aircraft and engine log covering the flight from San Antonio to Miami, as well as a mutilated flight plan and log sheet recovered from the wreckage, indicated that the flight was made at an altitude of 10,000 feet. All entries in the flight plan and log sheet covering check points between San Antonio and Miami were completed up to and including Cross City, Florida, the last check point before reaching Miami. The last entry gave the estimated time of arrival at Miami as 2324. The estimated and actual time over the various cheek points along the route as reflected in the flight log indicated that the flight had progressed very nearly as estimated. On the recovered aircraft and engine log covering the San Antonio-Miami flight under heading entitled "Difficulties Noted During Flight," there was found this entry, "EXCESSIVE PLAY ON ELE." The log sheet had been signed by both the captain and the copilot. At approximately 2317 the Miami tower operator received a broken radio transmission from which he was unable to identify either the aircraft or the nature of the call. An attempt to establish contact was unsuccessful until the following message was received. "Miami tower - NAN 79096 requesting emergency landing." Two-way contact was established and at approximately 2318 the flight was cleared to land on Runway 27L (preferential runway for calm wind) and the pilot was advised that if this runway was not satisfactory any runway was available. In the next transmission, the pilot advised the tower that the elevator control linkage was broken and he would attempt to bring the aircraft in, using trim tabs only. His position was given as high over the west boundary of the airport at an altitude estimated by the tower operator as 3,000 feet. Since the use of Runway 9R would permit an approach to be made over very thinly populated areas, it was suggested to the pilot that if it was satisfactory with him, Runway 9R be used. The pilot advised the tower that the change of runways was satisfactory. The area was cleared of all traffic while the aircraft made a circuit of the field, letting down slowly with a wide approach to a long final. As the aircraft neared the approach end of the runway, it appeared to tower personnel to be lined up properly. The following is quoted from testimony of the tower operator: "As the aircraft neared the approach end of the runway and at an altitude of approximately 150 feet, the nose of the aircraft appeared to come up slightly, then crop about the same degree below the horizon. This was repeated several times, each time two maneuver becoming more violent, with the last pull-up very stoop. At an altitude of approximately 150 feet the aircraft appeared to fall off slightly on the left wing, the nose dropped, and the aircraft struck the ground almost vertically." The fire which followed the crash was quickly extinguished by the airport fire-fighting equipment, the crews of which had been altered and were in standby position prior to the crash. The aircraft was destroyed and all four occupants were killed.
Probable cause:
The Board finds that the probable cause of this accident was failure of the elevator control system in flight, resulting in loss of control of the aircraft during landing. The failure of the elevator control system was the result of poor workmanship and inadequate inspection during overhaul and modification. The following findings were pointed out:
- Weather was not considered a factor in this accident,
- Total flight time on the aircraft since overhaul and modification was approximately 13 hours 27 minutes,
- At 2318 the flight advised the Miami tower that the elevator control linkage was broken and elevators functioning by use of trim tabs only,
- The aircraft became uncontrollable and crashed during an attempted landing on Runway 09R,
- The push-pull tube was found disconnected from its point of attachment on the elevator bellerrank.
Final Report:

Crash of a Boeing B-29A-40-BN Superfortress in Northcliffe

Date & Time: Jun 21, 1951
Type of aircraft:
Operator:
Registration:
44-61678
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
11155
YOM:
1944
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
En route, an engine caught fire and failed. All occupants decided to bail out and abandoned the aircraft that dove into the ground and crashed in a field located in Northcliffe, northeast suburb of San Antonio. There were no casualties but the aircraft was destroyed upon impact.
Probable cause:
Engine fire and failure in flight.

Crash of a Douglas C-47B-1-DL Skytrain near El Bonito: 9 killed

Date & Time: Feb 28, 1949
Operator:
Registration:
43-16256
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
El paso – San Antonio
MSN:
20722
YOM:
1944
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
9
Circumstances:
En route, the crew encountered poor weather conditions and a reduced visibility due to fog. The aircraft went off track and hit a mountain located near El Bonito, about 75 miles southwest of Del Rio. All nine occupants were killed.