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Crash of a Socata TBM-850 in Racine: 1 killed

Date & Time: Sep 5, 2011 at 1833 LT
Type of aircraft:
Operator:
Registration:
N850SY
Flight Type:
Survivors:
No
Schedule:
Mosinee – Waukegan
MSN:
546
YOM:
2010
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2075
Captain / Total hours on type:
165.00
Aircraft flight hours:
217
Circumstances:
During cruise flight, the pilot reported to an air traffic controller that the airplane was having engine fuel pressure problems. The controller advised the pilot of available airports for landing if necessary and asked the pilot's intentions. The pilot chose to continue the flight. GPS data recorded by an onboard avionics system indicated that the engine had momentarily lost total power about 20 seconds before the pilot reported a problem to the controller. About 7 minutes later, when the airplane was about 7,000 feet above ground level, the engine lost total power again, and power was not restored for the remainder of the flight. The pilot attempted to glide to an airport about 10 miles away, but the airplane crashed in a field about 3 miles from the airport. GPS data showed a loss of fuel pressure before each of the engine power losses and prolonged lateral g forces consistent with a side-slip flight condition. The rudder trim tab was found displaced to the left about 3/8 inch. Flight testing and recorded flight data revealed that the rudder trim tab displacement was consistent with that required to achieve no side slip during a typical climb segment. The GPS and flight data indicated that the lateral g-forces increased as the airplane leveled off and accelerated, indicating that the automatic rudder trim feature of the yaw damper system was either not engaged or not operating. The recorded data indicated autopilot system engagement, which should have automatically engaged the yaw damper system. However, the data indicated the yaw damper was not engaged; the yaw damper could have subsequently been turned off by several means not recorded by the avionics system. Testing of the manual electric rudder (yaw) trim system revealed no anomalies, indicating that the pilot would have still been able to trim the airplane using the manual system. It is likely that the pilot's failure to properly trim the airplane's rudder led to a prolonged uncoordinated flight condition. Although the fuel tank system is designed to prevent unporting of the fuel lines during momentary periods of uncoordinated flight, it is not intended to do so for extended periods of uncoordinated flight. Therefore, the fuel tank feed line likely unported during the prolonged uncoordinated flight, which resulted in the subsequent loss of fuel pressure and engine power. The propeller and propeller controls were not in the feathered position, thus the windmilling propeller would have increased the airplane's descent rate during the glide portion of the flight. The glide airspeed used by the pilot was 20 knots below the airspeed recommended by the Pilot's Operating Handbook (POH), and the reduced airspeed also would have increased the airplane's descent rate during the glide. The flight and GPS data indicated that the airplane had a gliding range of about 16 nautical miles from the altitude where the final loss of engine power occurred; however, the glide performance was dependent on several factors, including feathering the propeller and maintaining the proper airspeed, neither of which the pilot did. Although the POH did not contain maximum range glide performance data with a windmilling propeller, based on the available information, it is likely that the airplane could have glided to the alternate airport about 10 miles away if the pilot had followed the proper procedures.
Probable cause:
The pilot's failure to properly trim the airplane's rudder during cruise flight, which resulted in a prolonged uncoordinated flight condition, unporting of the fuel tank feed line, and subsequent fuel starvation and engine power loss. Contributing to the accident was the pilot's failure to feather the engine's propeller and maintain a proper glide airspeed following the loss of engine power.
Final Report:

Crash of a GAF Nomad N.22B in Richardsville

Date & Time: May 4, 1991 at 1715 LT
Type of aircraft:
Operator:
Registration:
N5590M
Flight Phase:
Survivors:
Yes
Schedule:
Bowling Green - Racine
MSN:
083
YOM:
1978
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6400
Captain / Total hours on type:
40.00
Aircraft flight hours:
770
Circumstances:
The pilot had just leveled at 4,000 feet when the right engine lost power. He immediately turned back toward his departure field but could not maintain altitude with the remaining engine. He then elected to make a gear up landing in an open field. On touchdown, the aircraft sustained substantial damage as it came to a stop in the grassy field. The pilot and passenger exited through the forward doors without further incident. Both occupants escaped uninjured.
Probable cause:
The loss of engine power brought on by a failure of the no.2 main engine bearing. Contributing to the accident was the lack of sufficient power on the remaining engine to maintain level flight.
Final Report:

Crash of a Beechcraft A90 King Air off Racine: 5 killed

Date & Time: May 1, 1972 at 0728 LT
Type of aircraft:
Operator:
Registration:
N295X
Survivors:
No
Schedule:
Toledo - Racine
MSN:
LJ-244
YOM:
1967
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
22668
Captain / Total hours on type:
2858.00
Circumstances:
The approach to Racine-Horlick Airport was completed in poor weather conditions. On final, the twin engine airplane struck the water surface and crashed into Lake Michigan. The aircraft was lost and all five occupants were killed. At the time of the accident, the visibility was limited to 1/4 mile with 700 feet overcast, 100-200 feet overcast at airport.
Probable cause:
Improper IFR operation on part of the crew. The following factors were reported:
- Low ceiling and fog,
- Limited visibility.
Final Report:

Crash of a Learjet 23 off Racine: 7 killed

Date & Time: Nov 6, 1969 at 1107 LT
Type of aircraft:
Operator:
Registration:
N1021B
Survivors:
No
Schedule:
Benton Harbor - Racine
MSN:
23-086
YOM:
1966
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
7076
Captain / Total hours on type:
625.00
Circumstances:
On approach to Racine-Batten Airport, the crew failed to realize his altitude was insufficient when the airplane struck the water surface and crashed into Lake Michigan, few miles offshore. The floating wreckage was recovered but all seven occupants were killed.
Probable cause:
Investigations were unable to determined the exact cause of the accident and the reason why the crew was approaching the airport below the minimum safe altitude.
Final Report: