Crash of an Embraer ERJ-190-100AR in Cuenca

Date & Time: Apr 28, 2016 at 0751 LT
Type of aircraft:
Operator:
Registration:
HC-COX
Survivors:
Yes
Schedule:
Quito – Cuenca
MSN:
190-00372
YOM:
2010
Flight number:
EQ173
Country:
Crew on board:
6
Crew fatalities:
Pax on board:
87
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
17523
Captain / Total hours on type:
2113.00
Copilot / Total flying hours:
3545
Copilot / Total hours on type:
2077
Aircraft flight hours:
11569
Aircraft flight cycles:
9707
Circumstances:
Following en uneventful flight from Quito, the crew initiated the descent to Cuenca-Mariscal La Mar Airport Runway 23. Weather conditions at destination were poor with rain falls and a contaminated runway. The pilot-in-command continued the approach below the glide and the aircraft passed over the runway threshold at a height of 37 feet instead the recommended 50 feet. The airplane landed 277 metres past the runway threshold at a speed of 127 knots and the crew activated the spoilers and the reverse thrust systems. Due to poor braking action, the captain activated the autobrake system, without success. As the aircraft could not be stopped within the remaining distance, the captain intentionally turn to the right when the aircraft ground looped, overran and came to rest in a grassy area. All 93 occupants were rescued, among them two passengers were slightly injured. The aircraft was damaged beyond repair.
Probable cause:
The following findings were identified:
- The condition of the runway at Cuenca airport, which at the time of the plane's landing was contaminated with water and slippery.
- The landing was made after a non-stabilized approach with a tailwind.
- During seven seconds, the crew continued the approach with an excessive rate of descent of 1,186 feet, 186 feet above the limit of 1,000 feet.
- The non-application of the Maximum Performance Landing procedure recommended by the aircraft manufacturer for landing on contaminated runways.
- The dispatch of the flight with 1,500 kg of fuel more than the amount of fuel usually used for this flight.
- Omission of the runway length calculation necessary to perform the landing using the braking efficiency information.
- The crew's decision to make the final approach with three red and one white lights, using the PAPI system, induced by the information in the Terminal Information document issued by the company, which authorized this procedure.
- The use of confusing terminology in the Terminal Information document, which used terms applicable to the Airbus fleet, instead of Embraer's.
- The crew's decision not to perform the thwarted approach maneuver after the maximum allowable vertical speed was exceeded and visibility was apparently limited after the minima were exceeded.
- Incorrect use of aircraft braking aids, in this case reverse braking aids
- The application of the emergency brake that inhibits the antiskid system.
- Lack of implementation of adequate management of crew resources, particularly within the cockpit.
- Lack of training in the use of tables for track distance calculation.
- In reference to landing conditions, the aircraft needed a runway length of 2,122 metres while the available distance was 1,900 metres.
Final Report:

Crash of an Embraer ERJ-190AR in Quito

Date & Time: Sep 16, 2011 at 1911 LT
Type of aircraft:
Operator:
Registration:
HC-CEZ
Survivors:
Yes
Schedule:
Loja - Quito
MSN:
190-00027
YOM:
2006
Flight number:
EQ148
Country:
Crew on board:
6
Crew fatalities:
Pax on board:
97
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6160
Captain / Total hours on type:
1879.00
Copilot / Total flying hours:
4891
Copilot / Total hours on type:
2807
Aircraft flight hours:
8752
Aircraft flight cycles:
13285
Circumstances:
Following an uneventful flight from Loja, the crew started the descent to Quito-Mariscal Sucre Airport runway 35 by night and poor weather conditions. After touchdown on wet runway 35, the aircraft encountered difficulties to decelerate properly. Unable to stop within the remaining distance, the airplane overran, went down an embankment, collided with a brick wall and came to rest. There was no fire. All 103 occupants were rescued, among them four passengers were slightly injured. The aircraft named 'Ciudad de Cuenca' was damaged beyond repair.
Probable cause:
The Board of Inquiry estimated that the probable cause of this accident was the crew's decision to continue the approach and landing without carrying out the procedures (ABNORMAL AND EMERGENCY PROCEDURES) established by Embraer in the Quick Reference Handbook when a malfunction occurred with the slat/flap system, resulting in a wrong approach configuration.
The following findings were identified:
- The slats were inoperative during the approach and the crew performed five trouble shooting without success,
- Despite this situation, the crew decided to continue the approach, failed to follow the approach checklist and failed to input the reference speed and distance for landing according to circumstances,
- The aircraft landed too far down the runway, about 880 metres past the runway 35 threshold,
- The braking action was low because the runway surface was wet,
- In normal conditions, with flaps down in second position and slats out, the landing reference speed was 119 knots with a landing distance of 880 metres,
- Because the slats were inoperative, the landing reference speed should be 149 knots and a landing distance of 1,940 metres was needed,
- The aircraft passed over the runway threshold at a height of 50 feet and at an excessive speed of 163,8 knots,
- Spoilers were activated 9 seconds after touchdown, 950 metres after the runway threshold,
- Reverse thrust systems were activated 1,280 metres after the runway threshold,
- The crew started to use brakes 2,300 metres after the runway threshold (runway 35 is 3,125 metres long), with the antiskid system activated,
- Due to an excessive approach speed (15 knots above Vref), a too long flare and a too late application of the brake systems, the aircraft could not be stopped within the remaining distance,
- The slats malfunction was the consequence of the failure of several actuators which did not support negative temperatures met during the last flight,
- Since last July 19, the slats failed 53 times on this aircraft, six times during the approach and 47 times in flight,
- The crew failed to initiate a go-around procedure.

Crash of a Beechcraft 200 Super King Air in Quito: 7 killed

Date & Time: Mar 19, 2009 at 1725 LT
Operator:
Registration:
AEE-101
Flight Type:
Survivors:
No
Site:
Schedule:
San Vicente - Quito
MSN:
BB-811
YOM:
1981
Country:
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
7
Circumstances:
The crew (four pilots under supervision and one instructor) departed San Vicente on a training flight to Quito-Mariscal Sucre Airport. On approach in foggy conditions, the twin engine aircraft descended too low, collided with a 4-floor building and crashed 4 km short of runway. All five occupants as well as two people on the ground were killed and four other people on the ground were seriously injured.

Crash of a Fokker F28 Fellowship 4000 in Quito

Date & Time: Sep 22, 2008 at 1115 LT
Type of aircraft:
Operator:
Registration:
HC-CDT
Flight Phase:
Survivors:
Yes
Schedule:
Quito – Coca
MSN:
11222
YOM:
1985
Flight number:
ICD504
Country:
Crew on board:
4
Crew fatalities:
Pax on board:
62
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
9292
Captain / Total hours on type:
109.00
Copilot / Total flying hours:
3889
Copilot / Total hours on type:
380
Aircraft flight hours:
42422
Aircraft flight cycles:
47727
Circumstances:
During the takeoff roll from runway 25 at Quito-Mariscal Sucre Airport, the crew noted a fire alarm connected to the forward cargo compartment. The captain decided to abandon the takeoff procedure and initiated an emergency braking manoeuvre. Unable to stop within the remaining distance, the aircraft overran, collided with the ILS antenna, went down an embankment then impacted a brick wall and came to rest 300 metres past the runway end. All 66 occupants were rescued, among them eight passengers were injured. The aircraft was damaged beyond repair.
Probable cause:
Failure of the crew to follow the published procedures following a fire alarm, as stated in the Operations Manual and the late application of the procedures once the decision to abort the takeoff was taken.
Contributing factors:
- Complacency on part of the crew who failed to proceed with a pre-takeoff briefing,
- A fact that influenced the lack of appropriate action from the crew to successfully tackle any emergency,
- Lack of crew resources management,
- The braking coefficient was low because the runway surface was wet.
Final Report:

Crash of an Airbus A340-642 in Quito

Date & Time: Nov 9, 2007 at 1706 LT
Type of aircraft:
Operator:
Registration:
EC-JOH
Survivors:
Yes
Schedule:
Madrid - Quito
MSN:
731
YOM:
2006
Flight number:
IB6463
Country:
Crew on board:
14
Crew fatalities:
Pax on board:
345
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
14024
Captain / Total hours on type:
2375.00
Copilot / Total flying hours:
10095
Copilot / Total hours on type:
1742
Aircraft flight hours:
8704
Aircraft flight cycles:
965
Circumstances:
Following an uneventful flight from Madrid, the crew contacted Quito Approach at 1650LT and received descent instructions in preparation for an instrument approach no. 4 (VOR QIT DME/ILS) for runway 35. During the descent the crew were notified that preceding flights had reported braking action medium to poor. The flight crew selected auto braking to 'High'. At 17:05, the crew reported the runway in sight, after which the controller stated that the wind was 170° at 4 knots, the runway was wet and reported braking action was poor. The flight was cleared to land. The pilot in command, following the procedures established by Iberia, decided to leave the ILS glide path and captured the path of the PAPI lights. The aircraft touched down 200 metres past the threshold at a 3.09g side load. The spoilers deployed automatically and main gear tyres 3 and 8 blew. The flap lever was moved involuntarily by the copilot, from the full position to position 2. The crew applied full manual braking and select reverse thrust. The Auto Brake function failed, after which the crew disconnected the antiskid braking system and continued to apply manual braking. The aircraft passed the end of runway 35, with a ground speed of 90 knots, hit the ILS localizer and stopped 232 meters further. Passengers and crew were evacuated using the slide at door 2R, thirty minutes after the aircraft stopped. All occupants escaped uninjured while the aircraft was considered as damaged beyond repair.
Probable cause:
Wrong approach configuration on part of the crew who decided to continue the approach to Quito Airport, knowing the poor runway conditions, poor weather conditions and the aircraft weight, and his failure to initiate a go-around procedure while forcing the aircraft to intercept the PAPI, causing the aircraft to be unstabilized.
Contributing factors:
- On the date of the incident, the crew did not have specific regulations and operating procedures (the briefing of the operator for the airport in Quito was inappropriate to the existent conditions).
- The fact that the crew still being experienced similar airports in Quito and had not experienced similar weather situations, circumstances that would have allowed a strategy of approximation consistent with the terms of this operation, in particular as regards:
- Calculations in flight for landing runway length,
- Minimum altitude to start the maneuver of changing the path of ILS to PAPI,
- Carrying out a very detailed briefing that allowed unwanted deviations on approach,
- The weather conditions existing at the time of landing (visibility, tail wind and moderate rain).

Crash of a Fokker F28 Fellowship 4000 in Coca

Date & Time: Apr 7, 2005 at 0955 LT
Type of aircraft:
Operator:
Registration:
HC-CDA
Survivors:
Yes
Schedule:
Quito – Coca
MSN:
11230
YOM:
1986
Flight number:
ICD504
Location:
Country:
Crew on board:
5
Crew fatalities:
Pax on board:
60
Pax fatalities:
Other fatalities:
Total fatalities:
0
Aircraft flight hours:
36087
Aircraft flight cycles:
46662
Circumstances:
Following an uneventful flight from Quito, the crew started the approach to Coca Airport runway 15. Too low on final, the aircraft landed 4,5 metres short of runway. Upon impact, the left main gear was torn off. The aircraft rolled for 112 metres then veered off runway to the left, rolled another 263 metres then came to rest against a concrete wall. All 65 occupants were rescued, among them seven passengers were injured. The aircraft was damaged beyond repair.
Probable cause:
It was determined that the crew thought the Coca runway was short. To be able to stop the plane on the runway without excessive use of the brakes, the crew decided to land as early as possible. Doing so, the aircraft landed 4,5 metres short of runway. The published procedure request a minimum altitude of 50 feet over the threshold and the AFM showed a landing distance of 930 metres needed at maximum landing weight considering 42° of flaps, speed brakes out, lift dumpers armed, antiskid operative. Wrong approach procedure on part of the crew.

Crash of a Fokker F28 Fellowship 4000 in Quito

Date & Time: Jan 17, 2003 at 0940 LT
Type of aircraft:
Operator:
Registration:
HC-BMD
Flight Phase:
Survivors:
Yes
Schedule:
Quito – Tulcán – Cali
MSN:
11220
YOM:
1984
Flight number:
EQ120
Country:
Crew on board:
5
Crew fatalities:
Pax on board:
72
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7085
Captain / Total hours on type:
4103.00
Copilot / Total flying hours:
1666
Copilot / Total hours on type:
124
Aircraft flight hours:
21547
Aircraft flight cycles:
40084
Circumstances:
During the takeoff roll on runway 35, at a speed of 125 knots, after a course of 2,110 metres, both tyres on the left main gear burst. The crew rejected the takeoff procedure but the aircraft was unable to stop within the remaining distance (runway 35 is 3,120 metres long). It overran, causing the nose gear to collapse, and came to rest 81 metres further. All 77 occupants escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
Lack of a positive actions and reaction on part of the crew following the bursting of both tires on the left main gear, causing the aircraft to overrun the runway.
Final Report:

Crash of a Boeing 727-134 on Mt El Cumbal: 94 killed

Date & Time: Jan 28, 2002 at 1024 LT
Type of aircraft:
Operator:
Registration:
HC-BLF
Flight Phase:
Survivors:
No
Site:
Schedule:
Quito - Tulcán - Cali
MSN:
19692
YOM:
1967
Flight number:
EQ120
Country:
Crew on board:
7
Crew fatalities:
Pax on board:
87
Pax fatalities:
Other fatalities:
Total fatalities:
94
Captain / Total flying hours:
12091
Captain / Total hours on type:
8263.00
Copilot / Total flying hours:
7058
Copilot / Total hours on type:
3457
Aircraft flight hours:
64001
Aircraft flight cycles:
49819
Circumstances:
The aircraft departed Quito-Mariscal Sucre Airport runway 17 at 1001LT on a flight to Cali with an intermediate stop in Tulcán, carrying 87 passengers and 7 crew members. The flight was completed at an altitude of 18,000 feet on airway G-675 towards Ipiales, south Colombia. At a distance of 29 NM from Tulcán, the crew was cleared to descend to 14,000 feet and was briefed about the last weather conditions at destination. For unknown reasons, the crew failed to comply with the company SOP's and started the descent at an excessive speed of 230 knots while the approach procedure called for a speed of 180 knots. Also, the crew was not following the proper approach track for the Tulcán-Teniente Coronel Luis A. Mantilla Airport. In poor visibility due to clouds, at an altitude of 14,700 feet, the aircraft struck the slope of Mt El Cumbal located about 30 km northwest of Ipiales. The aircraft disintegrated on impact and all 94 occupants were killed. The wreckage was found 1,400 feet below the summit.
Probable cause:
The probable cause was:
- The decision of the instructor captain and his crew to initiate and continue the operation towards Tulcán Airport below minima weather conditions as established in the company's SOPs.
- Inadequate navigation and operation of the aircraft by the pilot-in-command and directed by the instructor captain, consisting of entering the holding pattern of the Tulcán radio beacon with a speed of 230 knots (IAS) and with a banking of 15° exceeding the maximum stipulated speed limit of 180 knots during the entire procedure including the holding pattern and using a banking below the recommended range of 25° to 30°, thus exceeding the lateral navigation and obstacle protection limits of the holding pattern, leading this operation to the collision with Mt El Cumbal.
Final Report:

Crash of a Fairchild-Hiller FH-227C on Mt El Tigre: 26 killed

Date & Time: Jan 17, 2002 at 1101 LT
Type of aircraft:
Operator:
Registration:
HC-AYM
Flight Phase:
Survivors:
No
Site:
Schedule:
Quito – Nueva Loja
MSN:
511
YOM:
1966
Country:
Crew on board:
5
Crew fatalities:
Pax on board:
21
Pax fatalities:
Other fatalities:
Total fatalities:
26
Captain / Total flying hours:
17709
Captain / Total hours on type:
8338.00
Copilot / Total flying hours:
12229
Copilot / Total hours on type:
6066
Aircraft flight hours:
29154
Aircraft flight cycles:
45178
Circumstances:
The twin engine aircraft departed Quito-Mariscal Sucre Airport at 1038LT on a charter flight to Nueva Loja-Lago Agrio Airport, carrying 21 oil workers and and five crew members on behalf of the Texaco Oil Company. While cruising under VFR mode at an altitude of 15,500 feet, the crew was instructed by ATC to change heading to 094° in order to descent to Nueva Loja for a landing on runway 23. But the crew failed to comply with this instruction and continued straight ahead. Few minutes later, the crew started the descent in foggy conditions when the aircraft struck the slope of Mt El Tigre located in the south part of Colombia, near the border with Ecuador. The wreckage was found three days later at an altitude of 4,500 metres. The aircraft disintegrated on impact and all 26 occupants were killed.
Probable cause:
The accident was the consequence of a controlled flight into terrain after the crew suffered a loss of situational awareness since their attention was focused on aspects that were not related to the flight being executed and therefore neglecting the primary function of flight which is the control of the aircraft and decision making.
The following contributing factors were identified:
- The crew failed to maintain a sterile cockpit situation,
- The crew was continuously distracted during the flight,
- Lack of technical documentation in the CIA that supports the operation,
- Lack of crew training about Crew Resources Management, human factors and Control Flight Into Terrain(CFIT),
- The weather conditions at the time of the accident on Mt El Tigre made it impossible for the crew to see the mountain,
- The aircraft was not equipped with a Ground Proximity Warning System (GPWS).
Final Report:

Crash of a Boeing 727-230 in Bogotá: 53 killed

Date & Time: Apr 20, 1998 at 1645 LT
Type of aircraft:
Operator:
Registration:
HC-BSU
Flight Phase:
Survivors:
No
Site:
Schedule:
Bogotá - Quito
MSN:
21622
YOM:
1978
Flight number:
AF422
Country:
Crew on board:
10
Crew fatalities:
Pax on board:
43
Pax fatalities:
Other fatalities:
Total fatalities:
53
Captain / Total flying hours:
5062
Captain / Total hours on type:
2296.00
Copilot / Total flying hours:
7872
Copilot / Total hours on type:
528
Aircraft flight hours:
34586
Aircraft flight cycles:
26475
Circumstances:
The flight from Bogotá to Quito was completed by TAME on a wet-lease contract for Air France, second leg from the AF422 flight from Paris to Quito via Bogotá operated by an Airbus A340. After takeoff from runway 13 at Bogotá-El Dorado Airport, the crew was cleared for a Girardot 1 departure that consist of continuing on runway heading for 2 miles after takeoff, followed by a 90° right turn over the Romeo beacon. For unknown reasons, the crew continued straight forward until the aircraft impacted the Mt El Cable located ahead of the airport. The aircraft disintegrated on impact and all 53 occupants were killed, among them 25 European Nationals, seven Italians, six French, three Danish, three Spanish, two Germans, two Austrians, one British and one Swiss. The wreckage was found 50 metres below the summit. At the time of the accident, weather conditions were poor with rain, clouds at 2,300 feet and CB's.
Probable cause:
The crew suffered a loss of situational awareness after takeoff while climbing in IMC conditions. The crew failed to comply with the Girardot 1 departure procedure, deviated from the published departure procedures and maintain runway heading until the aircraft collided with terrain.
Final Report: