Crash of a Cessna 207 Skywagon near Juneau: 3 killed

Date & Time: Oct 3, 1979 at 1213 LT
Registration:
N1726U
Flight Phase:
Survivors:
No
Schedule:
Juneau – Hoonah
MSN:
207-0326
YOM:
1976
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
2623
Captain / Total hours on type:
21.00
Circumstances:
The single engine airplane departed Juneau Airport on a taxi flight to Hoonah, carrying two passengers and one pilot. While climbing in poor weather conditions, the pilot suffered spatial disorientation and lost control of the airplane that crashed in flames in an open field. The aircraft was totally destroyed and all three occupants were killed. At the time of the accident, weather conditions were poor with thunderstorm activity, low ceiling, rain and turbulences.
Probable cause:
Uncontrolled descent and subsequent collision with ground after the pilot continued VFR flight into adverse weather conditions. The following contributing factors were reported:
- Spatial disorientation,
- Inadequate preflight preparation,
- Physical impairment,
- Alcoholic impairment of efficiency and judgment,
- Low ceiling,
- Rain,
- Turbulences associated with thunderstorm activity,
- Squall line,
- Merging cloud layers forecasted,
- Blood alcohol level 1,08‰.
Final Report:

Crash of a Learjet 25 in Anchorage: 5 killed

Date & Time: Dec 4, 1978 at 1450 LT
Type of aircraft:
Operator:
Registration:
N77RS
Survivors:
Yes
Schedule:
Juneau - Anchorage
MSN:
25-094
YOM:
1973
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
7000
Captain / Total hours on type:
650.00
Copilot / Total flying hours:
2635
Copilot / Total hours on type:
21
Aircraft flight hours:
1549
Circumstances:
Following an uneventful flight from Juneau, the crew completed the final approach and was attempting to land on runway 06R when the airplane rolled sharply and struck the ground. out of control, it crashed inverted in a snow covered area near the runway. Two passengers were seriously injured while five other occupants were killed.
Probable cause:
It was determined that the probable cause of the accident was an encounter with strong, gusting crosswinds during the landing attempt, which caused the aircraft to roll abruptly and unexpectedly. The ensuing loss of control resulted from inappropriate pilot techniques during the attempt to regain control of the aircraft. Suspected light ice accumulations on the aerodynamic surfaces may have contributed to a stall and loss of control.
Final Report:

Crash of a Grumman G-44 Widgeon near Cordova: 3 killed

Date & Time: Oct 31, 1978
Type of aircraft:
Operator:
Registration:
N444W
Flight Phase:
Survivors:
No
Schedule:
Cordova - Juneau
MSN:
1450
YOM:
1944
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
While cruising unde VFR mode in poor weather conditions, the pilot lost control of the seaplane that entered a dive and crashed in flames in an isolated area located in the region of Cordova. SAR operations were initiated but eventually suspended as no trace of the aircraft nor the three occupants was found. The wreckage was eventually localized on May 21, 1979.
Probable cause:
Uncontrolled descent and ground collision after the pilot initiated flight in adverse weather conditions. The following contributing factors were reported:
- Continued VFR flight in adverse weather conditions,
- Low ceiling,
- Fog,
- Snow,
- Icing conditions.
Final Report:

Crash of a Cessna 411 off Yakutat: 7 killed

Date & Time: Aug 27, 1977
Type of aircraft:
Registration:
N4930T
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Juneau - Anchorage
MSN:
411-0130
YOM:
1965
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
2150
Captain / Total hours on type:
100.00
Circumstances:
En route from Juneau to Anchorage, while cruising in marginal weather conditions, the pilot reported engine problems when contact was lost. The airplane entered a spin and crashed into the ocean off Yakutat. Few debris and two dead bodies were found. The aircraft sank and was lost.
Probable cause:
Due to lack of evidences, the exact cause of the accident could not be determined. The following findings were reported:
- Powerplant failure for undetermined reasons,
- Icing conditions including sleet and freezing rain,
- Partial loss of power on one engine,
- Complete failure of one engine,
- Weather slightly worse than forecast,
- Ceiling 1,200 feet,
- Pilot reported securing engine n°2,
- Passengers recovered from bay,
- Aircraft damage and injury index presumed.
Final Report:

Crash of a Boeing 727-81 in Ketchikan: 1 killed

Date & Time: Apr 5, 1976 at 0819 LT
Type of aircraft:
Operator:
Registration:
N124AS
Survivors:
Yes
Schedule:
Anchorage - Juneau - Ketchikan - Seattle
MSN:
18821/124
YOM:
1965
Flight number:
AS060
Crew on board:
7
Crew fatalities:
Pax on board:
43
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
19813
Captain / Total hours on type:
2140.00
Copilot / Total flying hours:
3193
Copilot / Total hours on type:
1980
Aircraft flight hours:
25360
Circumstances:
About 0738LT on April 5, 1976, Alaska Airlines, Inc., Flight 60, a B-727-81, N124AS, departed Juneau, Alaska, on a regularly scheduled passenger flight to Seattle, Washington; an en route stop was scheduled for Ketchikan International Airport, Ketchikan, Alaska. There were 43 passengers and a crew of 7 on board. Anchorage air route traffic control center (ARTCC) cleared Flight 60 on an instrument flight rules (IFR) flight plan to the Ketchikan International Airport; the flight was routine en route. At 0805, Anchorage ARTCC cleared Flight 60 for an approach to runway 11 at Ketchikan. At 0807, the flight was 30 DME miles from the airport. At 0811, Flight 60 reported out of 10,000 feet and was cleared to contact Ketchikan Flight Service Station (FSS); the FSS advised the flight that the 0805 weather was: ceiling 800 ft., obscured, visibility 2 mi, light snow, fog, wind 330° at 5 kt. The FSS also advised the flight that braking action on runway 11 was poor; this report was based on braking tests performed by the airport manager. The captain testified that he did not recall hearing the braking condition report. Upon receipt of the clearance, the crew of Flight 60 began an ILS approach to Ketchikan. Near the 17-mile DME fix, as the flight descended through 4,000 feet, the crew acquired visual contact with the ground and water. As the flight approached Guard Island, the captain had the Island in sight and decided to abandon the ILS approach and to continue the approach visually. The captain testified that he established a 'visual glide slope of my own' at an altitude of about 1,000 feet, and stated that his eyes were '... the most reliable thing I have.' Visual contact with the approach lights was established about 2 miles from the runway threshold. The airport was visible shortly thereafter. The captain did not recall the airspeed at touchdown, but estimated that he touched down about 1,500 feet past the threshold of runway 11. He also testified that he did not see the yellow, 1,000-foot markers on the runway; he further testified that the runway '... was just wet.' A passenger on Flight 60, who was seated in seat 5A (just forward of the wing's leading edge), stated that the yellow runway marks were visible to him. The first officer has no recollection of the sequence of events leading to the accident; however, the second officer testified that airspeeds and descent rates were called out during the last 1,000 feet. The captain could not recall the flap setting either on approach or at touchdown. However, the second officer testified that after the landing gear was extended the first officer remarked, 'We're high,' and lowered the flaps from 30° to 40°. None of the cockpit crew remembered the airspeeds, descent rates, or altitudes of the aircraft during the approach and touchdown. Reference speed was calculated to be 117 kns with 40° flaps and 121 kns with 30° flaps. The captain testified that after touchdown he deployed the ground spoilers, reversed the engines, and applied the wheel brakes. Upon discovering that the braking action was poor, he decided to execute a go-around. He retracted the ground spoilers, called for 25° flaps, and attempted to obtain takeoff thrust. The thrust reverser mechanism did not disengage fully and the forward thrust could not be obtained. He then applied full reversing and quickly moved the thrust levers to 'idle.' This attempt to obtain forward thrust also was not successful. The captain then reapplied reverse thrust and again deployed the ground spoilers in an attempt to slow the aircraft. When he realized that the aircraft could not be stopped on the runway, he turned the aircraft to the right, raised the nose, and passed over a gully and a service road beyond the departure end of the runway. The aircraft came to rest in a ravine, 700 feet past the departure end of runway 11 and 125 feet to the right of the runway centerline. Flight attendants reported nothing unusual about the approach and touchdown, except for the relatively short time between the illumination of the no-smoking sign and the touchdown. The two flight attendants assigned to the rear jumpseats and the attendant assigned to the forward jumpseat did not have sufficient time to reach their assigned seats and had to sit in passenger seats. None of the flight attendants felt the aircraft decelerate or heard normal reverse thrust. Many passengers anticipated the accident because of the high speed of the aircraft after touchdown and the lack of deceleration. Two ground witnesses, who are also pilots, saw the aircraft when it was at an altitude of 500 to 700 feet and in level flight. The witnesses were located about 7,000 feet northwest of the threshold of runway 11. They stated that the landing gear was up and that the aircraft seemed to be 'fast' for that portion of the approach. When the aircraft disappeared behind an obstruction, these witnesses moved to another location to continue watching the aircraft. They saw the nose gear in transit and stated that it appeared to be completely down as the aircraft crossed over the first two approach lights. The first two approach lights are located about 3,000 feet from the runway threshold. A witness, who was located on the fifth floor of the airport terminal, saw the aircraft when it was about 25 feet over the runway. The witness stated that the aircraft was in a level attitude, but that it appeared 'very fast.' He stated that the aircraft touched down about one-quarter way down the runway, that it bounced slightly, and that it landed again on the nose gear only. It then began a porpoising motion which continued until the aircraft was past midfield. Most witnesses placed the touchdown between one-quarter and one-half way down the runway and reported that the aircraft seemed faster-than-normal during the landing roll. Witnesses reported varying degrees of reverse thrust, but most reported only a short burst of reverse thrust as the aircraft passed the airport terminal, about 3,800 feet past the threshold of runway 11.
Probable cause:
The captain's faulty judgement in initiating a go-around after he was committed to a full stop landing following an excessively long and fast touchdown from an unstabilized approach. Contributing to the accident was the pilot's unprofessional decision to abandon the precision approach. The following findings were reported:
- There is no evidence of aircraft structure or component failure or malfunction before the aircraft crashed.
- The flight crew was aware of the airport and weather conditions at Ketchikan.
- The weather conditions and runway conditions dictated that a precision approach should have been flown.
- The approach was not made according to prescribed procedures and was not stabilized. The aircraft was not in the proper position at decision height to assure a safe landing because of excessive airspeed, excessive altitude, and improperly configured flaps and landing gear.
- The aircraft's altitude was higher-than-normal when it crossed the threshold of runway 11 and its airspeed was excessively high.
- The captain did not use good judgment when he initiated a go-around after he was committed to full-stop landing following the touchdown.
- There is no evidence that the first and second officers apprised the captain of his departure from prescribed procedures and safe practices, or that they acted in any way to assure a more professional performance, except for the comment by the first officer, when near the threshold, that they were high after which he lowered the flaps to 40°.
- After applying reverse thrust shortly after touchdown, the captain was unable to regain forward thrust because the high speed of the aircraft produced higher-than-normal airloads on the thrust deflector doors.
- Braking action on runway 11 was adequate for stopping the aircraft before it reached the departure end of the runway.
- Before the accident the FAA had not determined adequately the airport's firefighting capabilities.
- Postaccident hearing tests conducted on the captain indicated a medically disqualifying hearing loss; however, the evidence was inadequate to conclude that this condition had any bearing on the accident.
Final Report:

Crash of a De Havilland DHC-3 Otter in the Hawk Inlet

Date & Time: Jul 31, 1975 at 0930 LT
Type of aircraft:
Registration:
N3382
Flight Type:
Survivors:
Yes
Schedule:
Juneau - Hawk Inlet
MSN:
288
YOM:
1958
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7000
Captain / Total hours on type:
101.00
Circumstances:
The pilot, sole on board, was completing a cargo flight from Juneau to Hawk Inlet. While landing in the Hawk Inlet, the single engine airplane overturned, came to rest upside down and sank. The pilot escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
Nosed over upon landing after the pilot failed to retract the landing gear. The following contributing factors were reported:
- Failed to use the checklist.
Final Report:

Crash of a De Havilland DHC-2 Beaver in Alaska: 5 killed

Date & Time: Jan 13, 1975 at 1700 LT
Type of aircraft:
Registration:
N1944
Flight Phase:
Survivors:
No
Site:
Schedule:
Tenakee - Juneau
MSN:
1692
YOM:
1969
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
9900
Captain / Total hours on type:
840.00
Circumstances:
Crashed in unknown circumstances somewhere in South Alaska while completing a flight from Tenakee to Juneau. No trace of the aircraft nor the five occupants was ever found.
Probable cause:
Due to lack of evidences, the cause of the accident could not be determined.
Final Report:

Crash of a De Havilland DHC-2 Beaver in Hoonah: 4 killed

Date & Time: Nov 15, 1974 at 1300 LT
Type of aircraft:
Registration:
N9770Z
Flight Phase:
Survivors:
No
Schedule:
Juneau - Tenakee
MSN:
376
YOM:
1952
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
2864
Captain / Total hours on type:
300.00
Circumstances:
En route from Juneau to Tenakee, the pilot encountered bad weather conditions with low clouds and heavy snow falls. While cruising at low height under VFR mode, the seaplane crashed into the bay off Hoonah and sank. All four occupants were killed.
Probable cause:
Improper in-flight decisions as the pilot continued VFR flight into adverse weather conditions. The following contributing factors were reported:
- Low ceiling and snow.
Final Report:

Crash of a Boeing 727-193 near Juneau: 111 killed

Date & Time: Sep 4, 1971 at 1215 LT
Type of aircraft:
Operator:
Registration:
N2969G
Survivors:
No
Site:
Schedule:
Anchorage – Cordova – Yakutat – Juneau – Sitka – Seattle
MSN:
19304/287
YOM:
1966
Flight number:
AS1866
Location:
Crew on board:
7
Crew fatalities:
Pax on board:
104
Pax fatalities:
Other fatalities:
Total fatalities:
111
Captain / Total flying hours:
13870
Captain / Total hours on type:
2688.00
Copilot / Total flying hours:
5000
Copilot / Total hours on type:
2100
Aircraft flight hours:
11344
Circumstances:
Alaska Airlines, Flight 1866 (AS66) was a scheduled passenger flight from Anchorage (ANC), to Seattle (SEA), with intermediate stops at Cordova (CDV), Yakutat (YAK), Juneau (JNU), and Sitka (SIT). The IFR flight departed Anchorage at 09:13 and landed at Cordova at 09:42. AS66 departed Cordova at 10:34 after a delay, part of which was attributable to difficulty in securing a cargo compartment door. The flight landed at Yakutat at 11:07. While on the ground, AS66 received an air traffic control clearance to the Juneau Airport via Jet Route 507 to the Pleasant Intersection, direct to Juneau, to maintain 9,000 feet or below until 15 miles southeast of Yakutat on course, then to climb to and maintain FL230. The flight departed Yakutat at 11:35, with 104 passengers and seven crew members on board. At 11:46, AS66 contacted the Anchorage ARTCC and reported level at FL230, 65 miles east of Yakutat. The flight was then cleared to descend at the pilot's discretion to maintain 10,000 ft so as to cross the Pleasant Intersection at 10,000 feet and was issued a clearance limit to the Howard Intersection. The clearance was acknowledged correctly by the captain and the controller provided the Juneau altimeter setting of 29.46 inches and requested AS66 to report leaving 11,000 ft. At 11:51, AS66 reported leaving FL230. Following this report, the flight's clearance limit was changed to the Pleasant Intersection. At 11:54, the controller instructed AS66 to maintain 12,000 feet. Approximately 1 minute later, the flight reported level at 12,000 feet. The changes to the flight's original clearance to the Howard Intersection were explained to AS66 by the controller as follows: "I've got an airplane that's not following his clearance, I've got to find out where he is." The controller was referring to N799Y, a Piper Apache which had departed Juneau at 11:44 on an IFR clearance, destination Whitehorse, Canada. On two separate occasions, AS66 acted as communications relay between the controller and N799Y. At 11:58, AS66 reported that they were at the Pleasant Intersection, entering the holding pattern, whereupon the controller recleared the flight to Howard Intersection via the Juneau localizer. In response to the controller's query as to whether the flight was "on top" at 12,000 feet, the captain stated that the flight was "on instruments." At 12:00, the controller repeated the flight's clearance to hold at Howard Intersection and issued an expected approach time of 12:10. At 12:01, AS66 reported that they were at Howard, holding 12,000 feet. Six minutes later, AS66 was queried with respect to the flight's direction of holding and its position in the holding pattern. When the controller was advised that the flight had just completed its inbound turn and was on the localizer, inbound to Howard, he cleared AS66 for a straight-in LDA approach, to cross Howard at or below 9,000 feet inbound. The captain acknowledged the clearance and reported leaving 12,000 feet. At 12:08 the captain reported "leaving five thousand five ... four thousand five hundred," whereupon the controller instructed AS66 to contact Juneau Tower. Contact with the tower was established shortly thereafter when the captain reported, "Alaska sixty-six Barlow inbound." (Barlow Intersection is located about 10 nautical miles west of the Juneau Airport). The Juneau Tower Controller responded, "Alaska 66, understand, ah, I didn't, ah, copy the intersection, landing runway 08, the wind 080° at 22 occasional gusts to 28, the altimeter now 29.47, time is 09 1/2, call us by Barlow". No further communication was heard from the flight. The Boeing 727 impacted the easterly slope of a canyon in the Chilkat Range of the Tongass National Forest at the 2475-foot level. The aircraft disintegrated on impact. The accident was no survivable.
Probable cause:
A display of misleading navigational information concerning the flight's progress along the localizer course which resulted in a premature descent below obstacle clearance altitude. The origin or nature of the misleading navigational information could not be determined. The Board further concludes that the crew did not use all available navigational aids to check the flight's progress along the localizer nor were these aids required to be used. The crew also did not perform the required audio identification of the pertinent navigational facilities.
Final Report:

Crash of a Grumman G-21A Goose near Juneau: 9 killed

Date & Time: Aug 21, 1966 at 1035 LT
Type of aircraft:
Operator:
Registration:
N88820
Flight Phase:
Survivors:
No
Site:
MSN:
1114
YOM:
1941
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total flying hours:
9230
Captain / Total hours on type:
2492.00
Circumstances:
En route, the seaplane went into an uncontrolled descent and crashed in flames in a glacier located in the region of Juneau. The wreckage was found few hours later in a crevasse and all nine occupants have been killed.
Probable cause:
The exact cause of the accident could not be determined as hazardous location precluded on scene investigation.
Final Report: