Crash of a Rockwell Aero Commander 500B near Armstrong

Date & Time: Nov 30, 2007 at 0917 LT
Operator:
Registration:
C-GETK
Flight Phase:
Survivors:
Yes
Schedule:
Dryden – Geraldton
MSN:
500-1093-56
YOM:
1961
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft departed from Dryden, Ontario, en route to Geraldton, Ontario. The flight was conducted under visual flight rules at 5500 feet above sea level with ambient temperatures aloft of -33°C. Approximately 40 minutes into the flight, the crew observed an abnormal right engine fuel flow indication. While troubleshooting the right engine, the engine rpm and fuel flow began to decrease and the crew diverted toward Armstrong, Ontario. A short time later, the left engine rpm and fuel flow began to decrease and the crew could no longer maintain level flight. At 0917 central standard time, the crew made a forced landing 20 nautical miles southwest of Armstrong, into a marshy wooded area. The captain sustained serious injuries and the co-pilot and passenger sustained minor injuries. The aircraft was substantially damaged. The crew and passenger were stabilized and transported to Thunder Bay, Ontario, for medical assistance.
Probable cause:
Findings as to Causes and Contributing Factors:
1. Suspended water in the fuel system precipitated out of solution and froze in the fuel distributor valve. This blocked the fuel supply to the fuel nozzles and led to the loss of engine power.
2. The aircraft was being operated without a fuel additive icing inhibiter. Use of such an additive would have inhibited ice formation in the aircraft’s fuel system and would likely have prevented the fuel system blockage.
Findings as to Risk:
1. The fuel distributor valve on the Aero Commander 500B is exposed directly to the cooling blast of the outside air, which under extremely cold conditions, can lead to the freezing of super-cooled water droplets present in the fuel stream.
2. The operator did not have procedures to describe how fuel additive icing inhibiter should be used during winter operations.
Final Report:

Crash of a De Havilland DHC-2 Beaver near Pickle Lake

Date & Time: Oct 2, 1999 at 1430 LT
Type of aircraft:
Operator:
Registration:
C-GZBQ
Flight Phase:
Survivors:
Yes
Schedule:
Big Trout Lake - Geraldton
MSN:
919
YOM:
1956
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1420
Captain / Total hours on type:
725.00
Aircraft flight hours:
13372
Circumstances:
The de Havilland DHC-2 Beaver seaplane departed from Big Trout Lake, Ontario, on a visual flight rules flight for Geraldton, Ontario, with a pilot and an aircraft maintenance engineer on board. After encountering adverse weather conditions en route to Geraldton, the pilot decided to divert to Pickle Lake, Ontario. At about 1430 central daylight time, the engine lost power at an altitude of about 300 feet above ground level while in the descent for Pickle Lake. The pilot turned the aircraft toward a nearby narrow river. In an attempt to restart the engine, the pilot confirmed that the fuel pressure was normal, the fuel selector was on the fullest tank (front), the throttle was at idle, the mixture was rich, and the ignition switch was on both, then he operated the wobble pump. When the engine did not restart, he switched to the centre fuel tank and operated the wobble pump again, but the engine still did not restart. He then switched back to the front tank and tried another restart, without success. He then landed the aircraft on the river at an estimated landing speed of about 40 to 45 mph. After the forced landing, the left wingtip collided with trees on the river bank, and the aircraft yawed to the left about 180 degrees and struck the river bank, breaking off the floats and the float struts. Impact with more trees on the river bank damaged the right wing and elevator. Both occupants were wearing lap belts with shoulder harnesses and were uninjured. The aircraft was substantially damaged. The pilot advised Thunder Bay flight service station by radio of the engine failure and crash and the crew were rescued two hours later.
Probable cause:
Findings as to Causes and Contributing Factors:
- The engine quit operating because the aircraft fuel system was contaminated with a large amount of water.
- The most likely source of the water contamination was the drums from which the aircraft was refuelled.
- A proper filter to prevent water contamination was not used when the aircraft was refuelled.
- The nose-level aircraft attitude when beached and the freezing of water probably prevented the water contamination from being drained from the front tank during the pilot's pre-flight checks.
Other Findings:
- The aircraft's maintenance records indicate that the aircraft was certified, equipped, and maintained in accordance with existing regulations and approved procedures.
- The use of the available shoulder harnesses probably prevented serious injury to the pilot and engineer.
Final Report:

Crash of a Piper PA-31-310 Navajo in Carnarvon

Date & Time: Aug 18, 1989 at 1856 LT
Type of aircraft:
Operator:
Registration:
VH-DEG
Flight Type:
Survivors:
Yes
Schedule:
Geraldton – Carnarvon
MSN:
31-7812098
YOM:
1978
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
At approximately 1809, (23 minutes before last light) during final approach to landing at Carnarvon, the pilot noticed that the landing gear had not extended correctly. The aircraft remained in the circuit area whilst the pilot attempted to lower the landing gear using both manual and emergency methods. He also sought assistance from the company's, Perth based, duty pilot and Carnarvon based engineers. After exhausting all possible methods of lowering the gear the pilot decided to land with the landing gear and flaps retracted. The pilot rejected a landing on the sealed runways because he was apprehensive that it would cause unnecessary damage to the aircraft and could result in a fire. He considered landing in a riverbed (rejected by the Senior Operational Controller), alongside one of the sealed runways (the surface was unsuitable) and on one of the dirt strips. The pilot was offered a flare path on dirt runway 27 however, he declined and indicated that he would try to land using the available light. At 1856 (last light was at 1832) the pilot attempted a landing on runway 27. On late final approach the aircraft collided with a one and a half metre high levy bank, 270 metres short and 115 metres to the right of the threshold. The pilot was trapped in the wreckage for some time after the aircraft came to a stop. While the passenger was slightly injured, the pilot was seriously wounded.
Probable cause:
The landing gear problem arose when the left main landing gear would not lower. Examination of the aircraft revealed that both hinges fitted to the inboard landing gear door had fractured. The forward hinge had fractured as a result of fatigue and the rear hinge as a result of overload. The fatigue crack initiation had occurred at a sharp edged, prominent forging flash on the inner radius of the hinge and had grown over approximately 4000 load cycles. A similar fatigue problem had been identified on an earlier version of the hinge (part number 46653-00), however, regular inspections for fatigue cracking were discontinued when hinges with part number 47529-32 (as fitted to VH-DEG) were introduced in 1980. Similar fatigue cracking was found in the forward door hinge of another PA31 during the investigation. The fractured hinges jammed the left main landing gear mechanism and neither the normal or emergency extension systems could extend the gear. The pilot was apprehensive about wheels up landings. Much of his decision making was aimed at reducing the risk of fire and minimising the damage the aircraft would sustain during the landing. eg. Selection of a dirt runway instead of the sealed strip, landing with flaps retracted etc. During the pilot's attempts to rectify the landing gear problem, and up until the time of his touchdown, he was subjected to considerable radio transmission traffic involving questions, directions and suggestions which distracted him from his primary tasks. The pilot indicated on at least two occasions that he was ready to land, however, each time advice and questions from the ground personnel involved overrode his intentions. When the pilot was asked if he wanted a flare path on runway 27 there was still some natural light available and he was intending to land. However, by the time he was able to make his final approach it was dark and he was unable to see the ground. Studies have shown that aircrew subjected to high levels of stress can suffer skill fatigue and cognitive task saturation, which in turn can lead to a breakdown in the decision making process. It was apparent from the pilot's radio transmissions and the quality of the decisions made in the latter part of the flight that his information processing and decision making abilities had been degraded by the stress of continuous radio transmissions and continuous, and sometimes conflicting, instructions. As a result, what should have been a relatively simple wheels up landing in daylight was turned into an extremely difficult wheels up landing at night. With the landing gear retracted the aircraft's taxi and landing lights were not available to the pilot.
The following factors were considered relevant to the development of the accident:
1. Manufacturing defect. A forging flash created a stress concentration which led to fatigue cracking.
2. Inadequate inspection procedures. Previous inspection procedures introduced to disclose similar cracking were withdrawn on the introduction of later part numbered hinges.
3. Apprehension of the pilot. The pilot was apprehensive about apparently significant dangers of landing an aircraft, wheels up, on a sealed runway.
4. Inordinate interference in aircraft operations by ground based advisors. The ground advisors input overrode the pilot's decision on a number of occasions with the result that a simple exercise became very complicated.
5. Cognitive task saturation and skill fatigue. The amount of information, advice and suggestions being passed via the radio communications system overloaded the pilot decision making abilities.
6. Improper in-flight decisions. As a result of task saturation the final decision made by the pilot to attempt a night landing on an unlighted strip was incorrect.
7. The pilot did not see and therefore was unable to avoid the levy bank.
Final Report:

Crash of a De Havilland DH.86A Express in Geraldton: 2 killed

Date & Time: Jun 24, 1945 at 1030 LT
Type of aircraft:
Operator:
Registration:
VH-USF
Flight Phase:
Survivors:
Yes
Schedule:
Perth – Geraldton – Carnarvon – Port Hedland
MSN:
2310
YOM:
0
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
10000
Captain / Total hours on type:
900.00
Circumstances:
This was its inaugural MMA service, from Perth to Geraldton and Carnarvon. After refueling at Geraldton, the takeoff appeared normal but the aircraft did not climb and turned back for a landing. It flew low over RAAF hangars at about 300 feet then made a steep turn to port, followed by a wide low circuit back to the runway with port wing low. When just inside the aerodrome boundary, it dropped heavily on the starboard main undercarriage, bounced, contacted the ground with the tail wheel and bounced again. Striking the ground for the third time, this time on the port main wheel, as it bounced higher, engine power was applied but the aircraft swung to the left, banking steeply until the left wings were torn off by ground contact. The aircraft cartwheeled and hit the ground nose-first. The fuselage broke up, spilling out most of the 11 occupants. Captain Branch and one passenger were killed, the other 9 occupants seriously injured.
Crew:
H. J. Branch, pilot,
Don W. Rumney, copilot.
Source:
http://www.goodall.com.au/australian-aviation/dh86/dh86.html
Probable cause:
The DCA accident investigation report placed the blame squarely on Captain Branch: “The accident was caused by an indifferent landing which had worsened until the aircraft became completely out of control.” However the investigation panel was criticized for not including, or failing to take evidence from, any DCA officer involved in previous Australian DH.86 accidents. Their report acknowledged that the type was prone to swung during takeoff or landing and that such swings were usually difficult to control, and listed 9 accidents to Australian DH.86s involving such swings. But the report did not address the extreme port wing drop soon after airborne or the reason for returning, or the very wide circuit so close to the ground. It seemed that events prior to touchdown were deemed irrelevant.

Crash of a Consolidated PBY-5 Catalina off Geraldton

Date & Time: Apr 18, 1942
Type of aircraft:
Operator:
Registration:
2409
Flight Type:
Survivors:
Yes
MSN:
225
YOM:
1941
Country:
Region:
Crew on board:
7
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The seaplane landed hard off Geraldton, took water and was later brought to the shore where it struck rocks and was damaged beyond repair. At the time of the accident, the aircraft was heavy loaded (some 30,000 pounds). All seven crew members were unhurt.
Probable cause:
Heavy landing.

Crash of a De Havilland DH.50A in Geraldton

Date & Time: May 11, 1929
Type of aircraft:
Operator:
Registration:
G-AUFD
Flight Phase:
Survivors:
Yes
Schedule:
Geraldton – Perth
MSN:
1
YOM:
1928
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed shortly after takeoff from Geraldton Airport. There were no casualties.

Crash of a Bristol Tourer 28 in Kalbarri: 2 killed

Date & Time: Dec 5, 1921
Type of aircraft:
Operator:
Registration:
G-AUDI
Survivors:
No
Schedule:
Geraldton – Kalbarri – Carnarvon – Karratha – Port Hedland – Broome – Derby
MSN:
6116
YOM:
1921
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The crew was performing the inaugural flight from Geraldton to Derby which was considered as the first commercial flight within Australia. On approach to Kalbarri, the aircraft crashed for unknown reasons near the Murchinson River, killing both occupants.
Crew:
Ted Broad,
Bob Fawcett.