Crash of a Rockwell Turbo Commander 680V in Fort Lauderdale: 2 killed

Date & Time: Nov 3, 1990 at 1025 LT
Registration:
N541F
Flight Type:
Survivors:
No
Schedule:
Fort Lauderdale - Fort Lauderdale
MSN:
680-1609-45
YOM:
1967
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1100
Aircraft flight hours:
6288
Circumstances:
The airplane had not flown since June 1989. The flight had made 2 high speed taxi operations before takeoff. Immediately after takeoff the flight called to land. The airplane was observed on downwind 200-800 feet agl, 15-25° nose high. The airplane then stalled. The compressor surge valves for the left and right engines were found in the open position. Both occupants were killed.
Probable cause:
The pilot-in-command's decision to continue takeoff with a known deficiency in the airplane - low power on both engines which resulted from open compressor surge valves. The pilot subsequently failed to maintain airspeed while maneuvering in a turn resulting in an inflight loss of control and a stall/spin.
Final Report:

Crash of a Piper PA-31-310 Navajo off New Town: 1 killed

Date & Time: Jun 20, 1990 at 0451 LT
Type of aircraft:
Operator:
Registration:
YV-2200P
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Fort Lauderdale - Caracas
MSN:
31-7400006
YOM:
1974
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
On June 20, 1990, at 04:51 Atlantic standard time (AST), a Piper PA-31, YV2200P, registered to and operated by Juan A. Zeley, crashed near New Town, Andros Island, Bahamas, while on a business flight from Fort Lauderdale, Florida, to Caracas, Venezuela. Visual meteorological conditions prevailed at the time and an instrument flight rules flight plan was filed. The Venezuelan registered airplane was destroyed. The pilot, the sole occupant of the airplane, who held a Venezuelan commercial pilot certificate was fatally injured. The flight originated at Fort Lauderdale Executive Airport, Fort, Lauderdale, Florida, on June 20, 1990 at 04:05 AST.

Crash of a Cessna 404 Titan II in Boca Raton

Date & Time: Jan 17, 1990 at 0009 LT
Type of aircraft:
Operator:
Registration:
N335GP
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
Schedule:
Wilmington - Fort Lauderdale
MSN:
404-0009
YOM:
1976
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1487
Captain / Total hours on type:
35.00
Aircraft flight hours:
3286
Circumstances:
While level after descending, the right engine quit. Pilot feathered the propeller, advised ATC, and was diverting to alternate when left engine quit. He positioned the left engine boost pump to high and low with negative results, but did not feather the propeller. Position of boost pumps, when engines quit, was not determined. Aircraft landed on overpass that was under construction. There was fuel leakage after accident due to aircraft damage. Fuel quantity was sufficient. Examination of aircraft revealed right engine flexible duct from turbocharger to plenum chamber separated due to loose clamp. Hose was installed and club prop installed for each engine run. Both engines operated normally. Induction air hose was pulled during right engine run. Engine ran rough due to excessive rich mixture. No determination could be made for the reason of the left engine power loss.
Probable cause:
Loss of power in the right engine due to a disconnected duct between the turbocharger and the plenum chamber. The reason for the loss of power in the left engine was not determined.
Final Report:

Crash of a Mitsubishi MU-2B-60 Marquise near Coral Springs: 1 killed

Date & Time: Jun 18, 1987 at 1730 LT
Type of aircraft:
Registration:
N184MA
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Fort Lauderdale - Fort Lauderdale
MSN:
218
YOM:
1972
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
8400
Circumstances:
The pilot reported to ground personnel at Fort Lauderdale that he was experiencing an avionics problem and the passenger entry door was sprung the day before when it was slammed; however, the pilot elected to depart. The aircraft wreckage was located on June 19 in the Everglades near Coral Springs, Florida. The aircraft impacted in a nose low attitude. Wreckage was scattered over an area 211 feet long by 55 feet wide. Investigation revealed no preimpact mechanical malfunctions/failures. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: loss of control - in flight
Phase of operation: unknown
Findings
1. (c) flight controls - improper use of - pilot in command
2. Operation with known deficiencies in equipment - performed - pilot in command
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain off Staniel Cay: 3 killed

Date & Time: Mar 28, 1985
Registration:
N3517W
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Staniel Cay – Fort Lauderdale
MSN:
31-7952096
YOM:
1979
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
After takeoff from Staniel Cay Airport, while climbing, the twin engine aircraft went out of control and crashed in the sea. All three occupants were killed.

Crash of a Piper PA-31-350 Navajo Chieftain near Petros: 2 killed

Date & Time: Aug 2, 1984 at 1400 LT
Operator:
Registration:
N27948
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Fort Lauderdale - Cincinnati
MSN:
31-7952059
YOM:
1979
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1100
Circumstances:
The flight departed Fort Lauderdale, FL, on 8-2-84 at approximately 0815 edt for Cincinnati, OH. The aircraft wreckage was found on 11-17-84 on an up slope of big Fodderstack Mountain. The aircraft had contacted a 25 feet tall tree located 200 feet west of the main wreckage. The only known radio contact was recalled by the Monroe County airport manager who stated the pilot radioed to exchange the day's greeting. Exact weather at the accident site could not be determined. However, the airport manager recalled the high terrain being obscured with poor visibility. Both occupants were killed.
Probable cause:
Occurrence #1: in flight encounter with weather
Phase of operation: cruise - normal
Findings
1. (f) weather condition - low ceiling
2. (c) vfr flight into imc - continued - pilot in command
3. (f) lack of total instrument time - pilot in command
----------
Occurrence #2: in flight collision with object
Phase of operation: cruise - normal
Findings
4. (c) clearance - not maintained - pilot in command
5. (f) terrain condition - mountainous/hilly
6. Object - tree(s)
Final Report:

Crash of a Cessna 340A near Orangeville: 1 killed

Date & Time: Nov 20, 1983 at 1255 LT
Type of aircraft:
Registration:
N85JK
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Savannah – Fort Lauderdale
MSN:
340A-0700
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The aircraft disappeared from radar coverage while in cruise flight at 10,000 feet msl near Orangeville, FL. The ATC transcript revealed that the pilot had been inquiring about the weather ahead of him and was cleared to descend to 6,000 feet in order to get below strong headwinds. One minute later he transmitted that he was going to stay at 10,000 feet because he did not have any choice (strong turbulence). His last transmission stated the weather was getting worse. The aircraft has not been located.
Probable cause:
Occurrence #1: missing aircraft
Phase of operation: unknown
Findings
1. Reason for occurrence undetermined
Final Report:

Crash of a Cessna 411 in Fort Lauderdale

Date & Time: Sep 10, 1983 at 0759 LT
Type of aircraft:
Registration:
N256EL
Flight Type:
Survivors:
Yes
Schedule:
Fort Lauderdale - Atlantic
MSN:
411-0242
YOM:
1967
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7200
Captain / Total hours on type:
500.00
Aircraft flight hours:
2439
Circumstances:
The aircraft crashed while maneuvering at low airspeed and altitude right after takeoff. The pilot said the left engine started losing power intermittently at 90 knots. The pilot had rotated the aircraft and tried to continue the takeoff. He was cleared to land on any runway and in attempting a turn with landing gear and partial flaps extended control was lost and a crash occurred. The aircraft flight manual states that if an engine fails below 105 mph the takeoff should be aborted. An on scene examination revealed no evidence to suggest a pre-impact failure or malfunction. Both propellers showed evidence of torsional overload damage. When the engines were further examined the left engine fuel strainer was partially clogged with dirt. During a run-up test the left engine would not develop more than 23 inches hg. At 2,750 rpm and magneto rpm drop was erratic. The engine would not run with the aux fuel boost pump off. The reason for the low power output was a disconnected pressure line for the turbocharger which appeared to have been disconnected for some time. All five occupants were injured, two of them seriously.
Probable cause:
Occurrence #1: loss of engine power (partial) - mech failure/malf
Phase of operation: takeoff - initial climb
Findings
1. (c) fuel system, strainer - blocked (partial)
2. (c) exhaust system, turbocharger - disconnected
----------
Occurrence #2: loss of control - in flight
Phase of operation: takeoff - initial climb
Findings
3. (c) flight controls - improper use of - pilot in command
4. (c) throttle/power control - improper use of - pilot in command
5. (c) abort - not performed - pilot in command
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: maneuvering

Crash of a Piper PA-31-310 Navajo in Fort Pierce

Date & Time: Feb 6, 1982 at 2115 LT
Type of aircraft:
Registration:
N747CE
Flight Type:
Survivors:
Yes
Schedule:
Montego Bay - Fort Lauderdale
MSN:
31-673
YOM:
1970
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Aircraft flight hours:
5211
Circumstances:
The aircraft crashed at night near a private strip in marginal weather conditions. The gear was found in the up position, the right engine was broken off, the nose section was crushed back to the windshield, and both propellers were bent and twisted. About 1,300 lbs of marijuana was found on board.
Probable cause:
Occurrence #1: in flight collision with terrain/water
Phase of operation: unknown
Findings
1. (f) stolen aircraft/unauthorized use - performed - pilot in command
2. (f) light condition - dark night
3. (f) weather condition - low ceiling
4. (c) vfr flight into imc - continued - pilot in command
5. (c) altitude - misjudged - pilot in command
6. (f) visual/aural perception - pilot in command
Final Report:

Crash of a Beechcraft D18S in Claxton

Date & Time: Mar 2, 1981 at 2100 LT
Type of aircraft:
Operator:
Registration:
N80162
Survivors:
Yes
Schedule:
Fort Lauderdale - Claxton
MSN:
A-123
YOM:
1946
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6024
Captain / Total hours on type:
638.00
Circumstances:
On a night approach to Claxton-Evans County (Clayton) Airport, both engines flamed out due to fuel exhaustion. The aircraft lost height and while the pilot was attempting an emergency landing, the airplane struck trees and crashed. Both occupants were seriously injured.
Probable cause:
Double engine failure on final approach and subsequent collision with trees and crash due to inadequate preflight preparation. The following contributing factors were reported:
- Mismanagement of fuel,
- Fuel exhaustion,
- Failure of both engines,
- Forced landing off airport on land.
Final Report: