Crash of a Cessna 402B in Walker's Cay

Date & Time: Mar 31, 2004 at 1235 LT
Type of aircraft:
Operator:
Registration:
N269JH
Flight Type:
Survivors:
Yes
Schedule:
Fort Lauderdale – Walker’s Cay
MSN:
402B-1213
YOM:
1976
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On March 31, 2004, about 1235 eastern standard time, a Cessna 402B, N269JH, registered to and operated by Tropic Air Charters, Inc., experienced collapse of all landing gears at the Walker's Cay Airport, Walker's Cay, Bahamas. Visual meteorological conditions prevailed at the time and a visual flight rules flight plan was filed for the 14 CFR Part 135 on-demand, non-scheduled, international, cargo flight from the Fort Lauderdale Executive Airport, Fort Lauderdale, Florida, to the Walker's Cay Airport, Walker's Cay, Bahamas. The airplane was substantially damaged and the commercial-rated pilot, the sole occupant, was not injured. The flight originated about 45 minutes earlier from the Fort Lauderdale Executive Airport. The pilot stated that after landing, the right wing tipped down in what appeared to be a flat tire. He attempted to maintain control of the airplane using the rudder and was successful until the airplane rolled approximately 1,000 feet. The airplane then veered to the right and collided with a tree. The left wing and fuselage were damaged.

Crash of a Learjet 25B in Fort Lauderdale

Date & Time: Feb 20, 2004 at 2157 LT
Type of aircraft:
Operator:
Registration:
N24RZ
Flight Type:
Survivors:
Yes
Schedule:
San Juan – Fort Lauderdale
MSN:
25-159
YOM:
1974
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4500
Aircraft flight hours:
4104
Circumstances:
The captain and first officer were conducting a CFR Part 135 on-demand charter flight, returning two passengers to the accident airplane's base airport. The multi-destination flight originated from the accident airport, about 16 hours before the accident. On the final leg of the flight, the flight encountered stronger than anticipated headwinds, and the first officer voiced his concern several times about the airplane's remaining fuel. As the flight approached the destination airport, the captain became concerned about having to fly an extended downwind leg, and told the ATCT specialist the flight was low on fuel. The ATCT specialist then cleared the accident airplane for a priority landing. According to cockpit voice recorder (CVR) data, while the crew was attempting to lower the airplane's wing flaps in preparation for landing, they discovered that the flaps would not extend beyond 8 degrees. After the landing gear was lowered, the captain told the first officer, in part: "The gear doors are stuck down.... no hydraulics." The captain told the first officer: "Okay, so we're gonna do, this is gonna be a ref and twenty...All right, probably not going to have any brakes..." According to a ATCT specialist in the control tower, the airplane touched down about midway on the 6001-foot long, dry runway. It continued to the end of the runway, entered the overrun area, struck a chain link fence, crossed a road, and struck a building. During a postaccident interview, the captain reported that during the landing roll the first officer was unable to deploy the airplane's emergency drag chute. He said that neither he nor the first officer attempted to activate the nitrogen-charged emergency brake system. The accident airplane was not equipped with thrust reversers. A postaccident examination of the accident airplane's hydraulic pressure relief valve and hydraulic pressure regulator assembly revealed numerous indentations and small gouges on the exterior portions of both components, consistent with being repeatedly struck with a tool. When the hydraulic pressure relief valve was tested and disassembled, it was discovered that the valve piston was stuck open. The emergency drag chute release handle has two safety latches that must be depressed simultaneously before the parachute will activate. An inspection of the emergency drag chute system and release handle disclosed no pre accident mechanical anomalies.
Probable cause:
The pilot in command's misjudged distance/speed while landing, and the flightcrew's failure to follow prescribed emergency procedures, which resulted in a runway overrun and subsequent collision with a building. Factors associated with the accident are the flightcrew's inadequate in-flight planning/decision making, which resulted in a low fuel condition; an open hydraulic relief valve, and inadequate maintenance by company maintenance personnel. Additional factors were an inoperative (normal) brake system, an unactivated emergency drag chute, the flightcrew's failure to engage the emergency brake system, and pressure placed on the flightcrew due to conditions/events.
Final Report:

Crash of a Beechcraft C90 King Air near Homestead: 2 killed

Date & Time: Jan 31, 2004 at 1632 LT
Type of aircraft:
Registration:
N75GC
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Marathon – Fort Lauderdale
MSN:
LJ-727
YOM:
1977
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
4528
Captain / Total hours on type:
200.00
Aircraft flight hours:
8208
Circumstances:
The instrument rated pilot received three weather briefings on the date of the accident from the Miami Automated Flight Service Station. The pilot obtained his IFR clearance while airborne, was advised to climb to 9000 feet mean sea level (MSL), then later advised to descend and maintain 2000 feet, and to fly heading 030 degrees. Radar data indicates that following the instruction from the controller, the airplane made a right descending turn to a southeasterly heading, followed by a left turn to an easterly heading where the airplane was lost from radar while at 2,200 feet mean sea level. The crash was located 138 degrees and .38 nautical mile from the last radar target. Between 1631:04, and 1631:16, the airplane descended from 7,600 to 6,100 feet. Between 1631:16, and the last radar target 12 seconds later at 1631:28, the airplane descended 3,900 feet. Weather radar data indicates the airplane encountered video integrator and processor (VIP) Level 2, or "moderate intensity" echoes in the area of the in-flight loss of control. Approximately 10 and 20 miles east-northeast through southeast of the accident site, maximum echoes of VIP Level 5 to 6, or "intends to extreme intensity" echoes were noted. The strongest reflectivities were located 20 miles east of the accident site. Disintegration of the airplane was noted; there was no evidence of in-flight, or post crash fire of any recovered components. The full span of the left wing, left aileron, left horizontal, and left elevator were accounted for. A section of the right wing and right outboard flap was identified; the right wing was fragmented. Examination of the engine and propellers revealed no evidence of preimpact failure or malfunction. No determination was made whether the pilot met the instrument recency of experience requirement of 14 CFR Part 61.57 (c).
Probable cause:
The pilot's inadequate in-flight planning/decision which resulted in an encounter with rain showers and turbulence, a loss of aircraft control, and overstress of the airframe.
Final Report:

Crash of a Piper PA-31-310 Navajo in Jupiter

Date & Time: Aug 2, 2003 at 1301 LT
Type of aircraft:
Operator:
Registration:
N876RD
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Akron – Fort Lauderdale
MSN:
31-7300974
YOM:
1973
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1106
Captain / Total hours on type:
29.00
Aircraft flight hours:
1493
Circumstances:
The pilot stated that he and his wife were en route to a medical conference which was to be held aboard a cruise ship that was departing from Fort Lauderdale, Florida, at 1700. He stated that both tanks were full of fuel when he departed the Canton Regional Airport, Canton, Ohio, en route to Fort Lauderdale Executive Airport. According to the pilot, the inboard tanks had been selected for the first hour and a half and the outboard tanks for the following two hours. He said the flight was vectored around thunderstorms, and during the descent, when about 12 miles to the north of Palm Beach International Airport, Palm Beach, Florida, the left engine ceased operating. He said that at this time he noticed that both inboard fuel indicators showed the tanks to be empty, and he switched to the outboard tanks, both of which were shown to be a quarter full. The pilot stated that two minutes later both engines began to surge, and after making an emergency radio communications call, he was advised by the FAA Air Traffic Controller that Tailwinds Airport was located 4 miles to the west. Unable to reach the runway at Tailwinds Airport, the pilot said he made a forced landing in an orange grove. the pilot also said that prior to the accident, there had not been any mechanical failure or malfunctions to the airplane or any of its systems. Examination of the accident site revealed that the airplane had incurred substantial damage, and there was little or no fuel present at the scene. Follow-on examination of the airplane, its fuel system and both engines revealed no anomalies.
Probable cause:
The pilot's failure to adequately plan for the flight which resulted in fuel exhaustion, a forced landing, and damage to the airplane during the landing.
Final Report:

Crash of a Beechcraft B200 Super King Air in Spanish Cay

Date & Time: Aug 12, 2000 at 1115 LT
Registration:
N3199A
Flight Type:
Survivors:
Yes
Schedule:
Fort Lauderdale – Spanish Cay
MSN:
BB-1499
YOM:
1995
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On August 12, 2000, about 1115 eastern daylight time, a Beechcraft B200, N3199A, registered to and operated by Great Texas Food Inc. as a Title 14 CFR Part 91 personal flight, ran off the side of the runway during landing in Spanish Cay, Bahamas. Visual meteorological conditions prevailed at the time and a visual flight rules flight plan was filed. The private-rated pilot and the two passengers received no injuries. The flight originated from Fort Lauderdale, Florida, the same day, about 1030. The pilot stated that he made an uneventful landing and as he applied the brakes, the left brake did not respond. He stated that he lost control of the aircraft and exited the runway from the right side and impacted a berm. The right landing gear collapsed, the left wing and the front fuselage incurred substantial damage.

Crash of a Canadair CL-600 Challenger in Fort Lauderdale

Date & Time: Aug 16, 1999 at 2347 LT
Type of aircraft:
Operator:
Registration:
N63HJ
Flight Type:
Survivors:
Yes
Schedule:
Pueblo – Columbia
MSN:
1021
YOM:
1981
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10162
Captain / Total hours on type:
540.00
Aircraft flight hours:
9503
Circumstances:
While enroute from Pueblo, Colorado, to Columbia, South Carolina, the captain's windshield delaminated, and the flight diverted to Fort Lauderdale, Florida, for repairs. The flight crew stated the first officer was flying the airplane and had been instructed by the captain to make a firm landing at Fort Lauderdale to get the airplanes weight on the wheels, due to the airplane being light. The landing was firm and the first officer activated the engine thrust reversers. As the nose landing gear touched down, the airplane began veering to the left. Attempts to control the veer to the left were unsuccessful and the airplane ran off the left side of the runway. The airplane then ran over a taxiway and collided with a taxiway sign and the concrete base for the sign. The nose landing gear collapsed and the airplane came to rest. Examination of the runway showed alternating dark and light marks from the left main landing gear tire were present on the runway about 160 feet before marks from the right main landing gear tire are present. Post accident examination of the airplanes landing gear, tires, wheels, bakes, spoilers, and engine thrust reversers, showed no evidence of pre-accident failure or malfunction. At the time of the accident the flight crew had been on duty for about 17 hours 45 minutes.
Probable cause:
The failure of the flight crew to main directional control of the airplane after landing, resulting in the airplane going off the side of the runway and colliding with a taxiway sign, collapsing the nose landing gear, and causing substantial damage to the airplane. A factor in the accident was flight crew fatigue due to being on duty for about 17 hours 45 minutes.
Final Report:

Crash of a Cessna 402B in Fort Lauderdale

Date & Time: Apr 20, 1999 at 1910 LT
Type of aircraft:
Registration:
N744MA
Flight Type:
Survivors:
Yes
Schedule:
Fort Myers – Fort Lauderdale
MSN:
402B-0592
YOM:
1974
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2600
Captain / Total hours on type:
500.00
Aircraft flight hours:
2675
Circumstances:
While on approach to land the left engine surged and lost power. The pilot switched the left engine fuel selector to another fuel tank and the engine restarted. A short time later the left engine surged and lost power again. The pilot switched the left engine fuel selector to the right main fuel tank and the engine again restarted. A short time later the left engine quit again and he shutdown the engine and feathered the propeller. A short time later the right engine surged and lost power. He shut down the right engine and feathered the propeller. He then made a forced landing in a field and during landing rollout the aircraft's left wing collided with a tree. A fire erupted in the left wing area. Post crash examination showed the right main fuel tank was empty. The right auxiliary fuel tank contained 2.5 gallons. The left main fuel tank contained one half gallon of fuel and the left auxiliary tank was ruptured. The pilot operating handbook stated that the main fuel tanks had one gallon unusable fuel and the auxiliary fuel tanks had one half gallon of unusable fuel.
Probable cause:
A loss of engine power due to fuel exhaustion and the pilot in command's failure to ensure that the aircraft had adequate fuel to complete the flight.
Final Report:

Crash of a Beechcraft UC-45J Expeditor in Miami

Date & Time: May 2, 1996 at 1052 LT
Type of aircraft:
Operator:
Registration:
N64819
Flight Type:
Survivors:
Yes
Schedule:
Miami - Fort Lauderdale
MSN:
5834
YOM:
1943
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8064
Captain / Total hours on type:
2245.00
Aircraft flight hours:
4254
Circumstances:
During departure, the rubber connector for the fuel supply line to the right engine oil dilution valve split at the dilution valve on the aft side of the firewall. The engine would not operate unless the electric boost pump was turned on. While returning to the departure airport, a fire erupted in the right wheel after the landing gear was extended. The cockpit filled with smoke during the landing rollout, and the pilot lost directional control do to not being able to see. The aircraft rolled into a canal and came to rest. The split rubber fuel line connector was dry and brittle and did not have any fire damage. No other sources of fuel leakage was found.
Probable cause:
Inadequate inspection of the fuel line connector by company maintenance personnel, and failure of a connector resulting in a fuel leak and fire.
Final Report:

Crash of a Beechcraft 65 Queen Air near Orlando: 5 killed

Date & Time: Dec 19, 1992 at 0739 LT
Type of aircraft:
Registration:
N555GC
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Sanford – Fort Lauderdale
MSN:
LC-164
YOM:
1965
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
8269
Captain / Total hours on type:
40.00
Aircraft flight hours:
3700
Circumstances:
Pilot reported level at 6,000 feet; no further transmissions were received. Radar data shows that after 5 minutes at cruise flight ground speed began to slow, and as speed reached 85 knots (VMC is 83 knots) aircraft made a rapid turn to the left and the speed dropped to 74 knots. Radar contact was then lost. Witnesses reported hearing and seeing aircraft with an engine sputtering and quitting, at which time no engine noise was audible. Engine would then restart, and at one point aircraft was observed initiating a climb after engine start. Engine restarted and obtained near full power, and a short time later sound of impact was heard. The left engine fuel servo was found contaminated with corrosion and dirt, and would not allow fuel flow to the engine. The fuel strainer for this engine was installed backwards allowing unfiltered fuel to enter the engine. The left propeller was not feathered and had no signs of rotation under power. Right engine fuel servo also contained corrosion and contamination. The aircraft did not have a current annual inspection. All five occupants were killed.
Probable cause:
The pilot's failure to feather the propeller to maintain altitude following a loss of power of the left engine. The power loss was due to an improperly maintained fuel system. In addition, the right engine lost power for an undetermined reason(s).
Final Report:

Crash of a Rockwell Turbo Commander 680V in Fort Lauderdale: 2 killed

Date & Time: Nov 3, 1990 at 1025 LT
Registration:
N541F
Flight Type:
Survivors:
No
Schedule:
Fort Lauderdale - Fort Lauderdale
MSN:
680-1609-45
YOM:
1967
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1100
Aircraft flight hours:
6288
Circumstances:
The airplane had not flown since June 1989. The flight had made 2 high speed taxi operations before takeoff. Immediately after takeoff the flight called to land. The airplane was observed on downwind 200-800 feet agl, 15-25° nose high. The airplane then stalled. The compressor surge valves for the left and right engines were found in the open position. Both occupants were killed.
Probable cause:
The pilot-in-command's decision to continue takeoff with a known deficiency in the airplane - low power on both engines which resulted from open compressor surge valves. The pilot subsequently failed to maintain airspeed while maneuvering in a turn resulting in an inflight loss of control and a stall/spin.
Final Report: