Crash of a Boeing 720-051B in the Everglades National Park: 43 killed

Date & Time: Feb 12, 1963 at 1350 LT
Type of aircraft:
Operator:
Registration:
N724US
Flight Phase:
Survivors:
No
Schedule:
Miami – Chicago – Spokane – Seattle – Portland
MSN:
18354
YOM:
1961
Flight number:
NW705
Crew on board:
8
Crew fatalities:
Pax on board:
35
Pax fatalities:
Other fatalities:
Total fatalities:
43
Captain / Total flying hours:
17835
Captain / Total hours on type:
150.00
Copilot / Total flying hours:
11799
Copilot / Total hours on type:
1093
Aircraft flight hours:
4684
Circumstances:
The aircraft arrived in Miami at 1240, following a routine flight from Chicago, Illinois The captain of the inbound flight reported that the only mechanical discrepancy was, "the outflow valves being a little sticky merely made it a little difficult to maintain the pressurization in a smooth manner. "These valves were cleaned, and a leaking rivet at the No. 4 reserve fuel tank was plugged when it was noticed by the mechanic. This was the only maintenance performed during the "turnaround". Flight 705 is regularly scheduled from Miami. to Portland, Oregon, with intermediate stops at Chicago, Illinois and Spokane and Seattle, Washington. The computed takeoff gross weight of 175,784 pounds, and center of gravity (e.g.) of 25 percent mean aerodynamic chord (MAC) were both well within the allowable limits. Prior to departing the ramp at 1325, the crew asked the ground controller about the departure routes being utilized, and he replied that most flights were departing ". . either through a southwest climb or a southeast climb and then back over the top of it. . . "The flight departed Miami with an Instrument Flight Rules (IFR) clearance at 1335 In accordance with the pilot's request for a". . . southeast vector "a left turn was rude after takeoff from runway 27L and circuitous routing was utilized in conjunction with radar vectors from Miami Departure Control, to avoid *** of anticipated turbulence associated with thunderstorm activity (See Attachment A). A similar departure pattern had been previously flown by another flight Subsequently, while maintaining 5,000 feet and a heading of 300 degrees, Flight 705 requested clearance to climb to a higher altitude. Following a discussion between the flight and the Federal Aviation Agency (FAA) radar departure controller about the storm activity, and while clearance to climb was being coordinated with the Miami Air Route Traffic Control Center (ARTCC), the flight advised "Ah-h we're in the clear now. We can see it out ahead . . . looks pretty bad." At 1343, Flight 705 was cleared to climb to flight level 2/ 250 (FL250). They responded, "OK ahhh, we'll make a left turn about thirty degrees here and climb. . "The controller asked of 270 degree was their selected climbout heading, and they replied that this would take them". . . out in the open again". . Accordingly, clearance was granted. Following some discussion about the severity of the turbulence, which was described as moderate to heavy, the flight advised, "OK, you better run the rest of them off the other way then." At 1345 radar service was terminated and control of Flight 705 was transferred to Miami ARTCC. When the flight did not establish radio communication with ARTCC on the initial frequency, Departure Control provided a secondary frequency, and instructed the flight to turn to a heading of 360 degrees which was acknowledged. When Miami ARTCC requested position and altitude, the flight replied, "We're just out of seventeen five (17,500 feet) and standby on the DME one." This transmission ended at 1348, and was the last known communication with Flight 705 The voice transmissions emanating from the flight were made by the first officer. Witnesses in the area reported that a loud explosion had occurred in the air, and several felt a subsequent ground tremor. They also reported that heavy rain had been failing in the area. One witness, in company with five other persons, was seven miles south of the main wreckage site She heard the sound of an explosion which had no echo. When she looked in that direction she saw an orange ball of flame in the edge of a cloud. As she directed the attention of her companions toward this flame, it dropped straight down, becoming a streak, and disappeared behind trees. Shortly after the disappearance a second sound was heard. Statements were received from the crews of four other flights operating in the Miami area at the approximate time of the accident. The first, in a large jet which approached Miami from the west at 7,000 feet, reported the weather as ". . . in and out of broken clouds and light rain showers with light turbulence. Darker heavy shower activity was observed to the (south) of course. We observed no small cells on our radar scope. . only a broad rain area. . . "Another crew, in a four-engine aircraft, departed Miami at 1318, via a departure pattern similar to that which Flight 705 later followed. They described the worst turbulence as". medium to moderate . . . "from west of the airport to north of the Miami VORTAC .3/ They were maintaining 5,000 feet at the time. A third crew in a 720B was folding southeast of Miami at 13,000 feet. They observed numerous rain cells on radar in the Miami area and encountered light ice at this altitude. The fourth crew, also flying a large jet, taxied out shortly after Flight 705 but delayed takeoff for nearly an hour because of the weather. The weather in the Miami area at the time of the accident was characterized by a pre-frontal squall line approximately 250 miles in length, oriented on a northeast-southwest line immediately northwest of Miami (See Attachment A). The U. S. Weather Bureau (USWB) radar observation at Miami at 1344 indicated a broken area of thunderstorms associated with this line, with cells two to twenty miles in diameter, and tops of detectable moisture at 30,000 feet. The line was moving southeast at eight knots, and moderate rain showers were occurring at the station. The 0600 and 1800 Miami radiosonde ascents showed the freezing level to have been at 11,100 and 12,400 feet m.s.1., respectively. SIGMET 4/ No. 3 prepared by the USWB at Miami, valid from 0900-1300, forecast moderate to severe turbulence 5/ in thunderstorms, with a chance of extreme turbulence in heavier thunderstorms. This advisory was called to the attention of the crew of Flight 705 by the operations agent at Miami, and was attached to their dispatch papers. SIGMET No. 4, valid from 1300-1700, was not received until approximately 1315, after the crew of Flight 705 had left the operations office. It forecast moderate to severe turbulence, but deleted the reference to extreme turbulence indicated in SIGMET No 3. Since the dispatcher for this flight is stationed in Minneapolis, the physical Limitations involved made it difficult to apprise the crew of this latest advisory prior to their taxi time of 1325. The aircraft was completely destroyed by impact forces and all 43 occupants have been killed.
Probable cause:
The Board determines that the probable cause of this accident was toe unfavorable interaction of severe vertical air drafts and large longitudinal control displacements resulting in a longitudinal "upset" from which a successful recovered was not made.
Final Report:

Crash of a Lockheed L-1049H Super Constellation in Burbank: 8 killed

Date & Time: Dec 14, 1962 at 2212 LT
Operator:
Registration:
N6913C
Flight Type:
Survivors:
No
Schedule:
Boston – Windsor Locks – Chicago – Burbank
MSN:
4810
YOM:
1957
Flight number:
FT183
Crew on board:
3
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
8
Captain / Total flying hours:
14164
Captain / Total hours on type:
5100.00
Copilot / Total flying hours:
560
Copilot / Total hours on type:
560
Aircraft flight hours:
20269
Circumstances:
On December 14, 1962, at 2212 P.s.t., a Flying Tiger Line Inc., Super Constellation, N6913C, crashed about 1-1/4 miles west of the Lockheed Air Terminal, Burbank California, during an ILS approach to runway 7. All five persons on board the aircraft and three persons on the ground sustained fatal injuries. The last radio communication with N6913C was the flight's acknowledgement of its radar-observed position two miles from the end of the runway on the localizer course. Twenty seconds later the aircraft crashed Into a fog-shrouded residential/industrial area.
Probable cause:
The incapacitation of the pilot-in-command, at a critical point in the approach resulting in a loss of control of the aircraft from which the co-pilot was unable to recover.
Final Report:

Crash of a Douglas DC-7 in Chicago

Date & Time: Dec 16, 1961
Type of aircraft:
Operator:
Registration:
N4871C
Survivors:
Yes
MSN:
44261
YOM:
1954
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed on landing for unknown reason. There were no injuries among the occupants while the aircraft was damaged beyond repair.

Crash of a Lockheed L-188C Electra in Chicago: 37 killed

Date & Time: Sep 17, 1961 at 0857 LT
Type of aircraft:
Operator:
Registration:
N137US
Flight Phase:
Survivors:
No
Schedule:
Milwaukee – Chicago – Tampa – Fort Lauderdale – Miami
MSN:
1142
YOM:
1961
Flight number:
NW706
Crew on board:
5
Crew fatalities:
Pax on board:
32
Pax fatalities:
Other fatalities:
Total fatalities:
37
Captain / Total flying hours:
15898
Captain / Total hours on type:
314.00
Copilot / Total flying hours:
6643
Copilot / Total hours on type:
90
Aircraft flight hours:
614
Circumstances:
At approximately 0855 1, the flight was cleared for takeoff on runway 14R. At this time the aircraft was taxing on a westerly heading in the runup area adjacent to runway 14R. Flight 706 acknowledged the clearance, while continuing toward the runway, and made a running takeoff No witnesses were found who observed the actual lift-off. N137US was observed after lift-off, 3,000 to 4,000 feet down the runway at an estimated altitude of 50 to 75 feet and in a normal climb attitude. At the 8,000-foot marker the altitude of the aircraft was estimated to have been approximately 100 feet, which is a slightly lower altitude than Electra aircraft normally attain at this point during takeoff. Five witnesses noted a change in engine sound during this portion of the flight. Between the 8,000 and the 9,000 foot runway marker the aircraft was observed to commence an apparently coordinated right turn with a slowly increasing rate of bank. When the bank angle was 30 to 45 degrees, the crew made a short, garbled transmission. Immediately thereafter, at a bank angle of 50 to 60 degrees, the aircraft began to lose altitude. The minimum altitude attained in the entire turn was 200 to 300 feet. The right wing near the No. 4 engine struck powerlines adjacent to the Chicago Northwestern Railroad tracks, severing the lines at an angle of about 70 degrees from the horizontal, and causing a bright bluish flash. The aircraft then continued in a direction of about 271 degrees magnetic and, when in a bank of about 85 degrees and a nose-down attitude of about 10 degrees, the right wing of the aircraft struck the railroad embankment. Continuing to roll about its longitudinal axis, the aircraft cartwheeled, the nose crashing into the ground 380 feet beyond the point of first Impact, and landed right side up It then slid tall first another 820 feet. The aircraft disintegrated throughout its path, and wreckage was strewn over an area 200 feet wide and 1,200 feet long. Evidence of ground fire was found at various points along this path. Impact occurred on airport property about 3,800 feet abeam and to the right of the end of runway 14R, about 500 feet north of Irving Park Road. After passing beyond the railroad embankment the aircraft was lost to view by most of the eye witnesses because of trees and other obstructions; immediately thereafter a large mushroom of orange-red flame accompanied by heavy black smoke was seen. Time of impact was established as 0857. The aircraft was demolished by impact and fire. All occupants were fatally injured.
Probable cause:
The Board determines that the probable cause of this accident was a mechanical failure in the aileron primary control system due to an improper replacement of the aileron boost assembly, resulting in a loss of lateral control of the aircraft at an altitude too low to effect recovery.
Final Report:

Crash of a Douglas DC-8-11 in New York: 90 killed

Date & Time: Dec 16, 1960 at 1033 LT
Type of aircraft:
Operator:
Registration:
N8013U
Survivors:
No
Site:
Schedule:
Chicago – New York
MSN:
45290
YOM:
1959
Flight number:
UA826
Crew on board:
7
Crew fatalities:
Pax on board:
77
Pax fatalities:
Other fatalities:
Total fatalities:
90
Captain / Total flying hours:
19100
Captain / Total hours on type:
344.00
Copilot / Total flying hours:
8500
Copilot / Total hours on type:
379
Aircraft flight hours:
2434
Circumstances:
On December 16, 1960, at 1033 e.s.t., a collision between Trans World Airlines Model 1049A Constellation, N 6907C, and a United Air Lines DC-8, N 8013U, occurred near Miller Army Air Field, Staten Island, New York. Trans World Airlines Flight 266 originated at Dayton, Ohio. The destination was LaGuardia Airport, New York, with one en route stop at Columbus, Ohio United Air Lines Flight 826 was a non-stop service originating at O'Hare Airport, Chicago, Illinois, with its destination New York International Airport, New York. Both aircraft were operating under Instrument Flight Rules. Following the collision the Constellation fell on Miller Army Field, and the DC-8 continued in a northeasterly direction, crashing into Sterling place near Seventh Avenue in Brooklyn, New York. Both aircraft were totally destroyed. All 128 occupants of both aircraft and 6 persons on the ground in Brooklyn were fatally injured. There was considerable damage to property in the area of the ground impact of the DC-8. TWA Flight 266 departed Port Columbus Airport at 0900, operating routinely under Air Traffic Control into the New York area The New York Air Route Traffic Control Center (ARTCC) subsequently advised that radar contact had been established and cleared the flight to the Linden. Intersection, Control of the flight was subsequently transferred to LaGuardia Approach Control. When the flight was about over the Linden Intersection, LaGuardia Approach Control began vectoring TWA 266 by radar to the final approach course for a landing on runway 4 at LaGuardia. Shortly thereafter TWA 266 was cleared to descend to 5,000 feet, and was twice advised of traffic in the vicinity on a northeasterly heading. Following the transmission of this information the radar targets appeared to merge on the LaGuardia Approach Control radar scope, and communications with TWA 266 were lost.United Air Lines Flight 826 operated routinely between Chicago and the New York area, contacting the New York ARTCC at 1012 Shortly thereafter the New York Center cleared UAL 826 to proceed from the Allentown, Pa., very high frequency omni directional radio range station (VOR) direct to the Robbinsville, New Jersey, VOR, and thence to the Preston Intersection via Victor Airway 123. At approximately 1021, UAL 826 contacted Aeronautical Radio, Inc. (ARINC) to advise their company that the No. 2 receiver accessory unit was inoperative, which would indicate that one of the aircraft's two VHF radio navigational receivers was not functioning. A "fix" is established by the intersection of two radials from two separate radio range stations. With one unit inoperative the cross-bearings necessary can be taken by tuning the remaining receiver from one station to the other. This process consumes considerable time, however, and is not as accurate as the simultaneous display of information on two separate position deviation indicators While UAL 826 advised the company that one unit was inoperative, Air Traffic Control was not advised. At 1025 the New York ARTCC issued a clearance for a new routing which shortened the distance to Preston by approximately 11 miles. As a result, this reduced the amount of time available to the crew to retune the single radio receiver to either the Colt' s Neck, New Jersey, or Solberg, New Jersey, VOR in order to establish the cross-bearing with Victor 123, which would identify the Preston Intersection. In the event the crew would not attempt to retune the single VOR receiver, crossbearings on the Scotland Low Frequency Radiobeacon could be taken with the aircraft direction finding (ADF) equipment. This would be a means of identifying the Preston Intersection but, under the circumstances, would require rapid mental calculation in the interpretation of a display which could be easily misread. Several factors support the conclusion that this occurred. Instructions had been issued to UAL 826 for holding at the Preston Intersection the clearance limit, should holding be necessary. Clearance beyond Preston for an approach to Idlewild Airport would be received from Idlewild Approach Control and the transfer of control of the flight from the New York Center to Idlewild Approach Control would normally take place as the aircraft was approaching Preston. UAL 826 was not receiving radar vectors, but was providing its own navigation. After the flight reported passing through 6,000 feet the New York Center advised that radar service was terminated and instructed the flight to contact Idlewild Approach Control. UAL 826 then called Idlewild Approach Control, stating "United 826 approaching Preston at 5,000." This was the last known transmission from UAL 826. At the time UAL 826 advised it was approaching Preston it had in fact gone on by this clearance limit several seconds before and was several miles past the point at which it should have turned into the holding pattern. This is confirmed by the data obtained from the flight recorder which had been installed in the UAL DC-8, as well as by analysis of the communication tapes At a point approximately 11 miles past the Preston Intersection a collision occurred between TWA 266 and UAL 826. Weather at the altitude of the collision and at the time of the accident was such as to preclude flight by visual means.
Probable cause:
The Board determines that the probable cause of this accident was that United Flight 826 proceeded beyond its clearance limit and the confines of the airspace allocated to the flight by Air Traffic Control A contributing factor was the high rate of speed of the United DC-8 as it approached the Preston intersection, coupled with the change of clearance which reduced the enroute distance along VICTOR 123 by approximately 11 miles.
Final Report:

Crash of a Lockheed PV-1 Ventura in Jeffersonville: 8 killed

Date & Time: May 15, 1956 at 1038 LT
Type of aircraft:
Operator:
Registration:
N64001
Flight Type:
Survivors:
No
Schedule:
Chicago – Louisville
MSN:
5326
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
8
Captain / Total flying hours:
17600
Captain / Total hours on type:
9.00
Copilot / Total flying hours:
2297
Copilot / Total hours on type:
29
Aircraft flight hours:
3109
Circumstances:
The flight was for the purpose of transporting six Crane officials from Chicago, Illinois, to Louisville, Kentucky, to attend a business convention. Departure was from O'Hare-Chicago International Airport on a VFR flight plan (changed en route to IFR) with the Crane Company's Chief Pilot Randolph A. Mulherin in command, and Robert H. Robinette, also a Crane pilot, as copilot. Gross weight upon departure was estimated to be 27,360 pounds; the maximum permissible takeoff weight was 31,000 pounds. Shortly after takeoff the pilot gave a routine report to Chicago radio of his time off as 0908 and his estimated elapsed flight time as one hour and 20 minutes. He did not request weather information at that time. Other radio contacts followed as the flight progressed, the final one being at 1034 over the Jeffersonville intersection. An approach was then started from that point to the Standiford Airport, 6-9/10 miles distant. During this approach the aircraft struck trees and crashed at a point one-half mile north of the Jeffersonville intersection. The airplane was destroyed and all eight occupants have been killed.
Probable cause:
The Board determines that the probable cause of this accident was a critical loss of altitude, due to a complete power loss from the left engine and the drag of its windmilling propeller. The following findings were reported:
- Pilot Mulherin was relatively inexperienced with the subject model aircraft,
- The left engine suddenly lost all power because of a disconnected carburetor control,
- The left propeller was found not feathered,
- Examination of the right engine revealed no significant defect,
- Altitude could not be maintained and the aircraft struck high trees and then plunged steeply to the ground.
Final Report:

Crash of a Lockheed L-1049 Super Constellation in McChord AFB

Date & Time: Sep 6, 1953 at 0231 LT
Operator:
Registration:
N6214C
Survivors:
Yes
Schedule:
Seattle – Chicago
MSN:
4014
YOM:
1952
Flight number:
NW008
Crew on board:
6
Crew fatalities:
Pax on board:
26
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10863
Captain / Total hours on type:
263.00
Copilot / Total flying hours:
4230
Copilot / Total hours on type:
206
Aircraft flight hours:
4509
Circumstances:
Northwest Airlines' Flight 8 departed Seattle-Tacoma Airport at 0148, September 6, 1953, for a nonstop flight to Chicago, Illinois. Gross weight on takeoff was 105,839 pounds; maximum allowable for takeoff was 116,740; maximum allowable for landing was 98.500 pounds. The location of the center of gravity was within prescribed limits. Weather at Seattle-Tacoma Airport during takeoff was: ceiling 200 feet and one-fourth mile visibility. Just after the aircraft became airborne No. 3 propeller oversped. Attempts by the flight engineer to correct this condition were unsuccessful and feathering was started one and one-half minutes later. However, the propeller continued to rotate at about 400 r.p.m. The flight's takeoff alternate was Yakima, Washington (a distance of 122 miles), but due to high terrain en route the captain elected to request clearance to proceed to Portland, Oregon (a distance of 132 miles), at 5,000 feet. This clearance was granted immediately. Using METO 2 power the aircraft reached 5,000 feet, well above the overcast, about 14 minutes after takeoff. Near the end of this climb the oil temperature of No. 4 engine was exceeding limits and the oil supply was being rapidly reduced. The flight engineer attempted to lower the temperature by fully opening the oil cooler flap. Temperature, however, remained high and the oil quantity continued to dwindle fast. Accordingly, the No. 4 propeller was feathered at about 0205 at the order of the captain who then declared an emergency and elected to land at McChord Air Force Base. Radio communication was established with McChord and arrangements made for a GCA approach after a short delay in establishing a frequency. No. 3 propeller had not feathered fully and was still windmilling at approximately 400 r.p.m. Meanwhile the captain had requested "takeoff" flaps, but the flaps would not extend hydraulically, and the copilot went to the cabin to crank them down. He stated that he turned the crank about 15-20 turns, at which point he found that it would no longer turn freely, whereupon he backed it to its original position. He was then called back to the cockpit to assist the captain in controlling the aircraft. Control difficulty had been continuously experienced with the aircraft yawing sharply and dropping a wing. The captain had placed the trim controls approximately in neutral, believing that he had a better feel and control of the aircraft without them at the recommended minimum speed of 130 knots. The aircraft, which had re-entered the overcast at about 2,000 feet, was then several miles from McChord Field under GCA direction on its first approach when its position and heading became such that the GCA operator directed a box pattern be flown to establish a proper approach. The second approach was executed in accordance with the directed pattern and the final approach was in line with Runway 34. The landing gear control was not actuated for gear extension until the aircraft broke out of the overcast at an altitude estimated at between 500 and 800 feet on a GCA controlled straight-in approach to Runway 34. At this time the captain ordered that No. 3 be unfeathered but it would not unfeather and continued to windmill. Only the right main gear extended fully and locked, as Indicated by its green light, but the landing was then committed. Shortly after touchdown retraction of the unlocked nose and left main gears allowed the aircraft to veer off the runway to the left. It then skidded sideways to its right, folding the right main gear inward, and the No. 2 engine was torn free. The aircraft came to rest on a heading of 212 degrees some 3,000 feet from the point of touch and about 7,000 feet short of the far end of the 10,000-foot runway. At about that time a gasoline fire started and spread rapidly over the ground below the airplane. Previously alerted fire apparatus, already standing by, kept the fire from spreading while all passengers and four of the crew left quickly by the main cabin door, the door sill being five or six feet above the ground. The flight engineer and the captain left by the cockpit crew door after ascertaining the cabin to be empty. All 32 occupants ware clear within an estimated two minutes. There were no fatalities although several persons were treated for burns at the McChord Air Force Base Hospital.
Probable cause:
The Board determines that the probable cause of this accident was a sequence of mechanical failures resulting in an emergency landing under adverse weather conditions with insufficient hydraulic pressure in the secondary system to extend fully the landing gear in the time available. A contributing factor was the design of the hydraulic system which did not permit use of the available pressure in the primary system for that purpose. The following findings were pointed out:
- Shortly after takeoff the aircraft lost the use of No. 3 engine due to an overspeeding propeller, and continued windmilling,
- Weather conditions at Seattle-Tacoma were satisfactory for takeoff but were below landing minimums and the captain elected to proceed to Portland,
- After reaching cruising altitude No. 4 propeller was feathered because of high engine oil temperature and depletion of oil supply,
- After losing the use of No. 4 engine, the captain declared an emergency and set up a GCA approach to McChord Air Force Base,
- A malfunction of the landing gear selector valve prevented normal use of the diminished hydraulic pressure to extend the flaps,
- A GCA instrument approach to McChord was necessary because of weather conditions. The captain decided that he would extend the gear only after breaking out under the low overcast,
- The short time interval between breaking out and touchdown was insufficient for extension and locking of all three landing gears with the existing hydraulic pressure,
- After touchdown the unlocked and partially extended left main and nose gears were forced up into their wheel wells with complete loss of control of the aircraft's ground movement, and fire occurred after rupture of the fuel tanks,
- The functional failure of No. 3 propeller governor was due to foreign metallic particles,
- The reason for the loss of oil supply for No. 4 engine was undetermined,
- The landing gear selector valve was improperly seated, resulting in insufficient hydraulic pressure.
Final Report:

Crash of a Douglas C-47A-90-DL in Chicago: 1 killed

Date & Time: Apr 30, 1953
Operator:
Registration:
43-15780
Flight Type:
Survivors:
Yes
Schedule:
Chicago - Chicago
MSN:
20246
YOM:
1944
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The crew was completing a local training flight at Chicago-O'Hare Airport. On final approach, the airplane went out of control and crashed three miles northwest of the airfield. A crew member was killed while two others were injured.