Crash of a Cessna 340A in Tatum: 1 killed

Date & Time: Apr 19, 2021 at 1346 LT
Type of aircraft:
Registration:
N801EC
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Longview - Tatum
MSN:
340A-0312
YOM:
1977
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
28665
Captain / Total hours on type:
120.00
Aircraft flight hours:
6500
Circumstances:
The pilot was planning to perform a functional test of the airplane’s newly upgraded autopilot system. Automatic dependent surveillance-broadcast data showed that, after takeoff, the airplane turned east and climbed to 2,750 ft. Air traffic control information indicated that the controller cleared the pilot to operate under visual flight rules to the east of the airport. Communications between ground control, tower control, and the pilot were normal during the ground taxi, takeoff, and climb. Radio and radar communications were lost 6 minutes after takeoff, and no radio distress calls were received from the pilot. The airplane impacted wooded terrain about 3/4 mile to the east of the last recorded radar data point. Groundspeeds and headings were consistent throughout the flight with no abrupt deviations. The airplane impacted the wooded terrain in a nose-down, near-vertical flight attitude. Most of the airplane, including the fuselage, wings, and empennage, were consumed by a postimpact fire. Both engines and propellers separated from the airplane at impact with the ground. Examination of the engines revealed no preaccident failures or malfunctions that would have precluded normal operations. Both propellers showed signs of normal operation. Flight control continuity was confirmed. The elevator trim cables stop blocks were secured to the cables and undamaged. They were found against the forward stop meaning the trim tab was at full down travel (elevator leading edge full down) which indicated that the airplane was trimmed full nose up at impact. The airplane’s cabin sustained fragmentation from impact and was consumed by fire; as a result, the autopilot system could not be examined. The investigation was unable to determine why the pilot lost control of the airplane.
Probable cause:
The pilot’s loss of airplane control for undetermined reasons.
Final Report:

Crash of a Cessna 340A in Orléans

Date & Time: Aug 10, 2020 at 1355 LT
Type of aircraft:
Operator:
Registration:
N413JF
Flight Type:
Survivors:
Yes
Schedule:
Perpignan – Orléans
MSN:
340A-0746
YOM:
1979
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2635
Captain / Total hours on type:
41.00
Circumstances:
Then twin engine airplane departed Perpignan-La Llabanère Airport on a private flight to Orléans, carrying one passenger and one pilot. On final approach to Orléans-Loiret Airport (ex Saint-Denis-de-l’Hôtel), the pilot encountered a loss of power on the left engine. He attempted an emergency landing when the airplane impacted trees and crash landed in a wooded area located about 3 km short of runway 23, bursting into flames. Both occupants escaped uninjured while the airplane was totally destroyed by a post crash fire.
Probable cause:
The exact cause of the loss of power on the left engine could not be determined. The pilot, concentrating on monitoring the approach parameters, did not immediately realize the left engine malfunction. He noticed that the aircraft's rate of descent was too high to follow the standard approach slope. The pilot first attempted to go around and reconfigured the aircraft to do so by retracting the landing gear and flaps. In spite of these actions, the pilot noticed that the power delivered by the aircraft's engines did not allow him to recover the plane and understood, by being aware of the action of his right foot on the rudder pedal, that the power delivered by the left engine was abnormally low. Given the low height of the plane at the time of this observation, the pilot decided to land in the country. Contributing to the high rate of descent after the occurrence of the left engine malfunction was the fact that the drags were extended at the time the engine power decreased and the fact that the left propeller probably windmilling until the landing.
Final Report:

Crash of a Cessna 340A in Ponoka

Date & Time: Nov 13, 2018 at 1815 LT
Type of aircraft:
Operator:
Registration:
C-GMLS
Flight Type:
Survivors:
Yes
MSN:
340A-0771
YOM:
1979
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On approach to Ponoka-Labrie Field, the pilot encountered technical problems with the autopilot and decided to make a go-around. While in the circuit pattern, the autopilot failed to disconnect properly so the pilot attempted an emergency landing in a field. The airplane belly landed then contacted trees. Upon impact, the tail was torn off and the aircraft came to rest. The pilot was seriously injured.

Crash of a Cessna 340A in Santa Cruz

Date & Time: Oct 28, 2018 at 1030 LT
Type of aircraft:
Operator:
Registration:
N5224J
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Santa Cruz - Manaus
MSN:
340A-1035
YOM:
1980
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The twin engine airplane was engaged in a humanitarian flight from Bolivia to Brazil, carrying one passenger and a pilot. Shortly after takeoff from a little private airstrip located in the suburb of Santa Cruz, the crew was supposed to land at Santa Cruz-Viru Viru International Airport before continuing to Manaus, Brazil. After takeoff, the pilot encountered engine problems (power issue) and decided to return for an emergency landing when the airplane struck trees and belly landed in a grassy area located in Barrio Lindo. Both occupants were uninjured while the aircraft was damaged beyond repair.

Crash of a Cessna 340A in Saint Clair County: 1 killed

Date & Time: Sep 6, 2018 at 2347 LT
Type of aircraft:
Operator:
Registration:
C-GLKX
Flight Type:
Survivors:
No
Schedule:
Saint Thomas - Saint Clair County
MSN:
340A-1221
YOM:
1981
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
690
Captain / Total hours on type:
51.00
Aircraft flight hours:
4038
Circumstances:
The private pilot of the multi-engine airplane was conducting an instrument approach during night visual meteorological conditions. About 1.3 nautical miles (nm) from the final approach fix, the right engine lost total power. The pilot continued the approach and notified air traffic control of the loss of power about 1 minute and 13 seconds later. Subsequently, the pilot contacted the controller again and reported that he was unable to activate the airport's pilot-controlled runway lighting. In the pilot's last radio transmission, he indicated that he was over the airport and was going to "reshoot that approach." The last radar return indicated that the airplane was about 450 ft above ground level at 72 kts groundspeed. The airplane impacted the ground in a steep, vertical nose-down attitude about 1/2 nm from the departure end of the runway. Examination of the wreckage revealed that the landing gear and the flaps were extended and that the right propeller was not feathered. Data from onboard the airplane also indicated that the pilot did not secure the right engine following the loss of power; the left engine continued to produce power until impact. The airplane's fuel system held a total of 203 gallons. Fuel consumption calculations estimated that there should have been about 100 gallons remaining at the time of the accident. The right-wing locker fuel tank remained intact and contained about 14 gallons of fuel. Fuel blight in the grass was observed at the accident site and the blight associated with the right wing likely emanated from the right-wing tip tank. The elevator trim tab was found in the full nose-up position but was most likely pulled into this position when the empennage separated from the aft pressure bulkhead during impact. Examination of the airframe and engine revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation. Although there was adequate fuel on board the airplane, the pilot may have inadvertently moved the right fuel selector to the OFF position or an intermediate position in preparation for landing instead of selecting the right wing fuel tank, or possibly ran the right auxiliary fuel tank dry, which resulted in fuel starvation to the right engine and a total loss of power. The airplane manufacturer's Pilot Operating Handbook (POH) stated that the 20-gallon right- and left-wing locker fuel tanks should be used after 90 minutes of flight. However, 14 gallons of fuel were found in the right-wing locker fuel tank which indicated that the pilot did not adhere to the POH procedures for fuel management. The fuel in the auxiliary fuel tank should be used when the main fuel tank was less than 180 pounds (30 gallons) per tank. As a result of not using all the fuel in the wing locker fuel tanks, the pilot possibly ran the right auxiliary fuel tank empty and was not able to successfully restart the right engine after he repositioned the fuel selector back to the right main fuel tank. Postaccident testing of the airport's pilot-controlled lighting system revealed no anomalies. The airport's published approach procedure listed the airport's common traffic advisory frequency, which activated the pilot-controlled lighting. It is possible that the pilot did not see this note or inadvertently selected an incorrect frequency, which resulted in his inability to activate the runway lighting system. In addition, the published instrument approach procedure for the approach that the pilot was conducting indicated that the runway was not authorized for night landings. It is possible that the pilot did not see this note since he gave no indication that he was going to circle to land on an authorized runway. Given that the airplane's landing gear and flaps were extended, it is likely that the pilot intended to land but elected to go-around when he was unable to activate the runway lights and see the runway environment. However, the pilot failed to reconfigure the airplane for climb by retracting the landing gear and flaps. The pilot had previously failed to secure the inoperative right engine following the loss of power, even though these procedures were designated in the airplane's operating handbook as "immediate action" items that should be committed to memory. It is likely that the airplane was unable to climb in this configuration, and during the attempted go-around, the pilot exceeded the airplane's critical angle of attack, which resulted in an aerodynamic stall. Additionally, the pilot had the option to climb to altitude using singleengine procedures and fly to a tower-controlled airport that did not have any landing restrictions, but instead, he decided to attempt a go-around and land at his destination airport.
Probable cause:
The pilot's improper fuel management, which resulted in a total loss of right engine power due to fuel starvation; the pilot's inadequate flight planning; the pilot's failure to secure the right engine following the loss of power; and his failure to properly configure the airplane for the go-around, which resulted in the airplane's failure to climb, an exceedance of the critical angle of attack, and an aerodynamic stall.
Final Report:

Crash of a Cessna 340 in Bartow: 5 killed

Date & Time: Dec 24, 2017 at 0717 LT
Type of aircraft:
Registration:
N247AT
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Bartow – Key West
MSN:
340-0214
YOM:
1973
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
1600
Aircraft flight hours:
1607
Circumstances:
The instrument-rated private pilot and four passengers boarded the multiengine airplane inside a hangar. The pilot then requested that the airplane be towed from the hangar to the ramp, since he did not want to hit anything on the ramp while taxiing in the dense fog. Witnesses heard the pre-takeoff engine run-up toward the end of the runway but could not see the airplane as it departed; the engines sounded normal during the run-up and takeoff. A witness video recorded the takeoff but the airplane was not visible due to the dense fog. During the takeoff roll the airplane's tires chirped, which is consistent with the wheels touching down on the runway with a side load. The video ended before the accident occurred. The witnesses stated that the takeoff continued and then they heard the airplane impact the ground and saw an explosion. The weather conditions at the time of the accident included visibility less than 1/4 mile in fog and an overcast ceiling at 300 ft above ground level. The airplane's weight at the time of the accident was about 105 lbs over the maximum takeoff weight, which exceeded the center of gravity moment envelope. The excess weight would have likely extended the takeoff roll, decreased the climb rate, and increased the amount of elevator pressure required to lift off of the runway. A majority of the airplane was consumed by postcrash fire. The ground impact marks and wreckage distribution were consistent with the airplane rolling left over the departure end of the runway and impacting the ground inverted in a nearly vertical, nose-low attitude. Examination of the engines revealed operating signatures consistent with takeoff power at the time of impact. The elevator trim tab and actuator were found beyond their full up travel limits and the trim cable exhibited tension overload separations near the actuator. It is likely that, when the cable separated in overload, the chain turned the sprocket and extended the actuator rod beyond full travel. No anomalies were observed with the airframe, engines, or cockpit instrumentation that would have precluded normal operation. The investigation was unable to determine the status of the autopilot during the accident takeoff. Based on the evidence it's likely that when the airplane entered instrument meteorological conditions the pilot experienced spatial disorientation, which resulted in a loss of control and descent into terrain.
Probable cause:
The pilot's loss of control due to spatial disorientation during takeoff in instrument meteorological conditions.
Final Report:

Crash of a Cessna 340 in Fargo: 1 killed

Date & Time: Dec 1, 2016 at 1629 LT
Type of aircraft:
Operator:
Registration:
N123KK
Survivors:
No
Schedule:
Fargo - Fargo
MSN:
340-0251
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
7898
Aircraft flight hours:
7012
Circumstances:
The airplane was equipped with an air sampling system used to collect air samples at various altitudes. The accident occurred when the pilot was returning to the airport after taking air samples at various altitudes over oil fields. As he was being vectored for an instrument approach, the airplane overshot the runway's extended centerline. The pilot then reported that he had a fire on board. The airplane lost altitude rapidly, and radar contact was lost. Examination of the accident site indicated that the airplane struck the ground at high velocity and a low impact angle. One piece of the airplane's shattered Plexiglas windshield exhibited soot streaking on its exterior surface. This soot streaking did not extend onto the piece's fracture surface, indicative of the smoke source being upstream of the windshield and the smoke exposure occurring before windshield breakup at impact. Both nose baggage compartment doors were found about 2 miles south of the main wreckage, which indicative that they came off at nearly the same time and most likely before the pilot's distress call. Although there was no soot deposits, thermal damage, or deformation to the doors consistent with a "high energy explosion," the separation of the luggage compartment doors could have occurred due to an overpressure caused by the ignition of a fuel air mixture within the nose portion of the airplane. The ignition of fuel air mixtures can create overpressure events when they occur in confinement. An overpressure in the nose baggage compartment may have stretched the airframe enough to allow the doors to push open without deforming the latches. If it was a lean fuel air mixture, it would likely leave no soot residue. Post-accident examination revealed no evidence that the air sampling system, which was strapped to the seat tracks behind the copilot's seat, was the cause of the fire. The combustion heater, which was mounted in the right front section of the nose baggage compartment, bore no evidence of fuel leakage, but a fuel fitting was found loose.
Probable cause:
The loose fuel fitting on the combustion heater that leaked a lean fuel-air mixture into the nose baggage compartment. The mixture was most likely ignited by the combustion heater, blowing off the nose baggage compartment doors and starting an in-flight fire.
Final Report: