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Crash of a Fletcher FU-24-954 in Fox Glacier: 9 killed

Date & Time: Sep 4, 2010 at 1327 LT
Type of aircraft:
Registration:
ZK-EUF
Flight Phase:
Survivors:
No
Schedule:
Fox Glacier - Fox Glacier
MSN:
281
YOM:
1981
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total flying hours:
4554
Captain / Total hours on type:
41.00
Circumstances:
Shortly after take off from Fox Glacier aerodrome, while climbing, aircraft stalled and crashed in flames in a paddock near the airfield. All nine occupants, the pilot and 8 skydivers, were killed. The new owner and operator of the aeroplane had not completed any weight and balance calculations on the aeroplane before it entered service, nor at any time before the accident. As a result the aeroplane was being flown outside its loading limits every time it carried a full load of 8 parachutists. On the accident flight the centre of gravity of the aeroplane was well rear of its aft limit and it became airborne at too low a speed to be controllable. The pilot was unable to regain control and the aeroplane continued to pitch up, then rolled left before striking the ground nearly vertically.
Probable cause:
Findings:
- There were no technical defects identified that may have contributed to the accident and the aeroplane was considered controllable during the take-off roll, with the engine able to deliver power during the short flight.
- The aeroplane’s centre of gravity was at least 0.122m rear of the maximum permissible limit, which created a tendency for the nose to pitch up. The most likely reason for the crash was the aeroplane being excessively out of balance. In addition, the aeroplane probably became airborne early and at too low an airspeed to prevent uncontrollable nose-up pitch.
- The aeroplane reached a pitch angle that would have made it highly improbable for the unrestrained parachutists to prevent themselves sliding back towards the tail. Any shift in weight rearward would have made the aeroplane more unstable.
- The engineering company that modified ZK-EUF for parachuting operations did not follow proper processes required by civil aviation rules and guidance. Two of the modifications had been approved for a different aircraft type, one modification belonged to another design holder and a fourth was not referred to in the aircraft maintenance logbook.
- The flight manual for ZK-EUF had not been updated to reflect the new role of the aeroplane and was limited in its usefulness to the aeroplane owner for calculating weight and balance.
- Regardless of the procedural issues with the project to modify ZK-EUF, the engineering work conducted on ZK-EUF to convert it from agricultural to parachuting operations in the standard category was by all accounts appropriately carried out.
- The weight and balance of the aeroplane, with its centre of gravity at least 0.122m outside the maximum aft limit, would have caused serious handling issues for the pilot and was the most significant factor contributing to the accident.
- ZK-EUF was 17 kg over its maximum permissible weight on the accident flight, but was still 242 kg lighter than the maximum all-up weight for which the aeroplane was certified in its previous agricultural role. Had the aeroplane not been out of balance it is considered the excess weight in itself would have been unlikely to cause the accident. Nevertheless, the pilots should have made a full weight and balance calculation before each flight.
- The aeroplane owner and their pilots did not comply with civil aviation rules and did not follow good, sound aviation practice by failing to conduct weight and balance calculations on the aeroplane. This resulted in the aeroplane being routinely flown overweight and outside the aft centre of gravity allowable limit whenever it carried 8 parachutists.
- The empty weight and balance for ZK-EUF was properly recorded in the flight manual, but the stability information in that manual had not been appropriately amended to reflect its new role of a parachute aeroplane. Nevertheless, it was still possible for the aeroplane operator to initially have calculated the weight and balance of the aeroplane for the predicted operational loads before entering the aeroplane into service.
- The aeroplane owner did not comply with civil aviation rules and did not follow good, sound aviation practice when they: used the incorrect amount of fuel reserves; removed the flight manual from the aeroplane; and did not formulate their own standard operating procedures before using the aeroplane for commercial parachuting operations.
- The Director of Civil Aviation delegated the task of assessing and overseeing major modifications to Rule Part 146 design organisations and individual holders of “inspection authorisations”. The delegations did not absolve the Director of his responsibility to monitor compliance with civil aviation rules and guidance.
Page 38 | Report 10-009
- The delegations increased the risk that unless properly managed the CAA could lose control of 2 safety-critical functions: design and inspection. The Director had not appropriately managed that risk with the current oversight programme.
- The CAA had adhered strictly to its normal practice and was acting in accordance with civil aviation rules when approving the change in airworthiness category from special to standard. However, knowing the scope, size and complexity of the modifications required to change ZK-EUF from an agricultural to a parachuting aeroplane, it should have had greater participation in the process to help ensure there were no safety implications.
- There was a flaw in the regulatory system that allowed an engineering company undertaking major modification work on an aircraft to have little or no CAA involvement by using an internal or contracted design delegation holder and a person with the inspection authorisation to oversee and sign off the work.
- The level of parachuting activity in New Zealand warranted a stronger level of regulatory oversight than had been applied in recent years.
- The CAA’s oversight and surveillance of commercial parachuting were not adequate to ensure that operators were functioning in a safe manner.
- The CAA had mechanisms through the Director’s powers under the Civil Aviation Act and his designated powers under the HSE Act to effectively regulate the parachuting industry pending the introduction of Rule Part 115.
- An alcohol and drug testing regime needs to be initiated for persons performing activities critical to flight safety, to detect and deter the use of performance-impairing substances.
- In this case the impact was not survivable and the passengers wearing safety restraints would not have prevented their deaths, but in other circumstances the wearing of safety restraints might reduce injuries and save lives.
- Safety harnesses or restraints would help to prevent passengers sliding rearward and altering the centre of gravity of the aircraft. It could not be established if this was a factor in this accident.
Final Report:

Crash of a GAF Nomad N.22 on Franz Josef Glacier: 9 killed

Date & Time: Oct 25, 1993 at 1245 LT
Type of aircraft:
Registration:
ZK-NOM
Flight Phase:
Survivors:
No
Site:
Schedule:
Glentanner - Queenstown
MSN:
004
YOM:
1975
Flight number:
Hibiscus One Mike
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total flying hours:
902
Captain / Total hours on type:
15.00
Copilot / Total flying hours:
2477
Copilot / Total hours on type:
99
Aircraft flight hours:
3850
Circumstances:
The aircraft had been chartered to fly a German group to a number of tourist destinations in New Zealand. It had departed from Glentanner on a VFR flight to Queenstown. The flight was to include scenic flying in the Mount Cook region. A 'taxiing' call was received at 1153 hours but later attempts by Christchurch Flight Information to communicate with the aircraft were unsuccessful. Aircraft wreckage, which proved to be that of ZK-NOM, was sighted during the afternoon in a severely crevassed and pinnacled area of Franz Josef Glacier, at an elevation of 4,500 feet amsl. The crew and passengers had all sustained fatal injuries on impact.
Probable cause:
The probable cause of this accident was the decision to attempt to climb above the lower region of Franz Josef Glacier which had an average slope steeper than the aircraft could outclimb. A causal factor was the crew's lack of training and experience in mountain flying rendering them vulnerable to visual misperception. Probable contributing factors included a cloud layer limiting the position and altitude at which climb could be commenced and an optimistic assessment of the aircraft's capability and progress during the climb.
Final Report:

Crash of a Fletcher FU-24-950 in Hokitika: 1 killed

Date & Time: Oct 28, 1984
Type of aircraft:
Operator:
Registration:
ZK-DJF
Flight Phase:
Survivors:
Yes
Schedule:
Hokitika - Hokitika
MSN:
177
YOM:
1972
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The single engine aircraft departed Hokitika Airport on a local skydiving flight, carrying four skydivers and one pilot. The ripcord of the reserve parachute of one of the jumpers was snagged as he climbed out of the cockpit and the chute streamed and began to deploy. The jumper struck the tailplane as he was dragged aft, damaging it, and the Fletcher went out of control and dived into the ground. The remaining parachutists all escaped the crashing plane by the use of their parachutes but the pilot, who was not wearing a parachute, was killed in the crash. The jumper whose reserve had accidentally deployed suffered a head injury which rendered him unconscious briefly but landed safely.

Crash of a Fletcher FU-24 in Harihari

Date & Time: Oct 18, 1968
Type of aircraft:
Operator:
Registration:
ZK-CLV
Flight Phase:
Survivors:
Yes
MSN:
3
YOM:
1954
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed in unknown circumstances while completing a topdressing mission. c/n TBC

Crash of a De Havilland DH.90A Dragonfly off Westport: 4 killed

Date & Time: Dec 21, 1942 at 1015 LT
Operator:
Registration:
ZK-AGP
Flight Phase:
Survivors:
Yes
Schedule:
Hokitika – Greymouth – Westport – Nelson
MSN:
7566
YOM:
1937
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
Shortly after take off from Westport Airport, while climbing to an altitude of 4,000 feet, the propeller blades detached from the right engine. The pilot increased power on left engine and attempted to return to Westport. Unfortunately, shortly later, the aircraft stalled and crashed into the sea 7 km off shore. All four passengers drowned while the pilot was injured. The propeller blades were found on a beach in March 1943.
Crew:
Arthur C. Baines.
Probable cause:
Examination of the propeller blades showed that the attachment bolts may not have been tightened correctly and had become loose in flight, causing the propeller blades to detach.

Crash of a De Havilland DH.60G Gipsy Moth in Whataroa

Date & Time: Feb 16, 1938
Type of aircraft:
Operator:
Registration:
ZK-AAD
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
927
YOM:
1929
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed on takeoff for unknown reasons. There were no casualties.

Crash of a De Havilland DH.60G III Moth Major in Waiho: 1 killed

Date & Time: Jun 20, 1935
Type of aircraft:
Registration:
ZK-ADO
Flight Type:
Survivors:
Yes
MSN:
5120
YOM:
1935
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The single engine airplane was completing a cargo flight to Waiho, carrying one female passenger, one pilot and a load consisting of newspapers. On final approach, the pilot lost control of the airplane that crashed, bursting into flames. Seriously injured, the pilot was able to evacuate the cabin but could not help the passenger who died in the burned wreckage.
Crew:
Harold Thomas Lawn, pilot.
Passenger:
Esther Jean Newman. †
Probable cause:
It is believed that a bundle of newspapers jammed the control column on approach, causing the airplane to be uncontrollable.

Crash of a De Havilland DH.60G Gipsy Moth in Mt Turiwhate: 2 killed

Date & Time: Nov 20, 1933 at 1430 LT
Type of aircraft:
Operator:
Registration:
ZK-AAI
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Hokitika – Christchurch
MSN:
869
YOM:
1929
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The airplane departed Hokitika in relative good weather conditions. About 30 minutes into the flight, while cruising at a height of some 1,250 metres, the aircraft impacted the slope of Mt Turiwhate located 30 km east of Hokitika. At the time of the accident, the visibility was poor due to rain falls and foggy conditions. The pilot John D. Renton and the passenger James Daniel Lynch were killed.
Probable cause:
Controlled flight into terrain.