Crash of a Partenavia P.68B in Cisterna d'Asti: 5 killed

Date & Time: Aug 22, 1982
Type of aircraft:
Operator:
Registration:
I-IEAB
Flight Phase:
Flight Type:
Survivors:
No
Site:
MSN:
110
YOM:
1977
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
Crashed in unknown circumstances onto a house located in Cisterna d'Asti and burst into flames. All five occupants were killed.

Crash of a Boeing 727-235 in New Orleans: 153 killed

Date & Time: Jul 9, 1982 at 1608 LT
Type of aircraft:
Operator:
Registration:
N4737
Flight Phase:
Survivors:
No
Site:
Schedule:
Miami - New Orleans - Las Vegas - San Francisco - San Diego
MSN:
19457
YOM:
1968
Flight number:
PA759
Crew on board:
7
Crew fatalities:
Pax on board:
138
Pax fatalities:
Other fatalities:
Total fatalities:
153
Captain / Total flying hours:
11727
Captain / Total hours on type:
10595.00
Copilot / Total flying hours:
6127
Copilot / Total hours on type:
3914
Aircraft flight hours:
39253
Aircraft flight cycles:
35643
Circumstances:
Pan Am Flight 759 was a scheduled flight from Miami (MIA) to Las Vegas (LAS), with an en route stop at New Or1eans (MSY). At 15:58:48 Boeing 727 "Clipper Defiance" taxied from its gate at the New Orleans International Airport. Before leaving the gate, the flightcrew had received ATIS message Foxtrot which read in part "....time one eight five five Zulu, weather, two thousand five hundred scattered, two five thousand thin broken, visibility six miles in haze, temperature niner zero, wind two four zero at two, winds are calm altimeter three zero zero one...". The flightcrew requested runway 10 for the takeoff and ground control cleared the flight to taxi to runway 10. At 15:59:03, the first officer requested a wind check. Winds were 040 degrees at 8 knots. At 16:02:34, while Flight 759 was taxiing to runway 10, the crew heard a transmission from ground control, advising another airplane of low level wind shear alerts in the northeast quadrants of the airport. At 16:03:33, the first officer requested another wind check. Ground control replied, "Wind now zero seven zero degrees at one seven... peak gusts two three, and we have low level wind shear alerts all quadrants, appears to be a frontal passing overhead right now, we're right in the middle of everything." The captain then advised the first officer to "...let your airspeed build up on takeoff..." and said that they would turn off the air conditioning packs for the takeoff, which would enable them to increase the EPR's on engines Nos. 1 and 3 to 1.92. The flightcrew completed the takeoff and departure briefings and turned onto the active runway for takeoff. At l6:06:22, Flight 759 informed the tower that it was ready for takeoff. The local controller cleared the flight for takeoff, and the first officer acknowledged the clearance. About 16:07:57, the Boeing 727 began its takeoff. According to witnesses, the airplane lifted off about 7,000 feet down runway 10, climbed in a wings-level attitude, reached an altitude of about 100 feet to 150 feet above the ground (AGL), and then began to descend towards trees. The airplane crashed into a residential area and was destroyed during the impact, explosion, and subsequent ground fire. Eight persons on the ground were killed.
Probable cause:
The airplane's encounter during the lift-off and initial climb phase of flight with a micro-burst induced windshear which imposed a downdraft and a decreasing headwind, the effects of which the pilot would have had difficulty recognizing and reacting to in time for the airplane's descent to be arrested before its impact with trees. Contributing to the accident was the limited capability of current ground based low level windshear detection technology to provide definitive guidance for controllers and pilots for use in avoiding low level wind shear encounters.
Final Report:

Crash of a Beechcraft UC-12B Huron in Pensacola: 1 killed

Date & Time: Jan 2, 1982 at 1325 LT
Type of aircraft:
Operator:
Registration:
161189
Flight Type:
Survivors:
Yes
Site:
Schedule:
Norfolk - Pensacola
MSN:
BJ-5
YOM:
1980
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The crew departed Norfolk-Chambers Field NAS on a flight to Pensacola-Forrest Sherman Field NAS, Florida. While descending to Pensacola, weather conditions worsened and the crew decided to divert to Pensacola-Intl Airport. On approach in limited visibility due to rain falls, the twin engine airplane struck tree tops and crashed in a residential area located north of the airport. A pilot was killed while seven other occupants were injured. The aircraft was destroyed.

Crash of a Mitsubishi MU-2B-35 Marquise in Edmonton: 1 killed

Date & Time: Dec 6, 1981 at 1805 LT
Type of aircraft:
Registration:
C-GLOW
Survivors:
Yes
Site:
Schedule:
Fort McMurray – Edmonton
MSN:
624
YOM:
1974
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
On final approach to Edmonton Airport runway 30, the airplane lost height and crashed on the roof of the Royal Alexandra Hospital. The airplane was destroyed and both occupants were seriously injured. A day later, the pilot died from his injuries.
Probable cause:
It appears that both engines stopped on approach for undetermined reasons.

Crash of a Mitsubishi LR-1 in Utsunomiya: 5 killed

Date & Time: Aug 10, 1981
Type of aircraft:
Operator:
Registration:
22011
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
MSN:
811
YOM:
1980
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
The twin engine airplane was engaged in a training flight, carrying six crew members. En route, the crew informed ATC about an engine failure when control was lost. The airplane entered a dive and crashed onto a house. A crew member was seriously injured while five other occupants were killed. There were no casualties on ground.
Probable cause:
Engine failure for unknown reasons.

Crash of a Cessna 411 in Columbus: 1 killed

Date & Time: Jul 9, 1981 at 2156 LT
Type of aircraft:
Operator:
Registration:
N7007R
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Ozark - Augusta
MSN:
411-0047
YOM:
1965
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
25
Circumstances:
While cruising by night on a flight from Ozark, Alabama, to Augusta, Georgia, the pilot lost control of the airplane that entered a dive and crashed in a residential area, bursting into flames. The pilot, sole on board, was killed. There were no casualties on ground.
Probable cause:
Loss of control after unqualified person operated the aircraft. The following contributing factors were reported:
- Failure of the electrical system,
- The pilot attempted operation beyond experience/ability level,
- The pilot diverted attention from operation of aircraft,
- The pilot failed to follow approved procedures,
- Improper emergency procedures,
- Battery weak,
- Alternators off during GPU start,
- Emergency gear handle extended, observed without light,
- Dark night.
Final Report:

Crash of a Piper PA-31T Cheyenne II in Perth: 1 killed

Date & Time: May 3, 1981 at 1125 LT
Type of aircraft:
Operator:
Registration:
VH-CCW
Flight Type:
Survivors:
No
Site:
Schedule:
Jandakot - Perth
MSN:
31-7720046
YOM:
1977
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4279
Captain / Total hours on type:
576.00
Circumstances:
The aircraft was flown from Jandakot to Perth at approximately 08:00 hours on 3.5.81. However, the engineer who had agreed to meet the pilot sent a message that he could not attend. At times during the morning, persons observed the aircraft parked at the airport. The engine cowls had been removed and the pilot was seen to be working in the area of the propeller governors. At about 11:00 hours, the pilot started the aircraft's engines, taxied to a clear area and carried out a series of checks" at high power. Then, at 11:09 hours, he contacted Perth Surface Movement Control by radio and requested clearance for an air test at Flight Level 200. This was approved and the aircraft was instructed to taxi to Runway 20. After take-off, the aircraft turned right and tracked to the west on the 270 radial of the VHF omni-directional radio range (VOR), in accordance with departure instructions give n by Perth Tower. When asked for his intentions, the pilot advised that he wished to continue tracking to the west until further notice. Weather conditions in the Perth area were fine; there was no cloud and the surface wind was a light southwesterly. The aircraft as it climbed out appeared to be operating normally , except for a thin smoke trail which was observed coming from the right engine. At 11:19 hours, the pilot advised that his test was completed. He reported he was at 7,000 feet and 10 miles from the airport by distance measuring equipment (DME). During the next five minutes there were a series of routine exchanges between VH-CCW and Perth Tower as the aircraft was cleared to track visually, north of Perth city, to a right base position for Runway 20. During these exchanges the pilot did not indicate that any abnormality or emergency existed and his voice sounded normal. At 11:24 hours, he reported at right base and was cleared to land. The final transmission received from the aircraft was the usual acknowledgement of the landing clearance. The right base position for Runway 20 is over the suburb of Bassendean and local residents are used to aircraft overflying. However, attention was drawn to VH-CCW as it was lower than normal traffic, the engine noise was louder and smoke was trailing from its right engine. Otherwise, it appeared to be operating normally; both propellers were rotating and the landing gear was reported to be retracted. The aircraft had commenced an apparently normal right base turn when it suddenly rolled inverted. The nose of the aircraft may have pitched up just before the sudden roll. The aircraft then began to rotate and rapidly descend. At some stage, it rolled back to the normal upright attitude. After about two turns, the rotation stopped and the aircraft dropped vertically to the ground in the backyard of a private house. The left wing and tailplane struck the roof of the house just prior to ground impact. An intense fire immediately broke out and consumed most of the wreckage. Subsequent examination of the wreckage found no evidence of pre-existing defects or malfunctions, apart from loose attachment nuts on the left side of the propeller governor fitted to the right engine. Oil had leaked from the governor at this position, covering the engine and causing the smoke trail observed by witnesses. Internal inspection of the right engine established that all bearing surfaces were oil-wetted, but it could not be determined how much oil remained in the engine at the time of ground impact as any residual oil had leaked and been consumed by fire. Both engines had been operating at impact. The right engine was at a low power setting, probably idle. The left engine was at a higher power, although the exact power setting could not be determined. The left propeller was at a blade angle consistent with higher power output. The right propeller was at a blade angle outside the normal operating range but consistent with the propeller moving towards the feather position, either as a result of pilot selection or exhaustion of the engine oil supply. It was not possible to determine whether or not the pilot had initiated feathering. The stability augmentation system servo was at the maximum, elevator-down spring tension position. The automatic system would drive the servo to this position when the aircraft was flown at low airspeed. The elevator trim was set at 10 degrees nose-up, also consistent with low-speed flight. The rudder trim was at the full-left rudder position, indicating that the pilot had been operating the aircraft for some time with high power on the left engine and the right engine at a low power setting. The flaps were half extended and the landing gear was down at ground impact. Post-mortem examination found that the pilot had extensive coronary artery disease, such that he may have suffered a sudden incapacitating attack or death. Alternatively, he may have experienced severe chest pain, causing him to unintentionally apply coarse movements to the aircraft controls. The pilot had completed regular medical examinations for the renewal of his pilot's licence, but his condition had not been detected.
Probable cause:
The exact cause of the accident could not be determined with certainty. However, the following defect was discovered: two nuts attaching the propeller governor to the right engine were loose, permitting oil to leak from the governor.
Final Report:

Crash of a Cessna 421A Golden Eagle I in Lisbon: 7 killed

Date & Time: Dec 4, 1980 at 2016 LT
Type of aircraft:
Operator:
Registration:
YV-314P
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Lisbon - Porto
MSN:
421A-0040
YOM:
1969
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
1613
Captain / Total hours on type:
42.00
Copilot / Total flying hours:
744
Aircraft flight hours:
1500
Circumstances:
The twin engine airplane, chartered by the Portuguese Government, was engaged in a special flight from Lisbon to Porto, carrying various members of the Portuguese Government. Shortly after takeoff from Lisbon-Portela de Sacavém Airport, while climbing by night, the twin engine airplane lost height and crashed onto several houses located in the district of Camarate. The aircraft was totally destroyed and all seven occupants were killed. There were no casualties on ground.
Occupants:
Mr. Francisco Sa Carneiro, Prime Minister,
Mrs. Francisco Sa Carneiro,
Mr. Amaro da Costa, Minister of Defence,
Mrs. Amaro da Costa,
One Chief of Cabinet and two pilots.
Probable cause:
The loss of control during initial climb was the consequence of the combination of the following factors:
- Poor flight preparation on part of the crew,
- Inadvertent shutdown of the left engine during initial climb for unknown reasons,
- The left propeller was not feathered, causing high drag,
- The flaps were not deployed in the correct position for takeoff,
- The CofG was off limits,
- Negligences of those responsible for planning and safety in the air transport of important figures of State, in an aircraft of foreign registration whose maintenance status was not previously maintained rated,
- Crew fatigue,
- Crew psychic stress accumulation.
Final Report:

Crash of a Lockheed C-130H Hercules in Caracas: 11 killed

Date & Time: Nov 4, 1980
Type of aircraft:
Operator:
Registration:
3556
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Caracas - Caracas
MSN:
4406
YOM:
1971
Country:
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
11
Circumstances:
The crew was engaged in a local training flight at Caracas-Maiquetía-Simón Bolívar Airport. After takeoff, while in initial climb, the airplane lost height and crashed onto several houses located near the airfield. The aircraft and five houses were destroyed. All six occupants as well as five people on the ground were killed.
Probable cause:
Loss of control during initial climb caused by an engine failure for undetermined reasons.

Crash of a Cessna 402B in Salley

Date & Time: Nov 1, 1980 at 0255 LT
Type of aircraft:
Registration:
N8159Q
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
Schedule:
Charleston - Charleston
MSN:
402B-0375
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1540
Captain / Total hours on type:
101.00
Circumstances:
While cruising by night on a regional flight out from Charleston, both engines failed. The pilot reduced his altitude in an attempt to make an emergency landing when the airplane crashed onto a house in Salley. Both occupants were seriously injured while there were no casualties on the ground. The aircraft was destroyed.
Probable cause:
Engine failure during normale cruise due to improper in-flight decisions. The following contributing factors were reported:
- Mismanagement of fuel,
- Fuel exhaustion,
- The pilot attempted operation with known deficiencies in equipment,
- Instruments: fuel quantity gauge erratic,
- Faire of both engines,
- Low ceiling,
- Visibility 1/4 mile or less.
Final Report: