Crash of a Fletcher FU-24A-954 in Wynella Station: 1 killed

Date & Time: Dec 20, 2010 at 1700 LT
Type of aircraft:
Registration:
VH-FNM
Survivors:
No
Schedule:
Wynella Station - Wynella Station
MSN:
263
YOM:
1979
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
5815
Circumstances:
On 20 December 2010, the owner/pilot of a Pacific Aerospace Corporation FU-24-954 Fletcher aircraft, registered VH-FNM, was conducting aerial spreading of urea fertilizer at Wynella Station; a property 40 km south-south-west of Dirranbandi, Queensland. At about 1650 Eastern Standard Time, the pilot was returning to the landing strip after the completion of an application run. The aircraft impacted the terrain, and the pilot was fatally injured.
Probable cause:
Examination of the accident site indicated that the aircraft’s engine was delivering power at the time of impact. Wreckage examination did not reveal evidence of any defect or mechanical failure that would have contributed to the event. Although the post-mortem report on the pilot noted that he had significant coronary atherosclerosis, there was insufficient information available to determine whether pilot incapacitation was involved in the accident. The investigation did not identify any organisational or systemic issues that might adversely affect the future safety of aviation
operations.
Final Report:

Crash of a Gippsland GA8 Airvan in Lady Barron

Date & Time: Oct 15, 2010 at 1715 LT
Type of aircraft:
Operator:
Registration:
VH-DQP
Survivors:
Yes
Site:
Schedule:
Lady Barron - Bridport
MSN:
GA8-05-075
YOM:
2005
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2590
Captain / Total hours on type:
1355.00
Circumstances:
The pilot was conducting a charter flight from Lady Barron, Flinders Island to Bridport, Tasmania with six passengers on board. The aircraft departed Lady Barron Aerodrome at about 1700 Australian Eastern Daylight-saving Time and entered instrument meteorological conditions (IMC) several minutes afterwards while climbing to the intended cruising altitude of about 1,500 ft. The pilot did not hold a command instrument rating and the aircraft was not equipped for flight in IMC. He attempted to turn the aircraft to return to Lady Barron Aerodrome but became lost, steering instead towards high ground in the Strzelecki National Park in the south-east of Flinders Island. At about 1715, the aircraft exited cloud in the Strzelecki National Park, very close to the ground. The pilot turned to the left, entering a small valley in which he could neither turn the aircraft nor out climb the terrain. He elected to slow the aircraft to its stalling speed for a forced landing and, moments later, it impacted the tree tops and then the ground. The first passenger to exit the aircraft used the aircraft fire extinguisher to put out a small fire that had begun beneath the engine. The other passengers and the pilot then exited the aircraft safely. One passenger was slightly injured during the impact; the pilot and other passengers were uninjured. During the night, all of the occupants of the aircraft were rescued by helicopter and taken to the hospital in Whitemark, Flinders Island.
Probable cause:
Contributing safety factors:
• The weather was marginal for flight under the visual flight rules, with broken cloud forecast down to 500 ft above mean sea level in the area.
• The pilot, who did not hold a command instrument rating, entered instrument meteorological conditions because he was adhering to an un-written operator rule not to fly below 1,000 ft above ground level.
• The pilot became lost in cloud and flew the aircraft towards the Mt Strzelecki Range, exiting the cloud in very close proximity to the terrain.
• The aircraft exited the cloud in a small valley, within which the pilot could neither turn round nor out-climb the terrain.
Other key findings:
• The aircraft exited cloud before impacting terrain and with sufficient time for the pilot to execute a forced landing.
• The design of the aircraft’s seats, and the provision to passengers in the GA-8 Airvan of three-point automotive-type restraint harnesses with inertia reel shoulder straps contributed to the passengers’ survival, almost without injury.
Final Report:

Crash of a Fletcher FU-24-954 in Fox Glacier: 9 killed

Date & Time: Sep 4, 2010 at 1327 LT
Type of aircraft:
Registration:
ZK-EUF
Flight Phase:
Survivors:
No
Schedule:
Fox Glacier - Fox Glacier
MSN:
281
YOM:
1981
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total flying hours:
4554
Captain / Total hours on type:
41.00
Circumstances:
Shortly after take off from Fox Glacier aerodrome, while climbing, aircraft stalled and crashed in flames in a paddock near the airfield. All nine occupants, the pilot and 8 skydivers, were killed. The new owner and operator of the aeroplane had not completed any weight and balance calculations on the aeroplane before it entered service, nor at any time before the accident. As a result the aeroplane was being flown outside its loading limits every time it carried a full load of 8 parachutists. On the accident flight the centre of gravity of the aeroplane was well rear of its aft limit and it became airborne at too low a speed to be controllable. The pilot was unable to regain control and the aeroplane continued to pitch up, then rolled left before striking the ground nearly vertically.
Probable cause:
Findings:
- There were no technical defects identified that may have contributed to the accident and the aeroplane was considered controllable during the take-off roll, with the engine able to deliver power during the short flight.
- The aeroplane’s centre of gravity was at least 0.122m rear of the maximum permissible limit, which created a tendency for the nose to pitch up. The most likely reason for the crash was the aeroplane being excessively out of balance. In addition, the aeroplane probably became airborne early and at too low an airspeed to prevent uncontrollable nose-up pitch.
- The aeroplane reached a pitch angle that would have made it highly improbable for the unrestrained parachutists to prevent themselves sliding back towards the tail. Any shift in weight rearward would have made the aeroplane more unstable.
- The engineering company that modified ZK-EUF for parachuting operations did not follow proper processes required by civil aviation rules and guidance. Two of the modifications had been approved for a different aircraft type, one modification belonged to another design holder and a fourth was not referred to in the aircraft maintenance logbook.
- The flight manual for ZK-EUF had not been updated to reflect the new role of the aeroplane and was limited in its usefulness to the aeroplane owner for calculating weight and balance.
- Regardless of the procedural issues with the project to modify ZK-EUF, the engineering work conducted on ZK-EUF to convert it from agricultural to parachuting operations in the standard category was by all accounts appropriately carried out.
- The weight and balance of the aeroplane, with its centre of gravity at least 0.122m outside the maximum aft limit, would have caused serious handling issues for the pilot and was the most significant factor contributing to the accident.
- ZK-EUF was 17 kg over its maximum permissible weight on the accident flight, but was still 242 kg lighter than the maximum all-up weight for which the aeroplane was certified in its previous agricultural role. Had the aeroplane not been out of balance it is considered the excess weight in itself would have been unlikely to cause the accident. Nevertheless, the pilots should have made a full weight and balance calculation before each flight.
- The aeroplane owner and their pilots did not comply with civil aviation rules and did not follow good, sound aviation practice by failing to conduct weight and balance calculations on the aeroplane. This resulted in the aeroplane being routinely flown overweight and outside the aft centre of gravity allowable limit whenever it carried 8 parachutists.
- The empty weight and balance for ZK-EUF was properly recorded in the flight manual, but the stability information in that manual had not been appropriately amended to reflect its new role of a parachute aeroplane. Nevertheless, it was still possible for the aeroplane operator to initially have calculated the weight and balance of the aeroplane for the predicted operational loads before entering the aeroplane into service.
- The aeroplane owner did not comply with civil aviation rules and did not follow good, sound aviation practice when they: used the incorrect amount of fuel reserves; removed the flight manual from the aeroplane; and did not formulate their own standard operating procedures before using the aeroplane for commercial parachuting operations.
- The Director of Civil Aviation delegated the task of assessing and overseeing major modifications to Rule Part 146 design organisations and individual holders of “inspection authorisations”. The delegations did not absolve the Director of his responsibility to monitor compliance with civil aviation rules and guidance.
Page 38 | Report 10-009
- The delegations increased the risk that unless properly managed the CAA could lose control of 2 safety-critical functions: design and inspection. The Director had not appropriately managed that risk with the current oversight programme.
- The CAA had adhered strictly to its normal practice and was acting in accordance with civil aviation rules when approving the change in airworthiness category from special to standard. However, knowing the scope, size and complexity of the modifications required to change ZK-EUF from an agricultural to a parachuting aeroplane, it should have had greater participation in the process to help ensure there were no safety implications.
- There was a flaw in the regulatory system that allowed an engineering company undertaking major modification work on an aircraft to have little or no CAA involvement by using an internal or contracted design delegation holder and a person with the inspection authorisation to oversee and sign off the work.
- The level of parachuting activity in New Zealand warranted a stronger level of regulatory oversight than had been applied in recent years.
- The CAA’s oversight and surveillance of commercial parachuting were not adequate to ensure that operators were functioning in a safe manner.
- The CAA had mechanisms through the Director’s powers under the Civil Aviation Act and his designated powers under the HSE Act to effectively regulate the parachuting industry pending the introduction of Rule Part 115.
- An alcohol and drug testing regime needs to be initiated for persons performing activities critical to flight safety, to detect and deter the use of performance-impairing substances.
- In this case the impact was not survivable and the passengers wearing safety restraints would not have prevented their deaths, but in other circumstances the wearing of safety restraints might reduce injuries and save lives.
- Safety harnesses or restraints would help to prevent passengers sliding rearward and altering the centre of gravity of the aircraft. It could not be established if this was a factor in this accident.
Final Report:

Crash of a Cessna 550 Citation II in Bwagaoia: 4 killed

Date & Time: Aug 31, 2010 at 1615 LT
Type of aircraft:
Registration:
P2-TAA
Survivors:
Yes
Schedule:
Port Moresby – Bwagaoia
MSN:
550-0145
YOM:
1980
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
14591
Copilot / Total flying hours:
872
Aircraft flight hours:
14268
Circumstances:
The aircraft was conducting a charter flight from Jackson’s International Airport, Port Moresby, National Capital District, Papua New Guinea (PNG), to Bwagaoia Aerodrome, Misima Island, Milne Bay Province, PNG (Misima). There were two pilots and three passengers on board for the flight. The approach and landing was undertaken during a heavy rain storm over Bwagaoia Aerodrome at the time, which resulted in standing water on the runway. This water, combined with the aircraft’s speed caused the aircraft to aquaplane. There was also a tailwind, which contributed the aircraft to landing further along the runway than normal. The pilot in command (PIC) initiated a baulked landing procedure. The aircraft was not able to gain flying speed by the end of the runway and did not climb. The aircraft descended into terrain 100 m beyond the end of the runway. The aircraft impacted terrain at the end of runway 26 at 1615:30 PNG local time and the aircraft was destroyed by a post-impact, fuel-fed fire. The copilot was the only survivor. Other persons who came to assist were unable to rescue the remaining occupants because of fire and explosions in the aircraft. The on-site evidence and reports from the surviving copilot indicated that the aircraft was serviceable and producing significant power at the time of impact. Further investigation found that the same aircraft and PIC were involved in a previous landing overrun at Misima Island in February 2009.
Probable cause:
Contributing safety factors:
• The operator’s processes for determining the aircraft’s required landing distance did not appropriately consider all of the relevant performance factors.
• The operator’s processes for learning and implementing change from the previous runway overrun incident were ineffective.
• The flight crew did not use effective crew resource management techniques to manage the approach and landing.
• The crew landed long on a runway that was too short, affected by a tailwind, had a degraded surface and was water contaminated.
• The crew did not carry out a go-around during the approach when the visibility was less than the minimum requirements for a visual approach.
• The baulked landing that was initiated too late to assure a safe takeoff.
Other safety factors:
• The aircraft aquaplaned during the landing roll, limiting its deceleration.
• The runway surface was described as gravel, but had degraded over time.
• The weather station anemometer was giving an incorrect wind indication.
Final Report:

Crash of a Gippsland GA-8 Airvan in Orange

Date & Time: Jul 6, 2010 at 1745 LT
Type of aircraft:
Operator:
Registration:
VH-YBH
Flight Type:
Survivors:
Yes
Schedule:
Parkes - Orange
MSN:
GA8-08-131
YOM:
2008
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The pilot was performing a cargo flight from Parkes to Orange, New South Wales. On final approach, the single engine aircraft was too low and impacted the roof of a metal hangar located near the runway threshold. The aircraft stalled and struck the runway surface. Upon impact, the nose gear was torn off. Out of control, the aircraft veered off runway and eventually collided with a metal hangar under construction. While the pilot was injured, the aircraft was destroyed.

Crash of a Piper PA-31 Cheyenne in Bankstown: 2 killed

Date & Time: Jun 15, 2010 at 0805 LT
Type of aircraft:
Operator:
Registration:
VH-PGW
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Bankstown - Brisbane - Albury
MSN:
31-8414036
YOM:
1984
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
2435
Captain / Total hours on type:
779.00
Aircraft flight hours:
6266
Circumstances:
The twin engine aircraft, with a pilot and a flight nurse on board, was being operated by Skymaster Air Services under the instrument flight rules (IFR) on a flight from Bankstown Airport, New South Wales (NSW) to Archerfield Airport, Queensland. The aircraft was being positioned to Archerfield for a medical patient transfer flight from Archerfield to Albury, NSW. The aircraft departed Bankstown at 0740 Eastern Standard Time. At 0752, the pilot reported to air traffic control (ATC) that he was turning the aircraft around as he was having ‘a few problems. At about 0806, the aircraft collided with a powerline support pole located on the eastern side of the intersection of Sackville Street and Canley Vale Road, Canley Vale, NSW. The pilot and flight nurse sustained fatal injuries and the aircraft was destroyed by impact damage and a post-impact fire.
Probable cause:
Contributing safety factors:
• While the aircraft was climbing to 9,000 feet the right engine sustained a power problem and the pilot subsequently shut down that engine.
• Following the shutdown of the right engine, the aircraft's descent profile was not optimized for one engine inoperative flight.
• The pilot conducted a descent towards Bankstown Airport that was consistent with a normal arrival profile without first verifying that the aircraft was capable of achieving adequate performance with one engine inoperative.
• Following the engine problem, the aircraft's flightpath and the pilot’s communication with air traffic control indicated that the pilot's situation awareness was less than optimal.
• The aircraft collided with a powerline support pole on the eastern side of the intersection of Sackville Street and Canley Vale Road, Canley Vale, about 6 km north-west of Bankstown Airport.
Other safety factors:
• The pilot did not broadcast a PAN following the engine shutdown and did not provide air traffic control with further information about the nature of the problem in order for the controller to positively establish the severity of the situation.
• Section 4 of Civil Aviation Advisory Publication (CAAP) 5.23-2(0), Multi-engine Aeroplane Operations and Training of July 2007 did not contain sufficient guidance material to support the flight standard in Appendix A subsection 1.2 of the CAAP relating to Engine Failure in the Cruise. [Minor safety issue]
Other key finding:
• Given the pilot’s extensive experience and testing in the PA-31 aircraft type, and subsequent endorsement training on a high performance turboprop multi-engine aircraft since the issue by CASA in 2008 of a safety alert in respect of the pilot’s PA-31 endorsement, it was unlikely that any deficiencies in that endorsement training contributed to the accident.
Final Report:

Crash of a Fletcher FU24-950 Fletcher in Waipukurau

Date & Time: Apr 20, 2010 at 1420 LT
Type of aircraft:
Operator:
Registration:
ZK-EGT
Flight Phase:
Survivors:
Yes
Schedule:
Waipukurau - Waipukurau
MSN:
242
YOM:
1977
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The pilot was engaged in a crop spraying mission on a plantation close to a farm located in Waipukurau. The accident occurred on takeoff in unknown circumstances. While the pilot was seriously injured, the aircraft was damaged beyond repair.

Crash of an Embraer EMB-120ER Brasília in Darwin: 2 killed

Date & Time: Mar 22, 2010 at 1009 LT
Type of aircraft:
Operator:
Registration:
VH-ANB
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Darwin - Darwin
MSN:
120-116
YOM:
1988
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
8217
Captain / Total hours on type:
3749.00
Copilot / Total flying hours:
5664
Copilot / Total hours on type:
3085
Aircraft flight hours:
32799
Aircraft flight cycles:
33700
Circumstances:
Aircraft crashed moments after takeoff from runway 29 at Darwin Airport, Northern Territory, fatally injuring both pilots. The flight was for the purpose of revalidating the command instrument rating of the pilot under check and was under the command of a training and checking captain, who occupied the copilot’s seat. The takeoff included a simulated engine failure. Data from the aircraft’s flight recorders was used to establish the circumstances leading to the accident and showed that the pilot in command (PIC) retarded the left power lever to flight idle to simulate an engine failure. That introduced a simulated failure of the left engine and propeller autofeathering system. The increased drag from the ‘windmilling’ propeller increased the control forces required to maintain the aircraft’s flightpath. The pilot under check allowed the speed to decrease and the aircraft to bank toward the inoperative engine. Additionally, he increased power on the right engine, and engaged the yaw damper in an attempt to stabilize the aircraft’s flight. Those actions increased his workload and made control of the aircraft more difficult. The PIC did not restore power to the left engine to discontinue the manoeuvre. The few seconds available before the aircraft became uncontrollable were insufficient to allow ‘trouble shooting’ and deliberation before resolving the situation.
Probable cause:
• The pilot in command initiated a simulated left engine failure just after becoming airborne and at a speed that did not allow adequate margin for error.
• The pilot in command simulated a failure of the left engine by selecting flight idle instead of zero thrust, thereby simulating a simultaneous failure of the left engine and its propeller autofeather system, instead of a failure of the engine alone.
• The pilot under check operated the aircraft at a speed and attitude (bank angle) that when uncorrected, resulted in a loss of control.
• The pilot under check increased his workload by increasing torque on the right engine and selecting the yaw damper.
• The pilot in command probably became preoccupied and did not abandon the simulated engine failure after the heading and speed tolerance for the manoeuvre were exceeded and before control of the aircraft was lost.
Final Report:

Crash of a Cessna 208B Grand Caravan in Beagle Bay

Date & Time: Jan 14, 2010 at 0645 LT
Type of aircraft:
Operator:
Registration:
VH-NTQ
Flight Type:
Survivors:
Yes
Schedule:
Broome - Koolan Island
MSN:
208B-0635
YOM:
1997
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft departed Broome on a charter flight to Koolan Island, WA. At about 0645 Western Standard Time1, when the aircraft was at an altitude of about 9,500 feet, the pilot noticed a drop in the engine torque indication with a corresponding drop in the engine oil pressure indication. The pilot increased the power lever setting but the engine torque and oil indications continued to reduce, all other engine indications were normal. During an interview with the Australian Transport Safety Bureau (ATSB) the pilot stated that he felt a power loss associated with the drop in indicated engine torque. The pilot diverted to the nearest airstrip, which was Beagle Bay, WA. He stated that the low oil pressure warning light illuminated so he shut the engine down and prepared for an emergency landing. The pilot reported that on the final approach to the airstrip he realized that the aircraft was too high and its airspeed was too fast. The aircraft touched down about mid way along the runway and overran the end of the runway by about 200 metres. The aircraft impacted a mound of dirt, coming to rest upside down. The pilot, who was the only occupant sustained minor injuries. Examination of the aircraft by a third party and inspection of the photographs taken of the accident site, revealed that the engine, left main gear and nose gear had separated from the airframe during the accident sequence. There was a significant amount of oil present on the underside of the aircraft, indicating that the oil had leaked from the engine during operation. The
engine was removed from the accident site as an assembly by a third party. The propeller was removed and the engine was shipped to an engine overhaul facility where a disassembly and
examination was conducted under the supervision of the ATSB.
Probable cause:
From the evidence available it was evident that the engine had a substantial in-flight oil leak, which necessitated the in-flight shut down of the engine and a diversion to the nearest available airstrip. The accident damage to the engine in the area of the apparent oil leak precluded a conclusive finding as to the source of the leak. Although the detailed examination of the oil tube attachment lug fracture surfaces was inconclusive, the oil tube remained the most likely source of the oil leak. Evidence from other oil tube failures indicated that significant vibratory loading can cause the oil tube attachment lugs to fracture in the manner observed in the oil tube fitted to VH-NTQ. There was no evidence that the transfer tube was subjected to vibration from a compressor turbine or power turbine blade failure or of an incorrectly fitted engine mount. There was also no evidence of a pre-accident defect that would have caused a reduction in actual engine torque.
Final Report:

Crash of a De Havilland DHC-3T Turbo Otter off Vomo Island

Date & Time: Dec 29, 2009 at 1800 LT
Type of aircraft:
Operator:
Registration:
DQ-GLL
Survivors:
Yes
Schedule:
Nadi - Vomo Island
MSN:
288
YOM:
1958
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
While approaching Vomo Island, near Viti Levu Island, Fiji, the single engine aircraft crashed into the sea few dozen metres offshore. All six occupants were slightly injured while the aircraft was damaged beyond repair.