Crash of an Embraer EMB-110P1 Bandeirante in Little Grand Rapids: 4 killed

Date & Time: Dec 9, 1997 at 1526 LT
Operator:
Registration:
C-GVRO
Survivors:
Yes
Schedule:
Winnipeg - Little Grand Rapids
MSN:
110-285
YOM:
1980
Flight number:
4K301
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
15
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
15000
Captain / Total hours on type:
114.00
Copilot / Total flying hours:
700
Copilot / Total hours on type:
367
Aircraft flight hours:
13724
Circumstances:
The Sowind Air Ltd. Embraer EMB-110P1 Bandeirante aircraft departed the operator's base at St. Andrews, Manitoba, with a crew of 2 and 15 passengers, on a 40-minute, scheduled flight to Little Grand Rapids, Manitoba. The aircraft arrived at Little Grand Rapids, and the crew flew an instrument approach to the airport and executed a missed approach because the required visual reference was not established. A second instrument approach was attempted. Ground-based witnesses observed the aircraft very low over the lake to the south of the airport and to the east of the normal approach path. Passengers in the aircraft also reported being very low over the lake and to the east of the normal approach path. The passengers described an increase in engine power followed by a rapid series of steep banking manoeuvres after the aircraft crossed the shoreline to the southeast of the airport. During the manoeuvres, the aircraft descended into the trees and crashed approximately 400 feet south and 1 600 feet east of the approach to runway 36 at Little Grand Rapids. The captain and three passengers were fatally injured, and the first officer and the remaining 12 passengers were seriously injured.
Probable cause:
Findings as to Causes and Contributing Factors:
1. At the time of the occurrence, the base of the cloud at Little Grand Rapids was between 100 and 300 feet agl, with fog to the east of the airport, and the visibility was one to two miles.
2. The aircraft was flown in marginal weather at low level, below the minimum en route altitude for commuter operations and below the MDA for the NDB A approach at Little Grand Rapids. The MDA for the approach was 1 560 feet asl, 555 feet above the airport elevation.
3. While the aircraft was being manoeuvred at very low level in marginal weather, it descended after an abrupt turn, and flew, in controlled flight, into the terrain.
Other Findings:
1. At both take-off and landing, the aircraft was about 1 000 pounds heavier than the relevant maximum allowable weight.
2. The GPS installed in C-GVRO was not approved as a primary navigational aid. The available information indicates that the flight crew used the GPS as a primary navigational aid during the last approach to Little Grand Rapids.
3. The aircraft was not equipped with a GPWS, nor was it required to be by regulation.
4. The weight and balance report that was submitted to Transport Canada, required for the importation of C-GVRO, contained numerous discrepancies; the report was not reviewed for accuracy by Transport Canada.
5. The emergency locator transmitter (ELT) produced a very weak signal because the antenna cable had been installed with little slack, and it pulled out of the antenna fitting during impact.
6. It could not be determined whether the presence of carbon monoxide and diphenhydramine in the captain's body affected his decision making and level of alertness.
7. The company, which had been an air taxi operator, did not effectively manage either the addition of the more complex commuter operations or the introduction of the larger Bandeirante aircraft.
8. The difficulty that the company had in the transition to commuter operations and in the introduction of the Bandeirante aircraft was underestimated by Transport Canada.
9. There were inadequacies in TC=s oversight, whereby the post-certification audit of the company was not conducted, thus eliminating an important mechanism by which TC could have found, and addressed, the inadequate safety management practices, non-conformance with pilot training requirements, and related operating irregularities.
10. The pilots had passed their flying proficiency and medical tests, but they had not completed elements of pilot training requirements with respect to servicing and operational control and right seat conversion as prescribed by TC. Also, no company pilot had received required training in the use of onboard survival or emergency equipment.
11. There was no indication found of any pre-impact failure or malfunction of the airframe, flight controls, or engines.
12. The aircraft was not equipped with either a CVR or an FDR; TC had given the company an exemption to operate without a CVR until 01 August 1998, and the aircraft was not required to be equipped with an FDR.
13. The absence of recorders on this aircraft, which was configured to carry 20 people, left many of the otherwise ascertainable facts associated with the accident unknown and reduced the opportunity of uncovering risks to safety associated with the flight.
14. Conditions were conducive to the pilot experiencing a false sensation that the aircraft was climbing (somatogravic illusion) after increasing the engine power, and he may have been manoeuvring to avoid an abandoned fire tower.
Final Report:

Crash of a Fokker F27 Friendship 500F in Saint Pierre

Date & Time: Dec 7, 1997 at 1818 LT
Type of aircraft:
Operator:
Registration:
G-BNCY
Survivors:
Yes
Schedule:
Southampton - Saint Pierre
MSN:
10558
YOM:
1977
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
50
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
14000
Captain / Total hours on type:
2865.00
Copilot / Total flying hours:
2150
Copilot / Total hours on type:
320
Aircraft flight hours:
44877
Aircraft flight cycles:
53639
Circumstances:
During his pre-flight preparation the commander noted that the crosswind at Guernsey would need close monitoring throughout the day as it would be close to the aircraft's crosswind limits. The aircraft departed from Guernsey at 16:10 for the first sector to Southampton, with the first officer acting as pilot flying (PF). On departure the first officer stated that the aircraft was 'difficult to keep straight' on the runway and moderate turbulence were encountered after takeoff between 500 to 1,000 feet agl but the remainder of the flight was uneventful. The aircraft departed again from Southampton at 17:23, with 50 passengers and 2 kg of freight on board, with the commander as the PF and the first officer as the pilot not flying (PNF). During the cruise the first officer obtained the latest weather for Guernsey: surface wind as 170°/19 gusting to 32 kt, visibility 5 km in rain, cloud scattered at 600 feet, broken at 800 feet, temperature 11°C, dew point 9°C, QNH of 1004 mb with turbulence and windshear below 200 feet agl. The commander briefed the first officer that he intended to carryout a 'radar vectored' ILS approach to runway 27 using 26.5° of flap, instead of the usual 40°, for greater aileron control in the crosswind conditions during the landing. He also intended to add 10 kt to the target threshold speed (TTS). In the final stages of the approach the aircraft experienced a drift angle of 25° to 30° in turbulent conditions. The aircraft was slightly above the prescribed glide path, as it crossed the threshold and the commander stated that when over the runway it was obvious to him that the aircraft would touchdown beyond the normal landing area. He therefore decided to initiate a go-around. Full power was applied and, when established with a positive rate of climb, the landing gear was selected up and the flaps retracted to 16°. The aircraft climbed to 1,500 feet, the flaps were retracted and the crew were given radar vectors for a second ILS approach to runway 27. The commander described the second approach as being more stable and on the correct 3° glide path throughout. The drift angle this time was between 30° and 40° from the inbound track. The crew had correctly calculated the TTS as 96 kt with 40° of flap and 106 kt when using 26.5° of flap. The 40° flap TTS of 96 kt was displayed on the landing data card on the flight deck. The aircraft was cleared to land by ATC approximately three minutes before the actual touchdown. The surface wind was passed as '180°/18 kt with the runway surface wet'. Nineteen seconds before touchdown ATC transmitted the surface wind as '190°/20 kt". The first officer stated that the indicated airspeed (IAS) had been 120 kt 'down the slope' and 110 kt as the aircraft crossed the threshold. The commander stated that the aircraft crossed the threshold, with 26.5° of flap selected, at the correct height with the projected touchdown point in the normal position. Both pilots stated that during the flare, at a height estimated by the commander to be between 10 to 15 feet above the runway, the aircraft appeared to float. The commander reduced the engine torques to zero. The aircraft then continued to descend and touched down, according to the commander, 'a little beyond the normal point, left main wheel first followed by the right and then the nose wheel'. Several fireman however, who were on standby in their vehicles at the airport fire station, saw the aircraft touch down. They described the touchdown point as being opposite the runway fire access road, i.e. with 750 meters to 900 meters of runway remaining. After touchdown the commander selected ground fine pitch on both engines but neither the first officer, the No 1 cabin attendant, who was seated at the rear of the aircraft, nor several of the passengers were aware of the normal aerodynamic braking noise from the propellers. The first officer selected the flaps up and, with the commander having called 'your stick', applied full left (into wind) aileron. It is normal for the PNF to then call '5 lights (indicating that both propellers were in ground fine pitch), TGTs (turbine gas temperatures) stable and flaps traveling'. The first officer can recall seeing five lights but stated that he did not make the normal call. The commander applied full right rudder and braking; applying maximum braking on the right side to keep the aircraft straight. The first officer described the commander as 'standing up in his seat' whilst applying full right rudder. As the aircraft traveled down the runway it felt to the crew as if it was 'skidding or floating with ineffective brakes'. The first officer did not assist with the braking. Sixteen seconds into the ground roll the aircraft started to turn uncontrollably to the left. Realizing that the aircraft would leave the paved surface the commander instructed the first officer to transmit a 'Mayday' message. The aircraft overran the end of the runway and entered the grass to the left of the extended center-line at a speed estimated by the crew to be 60 kt. It then impacted and crossed a narrow earth bank before stopping in an adjacent field.
Probable cause:
The following causal factors were identified:
- The commander decided to continue with the landing knowing that touchdown was beyond the normal point,
- The commander was not aware at touchdown that the crosswind component of the surface wind affecting the aircraft exceeded the Flight Manual limit,
- The commander could not apply maximum braking to both main landing gear brakes at the same time as maintaining directional control through differential braking and full rudder application.
Final Report:

Crash of a Beechcraft A100 King Air in Sioux Lookout

Date & Time: Dec 7, 1997 at 1505 LT
Type of aircraft:
Operator:
Registration:
C-GILM
Flight Type:
Survivors:
Yes
Schedule:
Winnipeg – Sioux Lookout
MSN:
B-124
YOM:
1972
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
A Voyageur Airways Beechcraft A100 aircraft, C-GILM, was on a flight from Winnipeg International Airport Winnipeg International Airport, MB (YWG) to Sioux Lookout Airport, ON (YXL). The crew of two pilots and two paramedics had completed a medevac flight and were returning to Sioux Lookout without a patient on board. The weather was reported to be: wind 060 degrees at two knots, visibility three statute miles in freezing drizzle, and ceiling overcast at 400 feet AGL. The First Officer was at the controls as they attempted two full NDB approaches for runway 34, each of which resulted in a missed approach. The captain then took control of the aircraft and conducted a full NDB approach for runway 34. On final approach, the crew had the runway in sight and the aircraft was lined up, but the aircraft was high on the approach. The captain called for full flap and pushed the props up to help slow the aircraft down. The aircraft developed a high rate of descent that was not fully countered before the aircraft contacted the runway firmly with the left main landing gear. The aircraft was taxied part way to the company ramp before the aircraft began pulling to the left very noticeably. The scissors had failed and the main wheels were turned slightly off-line. While conducting a heavy-landing inspection, company maintenance and operational personnel determined that in addition to the damage to the scissors for the left main landing gear, the rear spar of the left wing had failed in the vicinity of a pass-through hole for the flap actuator. The damage is reported to be overload in nature and consistent with the effects of landing hard on the left main wheel. During the approaches, the aircraft was above cloud during the penetration turns and was only in cloud during the final approach phases. A small amount of ice accumulated on the aircraft while in cloud (about 1/8th to 1/4 inch on the spinner remained after landing) but the de-ice equipment was working and was used.

Crash of a Beechcraft 99 Airliner in Webequie

Date & Time: Dec 4, 1997 at 0200 LT
Type of aircraft:
Operator:
Registration:
C-GXBE
Survivors:
Yes
Schedule:
Fort Hope - Webequie
MSN:
U-160
YOM:
1974
Flight number:
BLS310
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Bearskin Flight 310, a Beech 99, was inbound to Webequie Airport (YWP) on a scheduled passenger flight from Fort Hope Airport (YFH). The flight crew completed an approach to Webequie based on visual cues, GPS and ADF. The flight crew lowered the landing gear about three miles from the runway and set full flap on final approach. The captain reportedly initiated the flare at about 50 feet and the nose of the aircraft came up, but the descent was not arrested before the aircraft struck the runway. The aircraft's wings and tail reportedly had a small amount of residual ice at landing. Winds on the surface were northwest at five to ten knots but the winds aloft were reported to be easterly at up to 50 knots. Examination of the aircraft at the terminal building led the crew to call company maintenance for an inspection. Inspection of the aircraft revealed that the left wing spar was broken, the left wing skin was wrinkled and the left engine was drooping. There were no injuries reported.

Crash of a Cessna 402B in Spencer

Date & Time: Nov 29, 1997 at 0900 LT
Type of aircraft:
Operator:
Registration:
N22NC
Flight Type:
Survivors:
Yes
Schedule:
Cedar Rapids - Spencer
MSN:
402B-0227
YOM:
1972
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1712
Captain / Total hours on type:
197.00
Aircraft flight hours:
7998
Circumstances:
The pilot made four missed ILS approaches at the airport. He stated that he did not see the approach lights during any of the approaches and did not feel comfortable making a landing. The reported visibility during these approaches was 1/2-statute mile. On the fifth approach the pilot said he had '...mistaken closely inline cars and a road for the MALSR and runway.' He pilot stated the airplane continued to descend after initiating a go-around. He said he saw oncoming traffic in front of him, and turned the airplane to the right. He said he lost altitude and the right wing struck the ground. The pilot's employers operations specification require a 1/4- mile increase in visibility for an ILS approach that does not have an operating approach lighting system. The approach lights were checked by the airport manager and were confirmed to be in working order. An on-scene investigation revealed no pre-accident airframe or engine anomalies that would have prevented normal flight.
Probable cause:
The pilot failure to comply with the prescribed IFR procedure and his not following his company's operations specifications. Low clouds and fog were are contributing factors.
Final Report:

Crash of a Britten-Norman BN-2A-26 Islander in Sangafa-Siwo

Date & Time: Nov 27, 1997
Type of aircraft:
Operator:
Registration:
YJ-RV2
Survivors:
Yes
MSN:
172B
YOM:
1970
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The twin engine aircraft landed hard, went out of control, veered off runway and crashed in the sea. All three occupants were seriously injured and the aircraft was damaged beyond repair.

Crash of a Short 360-100 in Billings

Date & Time: Nov 25, 1997 at 0813 LT
Type of aircraft:
Operator:
Registration:
N691A
Flight Type:
Survivors:
Yes
Schedule:
Great Falls - Billings
MSN:
3618
YOM:
1983
Flight number:
CPT814
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8850
Captain / Total hours on type:
2800.00
Copilot / Total hours on type:
103
Aircraft flight hours:
18213
Circumstances:
The Short Brothers SD3-60 cargo flight was being vectored for the VOR/DME RWY 28R approach to the Billings Logan International airport during instrument meteorological conditions. Weather conditions one minute before the accident were winds 020 at 13 knots, light snow and mist, and visibility was deteriorating rapidly. The co-pilot (occupying the right seat) was flying the aircraft, and the PIC (occupying the left seat) was handling radio communications. At 0812:25, having crossed the final approach fix, the aircraft descended through 100 feet above the MDA (3,940 feet or 426 feet above the runway threshold), and immediately thereafter the crew visually acquired the runway. At 0813:01 the aircraft's GPWS alert of 'SINK RATE' was heard, followed 2 seconds later by the PIC calling for 'POWER,' and a 2 second delay to ground impact. The co-pilot had logged a total of 103 hours in the SD3-60 (all within the previous 90 days,) while the PIC had just begun flying the aircraft in Montana's late fall weather after a 6 year assignment flying in the Hawaiian islands. The left main landing gear collapsed in overload during the ground impact.
Probable cause:
The co-pilot's failure to maintain the proper descent rate on final approach, the pilot-in-command's delayed remedial action, and overload of the left main landing gear assembly. Factors contributing were snow, crosswind conditions and deteriorating visibility.
Final Report:

Crash of a GAF Nomad N.24 in La Ceiba

Date & Time: Nov 24, 1997
Type of aircraft:
Operator:
Registration:
HR-AQY
Survivors:
Yes
Schedule:
La Ceiba – Roatán
MSN:
38
YOM:
1977
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
10
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Few minutes after takeoff from La Ceiba-Goloson Airport, while climbing, the aircraft collided with a bird that struck the right engine. The crew decided to return to La Ceiba for an emergency landing when the right engine caught fire and detached. On final, the aircraft went out of control and crashed on a soccer field. All 12 occupants were injured and the aircraft was damaged beyond repair.
Probable cause:
Failure of the right engine that detached in flight following a bird strike. It is believed that the bird was probably a buzzard or a vulture.

Crash of a GAF Nomad N.24 in La Ceiba

Date & Time: Nov 19, 1997
Type of aircraft:
Operator:
Registration:
N244E
Survivors:
Yes
MSN:
119
YOM:
1981
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
During the takeoff roll at La Ceiba-Goloson Airport, the twin engine aircraft struck a rut in the ground. The crew heard a loud bang when the rotation was completed shortly later. During initial climb, the crew informed ATC about the situation and was cleared to return for an emergency landing. On touchdown, the nose gear collapsed and the aircraft slid on its nose for few dozen metres before coming to rest. All 11 occupants escaped uninjured while the aircraft was damaged beyond repair.

Crash of a Douglas DC-8-54F in Mwanza

Date & Time: Nov 18, 1997 at 2109 LT
Type of aircraft:
Registration:
EL-WVD
Flight Type:
Survivors:
Yes
Schedule:
Entebbe - Mwanza
MSN:
45885
YOM:
1968
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10000
Captain / Total hours on type:
30.00
Circumstances:
The aircraft was f1ying from Entebbe (Uganda) to Mwanza (Tanzania) for the purpose of uplifting some cargo of fish fillet which was bound for Ostend, Belgium. It was carrying a crew of four including two pilot s and two engineers. The Commander said that the flight from Entebbe to Mwanza was normal except for the n°1 generator warning light which came on 10 minutes after takeoff from Entebbe. The relevant generator was subsequently switched off and the flight was continued. The aircraft flew IFR, cruising at FL250. Shortly before landing at Mwanza the commander obtained the weather information from the Mwanza Tower. The wind was calm. The controller who was handling the flight said that whilst approaching runway 12 of Mwanza airport the aircraft was swaying from side to side. When EL-WVD touched down on the runway a loud bang was heard and one engine was observed to separate and roll down the runway whilst it was on fire. Examination of the impact and tire marks showed that the right wing tip impacted the runway first followed by the n°4 engine. The right main landing gear subsequently contacted the grass surface off the left edge of the runway followed by the left main landing gear. The aircraft continued to roll in a direction almost parallel to the runway centreline for 250 metres before it crossed the runway at an angle. It was also evident from the tyre marks that as it reached the runway the aircraft made a 180° turn to point in the opposite direction whilst sliding sideways at an angle with the centreline under its own momentum. As it did so, the main landing gear collapsed and three wing pylons sheared causing the engines to separate. EL-WVD finally settled at the edge of the runway pointing 310° with the right wing projecting 2.5 metres inside the runway. There was fuel leakage but no fire. The four crew members disembarked with minor injuries.
Final Report: