Crash of a Cessna 560 Citation V Ultra in Fairoaks

Date & Time: Sep 26, 1998 at 0703 LT
Registration:
VP-CKM
Survivors:
Yes
Schedule:
Sheffield - Fairoaks
MSN:
560-0413
YOM:
1997
Location:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
14500
Captain / Total hours on type:
400.00
Circumstances:
The crew left Sheffield in VP-CKM at 0622 hrs for their flight planned destination of Fairoaks with London Heathrow Airport as an alternate. By 0650 hrs they were in contact with the Aerodrome Flight Information Service Officer (AFISO) at Fairoaks but the AFISO advised the crew not to land until the normal operating time at 0700 hrs when the airfield would have fire cover available. The current weather was reported to the crew by the AFISO as follows: Sky clear; mist with a visibility of 1,200 metres; surface wind 060° less than 5 kt; QNH 1002 mb and QFE 1005 mb. The commander, who was the handling pilot, approached the airfield on a track of 060° using the Fairoaks Non-directional Radio Beacon (NDB) and the aircraft's Flight Management System (FMS), and descended to 1,000 feet agl with the intention of landing on Runway 06. However, neither pilot saw the airfield until they were overhead and, in agreement with the AFISO, decided to make an approach to Runway 24 because of better visibility in that direction. The AFISO switched on the Abbreviated Precision Approach Path Indicators (APAPIs) for Runway 24 and the commander flew a tear drop pattern to the east of the airfield and then established the aircraft on a track of 240° towards the airfield. During the pattern, the gear had been selected down and the flaps set to an intermediate position. At 1.8 nm DME range, the co-pilot saw the APAPIs slightly left of the aircraft nose and pointed them out to the commander; at the time, the co-pilot recalled that the APAPIs were showing 'two whites', the aircraft was at 1,000 feet agl and at 124 kt IAS. By now, the crew had been advised to land at their discretion with the wind calm. Subsequently, full flap was selected and the commander noted his speed on short finals as 104 kt. As VP-CKM approached the threshold, the commander called for the deployment of speedbrakes; as the co-pilot deployed the speedbrakes, he noted the DME range as 0.5 nm and that the FMS indicated a tailwind of 5 kt. The commander considered that touchdown was positive and just beyond the threshold; the co-pilot considered that touchdown was just past the APAPIs. Immediately after touchdown, the commander selected full thrust reverse on both engines and applied moderate wheel braking. Initially, he considered that the retardation seemed adequate but then seemed to reduce. The co-pilot was not aware of retardation and remembered applying maximum brake pedal pressure while noticing that the runway was damp and seemed "shiny". When he realised that he could not stop the aircraft before the end of the runway, the commander stowed the thrust reversers and attempted to close down the engines. During the later part of the landing run, the co-pilot heard a call of "going round" and saw the commander stow the thrust reversers. After leaving the runway, the aircraft travelled for 250 metres before coming to rest. The passenger evacuated through the cabin escape hatch and the co-pilot followed him after an unsuccessful attempt to open the normal cabin door. The co-pilot was then able to open the cabin door from the outside and assist the commander to leave. The commander had sustained back injuries and the copilot had received some cuts and bruises.
Probable cause:
Investigation indicated that there was no technical reason for the aircraft to overrun the runway. One factor outside the crew's control was that the APAPIs were not set at the glideslope angle described in the Jeppesen approach charts. However, the error was one quarter of one degree and should not have affected the touchdown point of the aircraft. Additionally, the crew stated that the APAPIs showed 'two whites' when first acquired and made no mention of them during the approach; it seems likely that the commander was flying his approach to land close to the threshold. Prior to departure, the commander checked the landing distance required for the expected weight of VP-CKM at Fairoaks and calculated that he had 30 to 40 metres longer than required based on zero surface wind. This calculation was subsequently confirmed as reasonable for a landing on Runway 24. However, the initial approach into Fairoaks was for Runway 06 which has a landing distance some 53 metres less than Runway 24. Therefore, the landing distance available on Runway 06 was less than that required by the Flight Manual by at least 13 metres. The commander was unable to land on Runway 06 because of the into sun visibility and so landed on Runway 24. For the approach to Runway 06, the surface wind was reported as 060° less than 5 kt and, for the subsequent approach to Runway 24 the surface wind was reported as calm. The landing distance available on Runway 24 was more than that required by the Flight Manual on a dry runway with no wind. However, the reported surface winds indicated a possibility that the aircraft could experience some tail wind component during the landing and the co-pilot also noted that the FMS displayed a tailwind of 5 kt as he deployed the speedbrakes. The presence of mist could indicate a runway surface other than dry and the co-pilot also noted that the runway was damp and seemed "shiny". Against these factors, the commander would have considered the added advantage of using thrust reversers. Nevertheless, since the commander was not applying any recommended safety factors, it would have been prudent for him to ensure that his approach and touchdown were accurate. He considered that his speed was close to that required as he approached the threshold and that the landing was just beyond the threshold. However, the co-pilot considered that the touchdown was just past the APAPIs positioned 142 metres from the threshold. Outside observers noted the touchdown as between 1/3 and 1/2 way down the runway and this view was corroborated by calculations from the CVR and radar information. The speed on touchdown, as assessed from the recorded information, was close to that required. From touchdown to leaving the paved runway surface, took a period of 11.5 seconds. Thrust reverse was used for three seconds and deselected some 6 seconds before the aircraft left the runway. As thrust reverse was deselected, the commander called "we're going round". This would indicate that the commander became concerned during his landing roll that he would not be able to stop in the distance available and deselected thrust reverse in preparation for a Go-Around. However, the Flight Manual warns that a Go-Around should not be attempted once thrust reverse has been selected. Since there was no evidence from the CVR that power was subsequently advanced, it seems likely that the commander immediately decided against this option. However, the action of deselecting thrust reverse reduced the aircraft rate of deceleration as the runway end approached and resulted in a longer overrun. The commander subsequently stated that he cancelled reverse thrust to enable him to shut down the engines and reduce the risk of fire in what was, by then, obviously going to be an overrun.
Final Report:

Crash of a BAe 146-100 in Cap de Trois Fourhces: 38 killed

Date & Time: Sep 25, 1998 at 0750 LT
Type of aircraft:
Operator:
Registration:
EC-GEO
Survivors:
No
Site:
Schedule:
Málaga – Melilla
MSN:
E1007
YOM:
1983
Flight number:
PV4101
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
34
Pax fatalities:
Other fatalities:
Total fatalities:
38
Captain / Total flying hours:
7818
Captain / Total hours on type:
1648.00
Copilot / Total flying hours:
3501
Copilot / Total hours on type:
408
Circumstances:
Following an uneventful flight from Málaga-Pablo Ruiz Picasso Airport, the crew initiated the descent to Melilla Airport in marginal weather conditions. After being cleared to descend to 7,000 feet from Sevilla ATC, the crew contacted Melilla Tower and was cleared to descend to 5,000 feet. Melilla Tower then reported that runway 33 was in use and reported wind at 270° at 5 knots, visibility 8 km with few clouds at 1,000 feet. At 0645LT the copilot reported that they were at 22 nm at an altitude of 3,000 feet. From this point, the crew descended below the minimum safe altitude of 4,000 feet and crossed the coast line in limited visibility due to low clouds. At 0749 and 52 seconds, the GPWS alarm sounded twice in the cockpit. Few seconds later, the aircraft struck the slope of a mountain located near Cap de Trois Fourche. The aircraft disintegrated on impact and all 38 occupants were killed.
Probable cause:
Given the facts and analysis conducted, the Commission concluded that the accident was caused by a collision with terrain in IMC conditions. This confirms the hypothesis put forward by members of the committee of investigation from the beginning of their investigations, it is a type of CFIT accident (collision with the ground without loss of control) due to the combination of the following factors:
- Non application of the arrival procedure, including descending below the minimum safe altitude,
- Inadequate crew coordination,
- Non application of company procedures regarding the GPWS alarm.
Final Report:

Crash of a Piper PA-31P Pressurized Navajo in Myrtle Beach

Date & Time: Sep 25, 1998
Type of aircraft:
Operator:
Registration:
N684AE
Survivors:
Yes
MSN:
31-7400207
YOM:
1974
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
For unknown reasons, the twin engine airplane belly landed at Myrtle Beach and was damaged beyond as a result. The pilot, sole on board, escaped uninjured.

Crash of a Convair CV-240-13 in San Juan

Date & Time: Sep 24, 1998 at 1319 LT
Type of aircraft:
Registration:
N91237
Flight Type:
Survivors:
Yes
Schedule:
San Juan – Santiago de Cuba
MSN:
140
YOM:
1949
Flight number:
TFA237
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7772
Captain / Total hours on type:
1409.00
Aircraft flight hours:
33835
Circumstances:
During the initial takeoff roll, there was a fluctuation of Brake Mean Engine Pressure (BMEPa measurement of engine output) on #2 engine, and the pilot elected to abort the takeoff. The pilot completed two additional engine run-ups, and no abnormalities were noted. During the second attempted takeoff, and as the airplane climbed through 200 feet MSL, a loud bang or back fire from the #2 engine was heard. BMEP fluctuated and dropped showing about 150 BMEP difference with engine #1. The engine oil temperature started to rise rapidly, the engine oil pressure dropped and the airplane started to vibrate. The first officer reduced the #2 engine to 'dry' power, upon which a second bang or backfire was heard from the #2 engine. The #2 propeller was then feathered by the First Officer. Since altitude could not be maintained, the pilot ditched the airplane in the salt water lagoon. An FAA Inspector who examined the crash site noted that the right engine propeller was not fully feathered, and the wing flaps were extended about three degrees.. The airplane was recovered from the water 70 days after the accident. The flight crew completed the engine out emergency procedure in accordance with the prescribed checklist.
Probable cause:
The loss of power in the No. 2 engine for undetermined reasons, and the inability of the pilot to establish a climb and/or maintain altitude. A factor was the incompletely feathered No. 2 propeller.
Final Report:

Crash of a Piper PA-60 Aerostar (Ted Smith 600) in North Myrtle Beach: 5 killed

Date & Time: Sep 20, 1998 at 1331 LT
Operator:
Registration:
N17MT
Flight Type:
Survivors:
No
Schedule:
North Myrtle Beach – Donegal Springs
MSN:
60-0641-7961203
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
1321
Captain / Total hours on type:
474.00
Aircraft flight hours:
3413
Circumstances:
After takeoff while over the departure end of the runway, deep gray colored smoke was observed by the tower controller trailing the right engine. The pilot was alerted of this and advised the controller the flight was returning. Witnesses reported seeing smoke trailing the right engine and that the airplane rolled to the left, pitched nose down, impacted trees, and then the ground. A fatigue crack was detected in the exhaust aft of the No. 6 cylinder of the right engine; and incomplete fusion of a weld repair was also noted. Heat damaged components from the right engine were replaced and the engine was started and found to operate normally. A foreign object of undetermined origin was found in the intake area of the No. 3 cylinder. Analysis of the voice tape revealed both engines/propellers were operating near full rated rpm when the pilot acknowledged the transmission that smoke was trailing the right engine, one engine/propeller rpm then decreased to about 2,160 rpm. Examination of the flight controls revealed no evidence of preimpact failure or malfunction. Flap positions at impact could not be determined. Calculations indicate that the airplane was approximately 55 pounds over the maximum certificated takeoff weight at takeoff.
Probable cause:
The pilot's failure to maintain airspeed (Vs) during a single engine approach resulting in an inadvertent stall. Factors contributing to the accident were a fatigue crack in the exhaust pipe in the right engine, the aircraft weight and balance was exceeded, degraded aircraft performance and the pilot's diverted attention.
Final Report:

Crash of a Boeing 737-524 in Guadalajara

Date & Time: Sep 16, 1998 at 2253 LT
Type of aircraft:
Operator:
Registration:
N20643
Survivors:
Yes
Schedule:
Houston - Guadalajara
MSN:
28904
YOM:
1997
Flight number:
CO475
Country:
Crew on board:
6
Crew fatalities:
Pax on board:
102
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On September 16, 1998, at 2253 central daylight time, a Boeing 737-524 transport airplane, N20643, operating as Continental Airlines flight 475, was substantially damaged following a loss of control during the landing roll at the Don Miguel Hidalgo International Airport near Guadalajara, Mexico. The 2 airline transport rated pilots, the 4 flight attendants, and the 102 passengers were not injured. The airplane was owned and operated by Continental Airlines of Houston, Texas, under Title 14 CFR Part 121. Night visual meteorological conditions prevailed for the scheduled international passenger-cargo flight for which an IFR flight plan was filed. The flight was dispatched from the George Bush International Airport near Houston, Texas, at 2056, for the two hour flight to Guadalajara, State of Jalisco, Mexico. The flight's scheduled arrival time was 2254. After executing a missed approach on their first ILS approach to runway 28, the flight was vectored for a second approach to runway 28. The second approach was reported by both pilots to be uneventful; however, after touchdown, the aircraft drifted to the left side of the runway. The left main landing gear exited the hard surface of the runway approximately 2,700 feet from the landing threshold and eventually all 3 landing gears exited the 197 foot wide asphalt runway. The first officer, who was flying the airplane, stated that he never felt any anti-skid cycling during the landing roll and did not feel any "radical braking" which was expected with the auto-brake in the number 3 setting. The airplane's nose landing gear collapsed resulting in structural damage to the avionics bay, the forward baggage compartment, the engine cowlings and pylons. Both engines incurred FOD. A total of 15 runway lights on the southern edge of runway 28 were found either sheared or knocked down. The tower operator reported that intermittent heavy rain showers accompanied with downdrafts and strong winds associated with a thunderstorm northeast of the airport prevailed throughout the area at the time of the accident. The two transport category airplanes that landed prior to Continental flight 475 reported windshear on final approach. The winds issued to Continental 475 by the tower while on short final were from 360 degrees at 20 knots, gusting to 40 knots. Prior to the arrival of Continental flight 475, an Aeromexico MD-82, drifted to the left side of the runway to the point where the left main gear exited the hard surface of the runway. The pilot of that flight stated that he used differential power to regain control and bring the aircraft back on the runway. The flight taxied to the gate without further incident.

Crash of a Piper PA-60 Aerostar (Ted Smith 600) in Donegal Springs: 1 killed

Date & Time: Sep 4, 1998 at 2040 LT
Registration:
N600JB
Flight Type:
Survivors:
No
Schedule:
Donegal Springs – Philadelphie
MSN:
60-0001
YOM:
1967
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1185
Captain / Total hours on type:
398.00
Circumstances:
The airplane departed at night after maintenance was performed on the left engine. The pilot attempted to return to the airport and while on base leg struck the ground inverted and nose down. The left engine propeller was found feathered. On the left engine, the # 5 cylinder was off the engine and the # 5 piston with the connecting rod still attached were found nearby. Interviews revealed that during maintenance, the # 1,3,5,and 6 cylinders had been removed and reinstalled; however, the # 5 cylinder had not been tightened. Several people had worked on the airplane at various stages of the work. The maintenance facility did not have a system to pass down what had been accomplished, and the FAA did not require the tracking of work accomplished in other than 14 CFR Part 121, or 14 CFR Part 145 facilities.
Probable cause:
The failure of the pilot to maintain airspeed during a precautionary landing which resulted in a loss of control while operating with one engine shutdown. An additional cause was the improper maintenance procedures that resulted in the #5 cylinder not being tightened down. A factor was the night conditions.
Final Report:

Crash of a Boeing 727-228F in New York

Date & Time: Aug 31, 1998 at 2235 LT
Type of aircraft:
Operator:
Registration:
N722DH
Flight Type:
Survivors:
Yes
Schedule:
New York - Covington
MSN:
19861
YOM:
1969
Flight number:
DHL1165
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
16000
Captain / Total hours on type:
5000.00
Copilot / Total flying hours:
6000
Copilot / Total hours on type:
1200
Aircraft flight hours:
50861
Circumstances:
Shortly after takeoff, the No. 2 engine failed and shutdown procedures for the No. 2 engine were accomplished. The flight crew declared an emergency and requested to return to the airport. On approach, an engine out go-around was required as ATC had instructed the flight crew of a B-747 to "position and hold" on the end of the runway. The first officer was the pilot flying. Following an uneventful touchdown, as the airplane slowed to about 80 knots, the captain took control of the airplane. Shortly thereafter, the right main landing gear (MLG) collapsed and the airplane slid to a stop on the runway. Examination of the No. 2 engine revealed that 80 percent of the main fuel pump main drive shaft was worn to the spline root. The examination also revealed that the grease used to lubricate the main drive shaft output splines was not the authorized grease specified per OHM 73-11-1 or MIL-G-81322. Additionally, the magnetic seal compression O-ring that rides on the drive gear journal outer diameter was hardened and exhibited inner diameter axial cracks. The component manufacturer indicated that the failure of the magnetic seal was the first such reported incident in 30 years; however, it agreed to review operational data from airlines to reevaluate the mean time between overhaul intervals for the seal and to recommend an inspection interval, as necessary. Examination of the right MLG revealed a fracture failure of the trunnion bearing support fitting that was caused by fatigue cracking and stress corrosion cracking.
Probable cause:
The failure of the right main landing gear caused by fatigue cracking and stress corrosion cracking of the trunnion bearing support fitting.
Final Report:

Crash of a Fokker F27 Friendship 600 in Tachilek: 36 killed

Date & Time: Aug 24, 1998 at 0835 LT
Type of aircraft:
Operator:
Registration:
XY-AEN
Survivors:
No
Schedule:
Yangon - Tachilek
MSN:
10476
YOM:
1972
Flight number:
UB635
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
32
Pax fatalities:
Other fatalities:
Total fatalities:
36
Circumstances:
While descending to Tachilek Airport following an uneventful flight from Yangon, the captain informed ATC he just passed 9,500 feet. Shortly later, on final approach, the aircraft struck the slope of the hill of Payakha located 3 km short of runway. The aircraft was totally destroyed and all 36 occupants were killed.
Probable cause:
For unknown reasons, the crew descended below MDA until the aircraft impacted the ground.

Crash of an Antonov AN-26 in Norilsk

Date & Time: Aug 24, 1998
Type of aircraft:
Registration:
RA-26568
Survivors:
Yes
Schedule:
Dikson – Norilsk
MSN:
38 08
YOM:
1976
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
15
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Following an uneventful flight from Dikson, the aircraft landed at Norilsk-Alykel Airport at a speed of 200 km/h. After touchdown, the crew started the braking procedure when the captain inadvertently raised the landing gear. As the gear were locked down, they remained extended but after entering the taxiway, the crew increased power and the speed reached 135 km/h when an unloading of the landing gear and a decompression of the right hand main landing gear damper occurred. This caused the right main gear to collapse slowly. The airplane went out of control, veered to the right and came to rest out of the taxiway. All 20 occupants escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
Failure of the crew who mistakenly raised the landing gear during the deceleration procedure and an excessive speed while taxiing.