Crash of a Piper PA-31P-425 Pressurized Navajo in Myrtle Beach: 1 killed

Date & Time: May 21, 2021 at 1814 LT
Type of aircraft:
Operator:
Registration:
N575BC
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Myrtle Beach - North Myrtle Beach
MSN:
31-7730003
YOM:
1977
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
20000
Aircraft flight hours:
4826
Circumstances:
The airplane departed Myrtle Beach International Airport (MYR), Myrtle Beach, South Carolina, at 1812, with the intended destination of Grand Strand Airport (CRE), North Myrtle Beach, South Carolina. According to automatic dependent surveillance-broadcast and air traffic control (ATC) communications information, the pilot established contact with ATC and reported that he was ready for departure from runway 18. He was instructed to fly runway heading, climb to 1,700 ft mean sea level (msl), and was cleared for takeoff. Once airborne, the controller instructed the pilot to turn left; however, the pilot stated that he needed to return to runway 18. The controller instructed the pilot to enter a right closed traffic pattern at 1,500 ft msl. As the airplane continued to turn to the downwind leg of the traffic pattern, it reached an altitude of about 1,000 ft mean sea level (msl). While on the downwind leg of the traffic pattern, the airplane descended to 450 ft msl, climbed to 700 ft msl, and then again descended to 475 ft msl before radar contact was lost. About 1 minute after the pilot requested to return to the runway, the controller asked if any assistance was required, to which the pilot replied, “yes, we’re in trouble.” There were no further radio communications from the pilot. The airplane crashed in a field and was destroyed by impact forces and a post crash fire. The pilot, sole on board, was killed.
Probable cause:
The mechanic’s inadvertent installation of the elevator trim tabs in reverse, which resulted in the pitch trim system operating opposite of the pilot’s input and the pilot’s subsequent loss of control.
Final Report:

Crash of a Beechcraft 200 Super King Air in North Myrtle Beach: 6 killed

Date & Time: Feb 3, 2006 at 2045 LT
Registration:
N266EB
Survivors:
No
Schedule:
Trenton - North Myrtle Beach
MSN:
BB-266
YOM:
1977
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
3400
Aircraft flight hours:
8154
Circumstances:
The multi-engine airplane rolled inverted and dove into the ground on a landing approach. According to witnesses, the airplane made two approaches to runway 23. During the first approach the airplane was observed, "fish tailing" while about 30' feet over the runway. The airplane appeared to regain control and continued flying over the runway until passing the air traffic control tower, at which time the airplane began a climbing left turn. The witnesses stated that they heard the pilot tell the air traffic controller that he was doing a go-around. The controller asked the pilot if he had problems with the sea fog. The pilot responded back to the controller "no that his left engine kept power up a little too much and would not come back." The witnesses observed the airplane circle the airport to the left, and watched it line up on runway 23 for the second time. The witnesses stated that as the airplane descended to the runway and without any indication of trouble, the airplane "climbed and rolled left, went inverted and nosed down into the grass to the left of the runway and burst into flames." Examination of the airplane, airplane systems, engines, and propellers found no abnormal preimpact conditions that would have interfered with the normal operation of the airplane. No recorded radar data for the flight was located that captured the airplane's two attempted landings. Information contained in the Super King Air 200 Pilot's Operating Handbook (POH) and FAA Approved Flight Manual (AFM) showed the stall speed with gear extended, 40-degrees flaps, and zero bank angle as 84 knots Indicated Air Speed.
Probable cause:
The pilot's failure to maintain control during landing approach for undetermined reasons.
Final Report:

Crash of a Piper PA-60 Aerostar (Ted Smith 600) in North Myrtle Beach: 5 killed

Date & Time: Sep 20, 1998 at 1331 LT
Operator:
Registration:
N17MT
Flight Type:
Survivors:
No
Schedule:
North Myrtle Beach – Donegal Springs
MSN:
60-0641-7961203
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
1321
Captain / Total hours on type:
474.00
Aircraft flight hours:
3413
Circumstances:
After takeoff while over the departure end of the runway, deep gray colored smoke was observed by the tower controller trailing the right engine. The pilot was alerted of this and advised the controller the flight was returning. Witnesses reported seeing smoke trailing the right engine and that the airplane rolled to the left, pitched nose down, impacted trees, and then the ground. A fatigue crack was detected in the exhaust aft of the No. 6 cylinder of the right engine; and incomplete fusion of a weld repair was also noted. Heat damaged components from the right engine were replaced and the engine was started and found to operate normally. A foreign object of undetermined origin was found in the intake area of the No. 3 cylinder. Analysis of the voice tape revealed both engines/propellers were operating near full rated rpm when the pilot acknowledged the transmission that smoke was trailing the right engine, one engine/propeller rpm then decreased to about 2,160 rpm. Examination of the flight controls revealed no evidence of preimpact failure or malfunction. Flap positions at impact could not be determined. Calculations indicate that the airplane was approximately 55 pounds over the maximum certificated takeoff weight at takeoff.
Probable cause:
The pilot's failure to maintain airspeed (Vs) during a single engine approach resulting in an inadvertent stall. Factors contributing to the accident were a fatigue crack in the exhaust pipe in the right engine, the aircraft weight and balance was exceeded, degraded aircraft performance and the pilot's diverted attention.
Final Report:

Crash of a Beechcraft 65-80 Queen Air in North Myrtle Beach

Date & Time: Jun 5, 1998 at 1531 LT
Type of aircraft:
Registration:
N215AB
Flight Type:
Survivors:
Yes
Schedule:
Malone - North Myrtle Beach
MSN:
LD-58
YOM:
1963
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
535
Captain / Total hours on type:
48.00
Aircraft flight hours:
6758
Circumstances:
After a 4.7 hour flight, while turning onto final, the airplane landed short. The pilot did not mention engine problems during a police interview. He subsequently told an FAA Inspector that the left engine failed, then later, that the right engine failed. He told the Safety Board that both engines failed. Adequate fuel was confirmed. The previous day, the right engine failed approaching another airport. The pilot performed a single-engine go-around, with landing gear and flaps down. He refused assistance and performed his own maintenance. He cleaned the fuel filters of both engines. During a ground runup, the right engine was hard to start, and required a high fuel flow to remain running. After the pilot re-cleaned the right fuel filter the engine ran fine. The flight was uneventful until the accident. Post-flight examination revealed all propeller blades bent back 90 degrees, with significant chordwise scoring on one blade per engine. The left engine fuel filter was relatively clean, with some brown residue which contained ferrous material. The right engine fuel filter was heavily coated with a white residue which contained aluminum, and brown material which contained ferrous material. The pilot received his multi-engine rating on April 22, 1998.
Probable cause:
The pilot's failure to follow emergency procedures, and his failure to maintain control of the airplane after a loss of power from one engine. Factors include fuel filter blockage, inadequate maintenance, and the pilot's lack of experience in multi-engine airplanes.
Final Report: