Crash of a Boeing EC-135C at Pope AFB

Date & Time: Sep 2, 1997
Type of aircraft:
Operator:
Registration:
63-8053
Flight Type:
Survivors:
Yes
Schedule:
Pope - Pope
MSN:
18701
YOM:
1964
Crew on board:
11
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was completing a local training flight at Pope AFB. For unknown reasons, the aircraft landed very hard, causing the nose gear to collapse. The aircraft was stopped on the runway and all 11 occupants escaped uninjured. The aircraft was damaged beyond repair.

Crash of a Lockheed C-130H Hercules in Tegucigalpa: 3 killed

Date & Time: Apr 1, 1997
Type of aircraft:
Operator:
Registration:
88-4408
Flight Type:
Survivors:
Yes
Schedule:
Milwaukee – Tegucigalpa – Howard AFB
MSN:
5161
YOM:
1989
Country:
Crew on board:
10
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
The aircraft departed Milwaukee-General Billy Mitchell Airport on a flight to Howard AFB, Panama City, with an intermediate stop in Tegucigalpa, carrying 10 crew members and a load consisting of foods and electronics. At Tegucigalpa-Toncontin Airport, the aircraft landed 2,000 feet past the runway threshold in a 50° flaps down configuration. Unable to stop within the remaining distance, it overran and crashed on a road and a bridge, bursting into flames. Three crew members were killed and seven others were injured.

Crash of a Lockheed HC-130P Hercules in the Pacific Ocean: 10 killed

Date & Time: Nov 22, 1996 at 1846 LT
Type of aircraft:
Operator:
Registration:
64-14856
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Portland - North Island
MSN:
4072
YOM:
1965
Flight number:
King 56
Country:
Region:
Crew on board:
11
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
10
Circumstances:
Based upon digital flight data recorded (DFDR) information, the mishap aircraft departed Portland IAP at 1720 PST on 22 Nov 96 on an instrument flight rules (IFR) flight en route to North Island Naval Air Station. The purpose of the sortie was to conduct an overwater navigation evaluation. King 56 began the sortie with a normal takeoff, departure and climbout. One hour and 24 minutes after takeoff in level flight at FL 220 the mishap sequence began with the engineer commenting on a torque flux on the number 1 engine. Nothing on the cockpit voice recorder (CVR), the DFDR, or the survivor’s testimony suggested any unusual events prior to the engineer’s comment. Over the next three minutes, the operations of all four engines became unstable and eventually failed. Crew actions during these critical three minutes are known only by verbal comments on the CVR and the survivor’s testimony. The following discusses what we know of those actions. The engineer called for n°1 propeller to be placed in mechanical governing. This would normally remove electrical inputs to the propeller through the synchrophaser. The pilot then called for all four propellers to be placed in mechanical governing. This action was consistent with treating this emergency as a four-engine rollback. There is no indication on the DFDR or the CVR as to whether or not the crew selected mechanical governing on any of the remaining three propellers. At the same time the crew was analyzing the emergency, they also declared an in-flight emergency with Oakland ARTCC and turned the mission aircraft east to proceed toward Kingsley Field, Klamath Falls, OR, approximately 230 miles away and approximately 80 miles from the coast. The Radio Operator radioed the USCG Humboldt Bay Station and notified them of the in-flight emergency. During the turn toward the shore the number 3 and number 4 engines once briefly recovered most of their torque. These increases are recorded by the flight data recorder. When the RPM on number 3 (the aircraft’s last functioning engine) finally decreased below 94% RPM the last generator producing electrical power dropped off line due to low frequencies. As a result, at 1846 Pacific Standard Time all electrical power was lost. After a brief period, power was restored to the equipment powered by the battery bus. From this point on, the aircraft glided to the attempted ditching. There is no record of that portion of the flight, except the survivor’s testimony.The outboard wing sections and all four engines separated from the center wing section that in turn separated from the fuselage. Subsequently, the engines and fuselage went straight to the ocean floor at a depth of approximately 5500 feet. The outer wing and the center wing sections floated on the surface for several days and sank more than 50 nm from the impact location. The radio navigator was rescued while 10 other crew members were killed.
Probable cause:
Fuel starvation for unknown reasons.

Crash of a Lockheed C-130H Hercules on Mt Sleeping Indian: 9 killed

Date & Time: Aug 17, 1996 at 2250 LT
Type of aircraft:
Operator:
Registration:
74-1662
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Jackson Hole - New York
MSN:
4597
YOM:
1975
Flight number:
Havoc 58
Crew on board:
8
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total flying hours:
1744
Captain / Total hours on type:
904.00
Copilot / Total flying hours:
188
Copilot / Total hours on type:
149
Circumstances:
The aircraft departed Jackson Hole Airport at 2245LT on a flight to New York-JFK, carrying eight crew members and a U.S. Secret Service agent. The purpose of the flight was to transport a U.S. Secret Service communications vehicle to New York after President Bill Clinton spent some vacations in Jackson Hole. Five minutes after takeoff, while climbing by night, the four engine aircraft struck the slope of Mt Sleeping Indian (Mt Sheep - 3,427 metres high) located about 18 km southeast of the airport. The aircraft disintegrated on impact and all nine occupants were killed.
Probable cause:
Controlled flight into terrain after the crew's failure to properly plan for a night departure from an unfamiliar airport. The crew did not follow the published instrument departure procedures and was relatively inexperienced.
Final Report:

Crash of a Boeing CT-34A in Dubrovnik: 35 killed

Date & Time: Apr 3, 1996 at 1457 LT
Type of aircraft:
Operator:
Registration:
73-1149
Flight Type:
Survivors:
No
Schedule:
Tuzla - Dubrovnik
MSN:
20696
YOM:
1973
Flight number:
IFO21
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
29
Pax fatalities:
Other fatalities:
Total fatalities:
35
Circumstances:
A United States Air Force Boeing T-43A (USAF designation for the Boeing 737-200) was destroyed after impacting a hillside during an NDB approach to Dubrovnik Airport, Croatia. All 35 on board were killed. The aircraft was engaged in a mission to fly United States Secretary of Commerce Ron Brown and a delegation of industry executives around the region for visits. The party was to be flown from Zagreb to Tuzla and Dubrovnik before returning to Zagreb. Operating with a call sign of IFO21, the accident aircraft departed Zagreb at 06:24 hours. The crew landed at Tuzla at 07:15 after an uneventful flight. The passengers deplaned, and the aircraft was then repositioned to Split because of insufficient ramp space at Tuzla to park the aircraft for the duration of the visit. At 12:47, the aircraft landed at Tuzla, where the passengers reboarded. The accident flight departed Tuzla for Dubrovnik at 13:55. After crossing Split at 14:34 the flight was cleared to descend from FL210 to FL140. Further descent clearance was given to FL100. After the aircraft reached FL100 at 14:45, south of Split VOR, Zagreb Center transferred control to Dubrovnik Approach/Tower. The controller cleared IFO21 direct to the Kolocep (KLP) NDB. After opposite-direction traffic had been cleared, IFO21 was cleared to descend to 5000 feet. At 14:52, the crew told Dubrovnik Approach/Tower that they were 16 NM from the airport. They were cleared to descend to 4,000 feet and told to report crossing the KLP beacon. At 14:53, the aircraft crossed KLP, which was the Final Approach Fix (FAF), at 4100 feet and began the approach without approach clearance from Dubrovnik Tower. At that point the aircraft was slightly high and fast and not completely configured for the approach, as it should have been. At 14:54, the copilot of IFO21 called Dubrovnik Approach/Tower and said, "We’re inside the locator, inbound." IFO21 was then cleared for the NDB approach to runway 12. The aircraft tracked a course of 110 degrees after crossing KLP, instead of tracking the published course of 119 degrees. The aircraft maintained this track from KLP to the point of impact. The accident aircraft descended to 2200 feet which was consistent with the published minimum descent altitude of 2,150 feet. At 14:57, the aircraft impacted a rocky mountainside approximately 1.7 NM to the left (northeast) of the extended runway centerline and 1.8 NM north of the approach end of runway 12 at Dubrovnik Airport.
Probable cause:
Controlled flight into terrain. The following findings were reported:
- The command failure to comply with directives that required a review of all instrument approach procedures, not approved by the Defense Dept,
- Preflight planning errors, combined with errors made during the flight made by the aircrew,
- Improper design of the Dubrovnik NDB.

Crash of a Boeing E-3B Sentry at Elmendorf AFB: 24 killed

Date & Time: Sep 22, 1995 at 0747 LT
Type of aircraft:
Operator:
Registration:
77-0354
Flight Phase:
Survivors:
No
Schedule:
Elmendorf - Elmendorf
MSN:
21554
YOM:
1978
Flight number:
Yukla 27
Crew on board:
4
Crew fatalities:
Pax on board:
20
Pax fatalities:
Other fatalities:
Total fatalities:
24
Circumstances:
The aircraft was dispatched out from Elmendorf AFB on an AWACS survey mission under call sign Yukla 27, carrying 20 passengers and four crew members. Shortly after takeoff from runway 05, while in initial climb, the aircraft collided with a flock of Canada geese that struck both left engines n°1 and 2. The aircraft climbed to a maximum height of about 250 feet when the engine n°1 failed and the engine n°2 exploded. The aircraft entered an uncontrolled left roll, causing the left wing to struck trees. Out of control, it crashed in a huge explosion in a wooded area located about a mile from the runway end. The aircraft disintegrated on impact and all 24 occupants were killed. Numerous dead geese were found at the crash site.
Probable cause:
It was determined that the loss of control and subsequent crash was the consequence of a collision with Canada geese during initial climb. Investigations revealed that a USAF Lockheed C-130 just took off from the same runway about two minutes prior to the accident. At that time, numerous geese were standing near the runway end and were probably disturbed by the C-130 low pass. All geese took off and remained hovering at low height. This phenomenon was spotted by the tower controller who failed to warn the Sentry crew accordingly. It was also determined that there was no efficient program to detect and deter bird hazard at Elmendorf AFB.

Crash of a Lockheed C-130E Hercules near Bliss: 6 killed

Date & Time: May 13, 1995
Type of aircraft:
Operator:
Registration:
62-1838
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Boise - Colorado Springs
MSN:
3801
YOM:
1963
Flight number:
Sumit 38
Location:
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
After departure from Boise-Gowen Field, en route to Peterson AFB in Colorado Springs, the crew encountered technical problems with the engine n°2. The crew declared an emergency and elected to divert to Mountain Home AFB. About 20 minutes into the flight, the engine n°2 compressor disintegrated. The aircraft entered an uncontrolled descent and crashed 12 miles north of Bliss. All six crew members were killed.
Crew:
Lt Col Robert Buckout, Commander
1st Lt Lance Daugherty, pilot,
Cpt Geoffery Boyd, navigator,
CMSgt Jimmy Vail, flight engineer,
M/Sgt Jay Kemp, loadmaster,
S/Sgt Michael Scheideman, loadmaster.
Probable cause:
The cause of the crash was that the number 2 (inside left wing) engine had a buggy undertemp sensor, causing the crew to enrich the fuel mixture, leading to an actual engine overtemp. One of the fuel lines ruptured or melted, causing the fire, and one of the crewmen hit the fire carts, but the fire re-erupted moments later, and there were no more extinguishers available for that engine. One of the pins that was supposed to melt in an engine fire, releasing the engine from the AC, failed to release the engine properly, while another worked properly. Still half connected to the wing hard point, the engine torqued at an awkward angle, causing severe wing and fuselage damage, which led to the crash.

Crash of a Learjet C-21A in Alexander City: 8 killed

Date & Time: Apr 17, 1995 at 1820 LT
Type of aircraft:
Operator:
Registration:
84-0136
Flight Type:
Survivors:
No
Schedule:
Randolph – Wright-Patterson – Andrews – Randolph
MSN:
35-583
YOM:
1985
Flight number:
Kiowa 71
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
8
Captain / Total flying hours:
1074
Captain / Total hours on type:
877.00
Copilot / Total flying hours:
2242
Copilot / Total hours on type:
547
Circumstances:
The C-21A, a USAF designation of the Learjet 35A was assigned to the 332nd Airlift Flight at Randolph AFB, Texas. The aircraft would depart Randolph AFB as flight Kiowa 71 to Wright-Patterson AFB, Andrews AFB and then back to Randolph. The aircraft was landed at Andrews AFB at 10:57. The crew requested a full load of fuel and told Serv-Air maintenance technicians that they had been unable to transfer fuel from the wing tanks to the fuselage tank. A Serv-Air maintenance technician removed the fuel-control panel from the aircraft and replaced the fuselage-tank transfer/fill switch. The maintenance technician told the crew that replacement of the fuselage-tank switch had not corrected the problem and that he was going to try to correct the problem by replacing the fuel-control relay panel. This was a time consuming job. The crew decided to continue back to Randolph without the repairs. The fuselage fuel tank was full and they had not had trouble earlier in the day getting fuel out of the fuselage tank. The aircraft departed from Andrews AFB at 16:38. The aircraft was in cruise flight at FL390 at 17:53 when the crew began to transfer fuel from the fuselage tank to the wing tanks. The crew did not know that the right standby fuel pump was operating and was preventing fuel from being transferred from the fuselage tank to the right wing. Bearings in the right standby pump were in a deteriorated condition and the pump had required higher-than-normal electrical current for rotation. The higher-than-normal electrical current had caused progressive damage to two contacts in the fuel control relay panel and eventually had caused the contacts to bond together. This caused the pump to run continuously throughout the flight and to prevent fuel transfer from the fuselage tank to the right wing. The aircrew noticed that the left wing-tip tank had become 800 pounds [363 kilograms] heavier than the right wing-tip tank during the transfer, and they attempted to analyse the malfunction and correct the imbalance. A fuel-imbalance during-fuel-transfer malfunction however was not included in the Air Force training syllabus, nor was the procedure contained in the C-21A checklist. At 17:56, the copilot told the Atlanta Air Route Traffic Control Center (Atlanta Center) controller, "Sir, we need to revise our flight plan. We’re having a problem getting some fuel out of one of our wings. Can we get vectors to Maxwell Air Force Base? And we’re going to need to dump fuel for about five minutes." The crew at 18:00 began to dump fuel from the left wing-tip tank. However, they still had an imbalance in the wing tanks themselves of about 200 pounds (91 kilograms). At 18:03 the flight was cleared to descend from FL350. The crew then observed that fuel quantity was decreasing rapidly in the right wing tank, that the left wing tank was full and that the left wing-tip tank had begun to fill with fuel. At 18:07, the copilot told the Atlanta Center controller, "Sir, we’d like to declare an emergency at this time for a fuel problem and, ah, get to Maxwell quick as we can." They were cleared direct to Maxwell AFB and cleared to descend to 17,000 feet, and later to 11,000 feet. At 18:15, the copilot told Atlanta Center, "We need to change the airfield, to get to the closest piece of pavement we can land on." The controller said, "Kiowa 71, we got an airport at 12 o’clock and 12 miles. It’s Alexander City." The crew accepted this and began their emergency descent into Alexander City airport. At 18:16 the copilot took over control since the captain did not have the airfield in sight and the copilot did. The aircraft was northeast of the airport at 8,800 feet and was descending at 5,600 feet per minute with the wing-lift spoilers extended when the copilot told Atlanta Center that they were on a left base for the runway. The crew attempted to fly a visual traffic pattern to runway 18 but were in a poor position to complete the approach and landing. They subsequently elected to enter a left downwind leg for runway 36. As airspeed was reduced, aileron authority diminished and, because of the fuel imbalance, the aircraft became difficult to control. The copilot, flying from the right seat, did not have a good view of the runway and asked the aircraft commander for help in positioning the aircraft on downwind and in beginning the turn toward the runway. The captain wanted to get the gear down but the copilot had difficult controlling the plane already: "Don’t put anything down," the copilot said. "Nothing down, nothing down." The aircraft was at 2,030 feet when the gear-warning horn sounded. The captain said, "Gear down. Gear down." The copilot said, "No. Stand by. Stand by." "Gear down," the captain said. "Gear down, man." "No, not yet, not yet," the copilot said. The copilot then asked the aircraft commander to "push the power up a little bit for me." Power was increased and the gear was extended. The aircraft was at about 1,500 feet and was one mile southwest of the runway at 18:19 when the copilot began a left turn. Approximately halfway through the final turn and one mile due south of runway 36, the aircraft abruptly rolled out, flew through the extended runway centerline and continued in an east, northeasterly direction approximately 800 feet above the ground. The copilot had rolled out of the turn to regain lateral control of the aircraft. At this time the right engine was operating at a reduced thrust setting in an attempt to counteract the effects of the fuel imbalance. The captain, to center the ball in the slip indicator, applied pressure on the left rudder, against pressure that was being applied on the right rudder by the copilot. The captain said, "Step on the rudder. Step on the rudder." The copilot said, "Paul, no. Paul, don’t." The application of left rudder caused the aircraft to roll left rapidly. It rolled inverted entered the trees and struck the ground.
Probable cause:
The investigating officer found that the mechanical malfunction consisted of the right standby [fuel] pump continuing to operate uncommanded after engine start. This malfunction resulted in fuel being pumped into the left wing and prevented fuel from being transferred to the right wing during normal transfer procedures. This condition caused a fuel imbalance. The Air Force, for whatever reason, did not contract for flight-manual updates from Learjet following purchase of the airplane in 1984. The "fuel imbalance during fuel transfer" emergency procedure was included in civilian Learjet flight-manual updates published by subsequent to 1984. As a result, the Air Force training syllabus likewise did not include this emergency procedure. Because the crew did not have checklist or flight-manual guidance on this problem, the crew misanalysed the malfunction. They failed to correct the fuel imbalance as a result, allowed their airspeed to become too slow for the aircraft’s configuration when attempting to land and then made control inputs that caused the aircraft to enter a flight regime from which they could not recover.