Crash of a Fokker F28 Fellowship 4000 in Sittwe

Date & Time: Jun 6, 2009 at 0820 LT
Type of aircraft:
Operator:
Registration:
XY-ADW
Survivors:
Yes
Schedule:
Yangon - Sittwe
MSN:
11114
YOM:
1977
Flight number:
UB409
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
62
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Following an uneventful flight from Yangon, the crew completed the approach to Sittwe Airport in poor weather conditions. The aircraft landed hard on runway 11, causing the right main gear to collapse. The right wing struck the ground and was partially sheared off. The aircraft went out of control, veered off runway to the left and came to rest against a fence. Three occupants, among them the captain, were slightly injured and the aircraft was damaged beyond repair. At the time of the accident, the runway threshold and edge lights as well as the VASIS were unserviceable.

Crash of an Airbus A330-203 off Fernando de Noronha: 228 killed

Date & Time: Jun 1, 2009 at 0014 LT
Type of aircraft:
Operator:
Registration:
F-GZCP
Flight Phase:
Survivors:
No
Schedule:
Rio de Janeiro – Paris
MSN:
660
YOM:
2005
Flight number:
AF447
Country:
Crew on board:
12
Crew fatalities:
Pax on board:
216
Pax fatalities:
Other fatalities:
Total fatalities:
228
Captain / Total flying hours:
6547
Captain / Total hours on type:
4479.00
Copilot / Total flying hours:
2936
Copilot / Total hours on type:
807
Aircraft flight hours:
18870
Aircraft flight cycles:
2644
Circumstances:
On Sunday 31 May 2009, the Airbus A330-203 registered F-GZCP operated by Air France was programmed to perform scheduled flight AF 447 between Rio de Janeiro-Galeão and Paris Charles de Gaulle. Twelve crew members (3 flight crew, 9 cabin crew) and 216 passengers were on board. The departure was planned for 22 h 00. At around 22 h 10, the crew was cleared to start up engines and leave the stand. Takeoff took place at 22 h 29. The Captain was Pilot Not Flying (PNF); one of the copilots was Pilot Flying (PF). At the start of the Cockpit Voice Recorder (CVR) recording, shortly after midnight, the aeroplane was in cruise at flight level 350. Autopilot 2 and auto-thrust were engaged. Auto fuel transfer in the “trim tank” was carried out during the climb. The flight was calm. At 1 h 35, the aeroplane arrived at INTOL point and the crew left the Recife frequency to change to HF communication with the Atlántico Oceanic control centre. A SELCAL test was successfully carried out, but attempts to establish an ADS-C connection with DAKAR Oceanic failed. Shortly afterwards, the co-pilot modified the scale on his Navigation Display (ND) from 320 NM to 160 NM and noted “…a thing straight ahead”. The Captain confirmed and the crew again discussed the fact that the high temperature meant that they could not climb to flight level 370. At 1 h 45, the aeroplane entered a slightly turbulent zone, just before SALPU point. Note: At about 0 h 30 the crew had received information from the OCC about the presence of a convective zone linked to the inter-tropical convergence zone (ITCZ) between SALPU and TASIL. The crew dimmed the lighting in the cockpit and switched on the lights “to see”. The co-pilot noted that they were “entering the cloud layer” and that it would have been good to be able to climb. A few minutes later, the turbulence increased slightly in strength. Shortly after 1 h 52, the turbulence stopped. The co-pilot again drew the Captain’s attention to the REC MAX value, which had then reached flight level (FL) 375. A short time later, the Captain woke the second co-pilot and said “[…] he’s going to take my place”. At around 2 h 00, after leaving his seat, the Captain attended the briefing between the two co-pilots, during which the PF (seated on the right) said specifically that “well the little bit of turbulence that you just saw we should find the same ahead we’re in the cloud layer unfortunately we can’t climb much for the moment because the temperature is falling more slowly than forecast” and that “the logon with DAKAR failed”. Then the Captain left the cockpit. The aeroplane approached the ORARO point. It was flying at flight level 350 and at Mach 0.82. The pitch attitude was about 2.5 degrees. The weight and balance of the aeroplane were around 205 tonnes and 29%. The two copilots again discussed the temperature and the REC MAX. The turbulence increased slightly. At 2 h 06, the PF called the cabin crew, telling them that “in two minutes we ought to be in an area where it will start moving about a bit more than now you’ll have to watch out there” and he added “I’ll call you when we’re out of it”. At around 2 h 08, the PNF proposed “go to the left a bit […]”. The HDG mode was activated and the selected heading decreased by about 12 degrees in relation to the route. The PNF changed the gain adjustment on his weather radar to maximum, after noticing that it was in calibrated mode. The crew decided to reduce the speed to about Mach 0.8 and engine de-icing was turned on. At 2 h 10 min 05, the autopilot then the auto-thrust disconnected and the PF said “I have the controls”. The aeroplane began to roll to the right and the PF made a nose-up and left input. The stall warning triggered briefly twice in a row. The recorded parameters showed a sharp fall from about 275 kt to 60 kt in the speed displayed on the left primary flight display (PFD), then a few moments later in the speed displayed on the integrated standby instrument system (ISIS). The flight control law reconfigured from normal to alternate. The Flight Directors (FD) were not disconnected by the crew, but the crossbars disappeared. Note: Only the speeds displayed on the left side and on the ISIS are recorded on the FDR; the speed displayed on the right side is not recorded. At 2 h 10 min 16, the PNF said “we’ve lost the speeds ” then “alternate law protections”. The PF made rapid and high amplitude roll control inputs, more or less from stop to stop. He also made a nose-up input that increased the aeroplane’s pitch attitude up to 11° in ten seconds. Between 2 h 10 min 18 and 2 h 10 min 25, the PNF read out the ECAM messages in a disorganized manner. He mentioned the loss of autothrust and the reconfiguration to alternate law. The thrust lock function was deactivated. The PNF called out and turned on the wing anti-icing. The PNF said that the aeroplane was climbing and asked the PF several times to descend. The latter then made several nose-down inputs that resulted in a reduction in the pitch attitude and the vertical speed. The aeroplane was then at about 37,000 ft and continued to climb. At about 2 h 10 min 36, the speed displayed on the left side became valid again and was then 223 kt; the ISIS speed was still erroneous. The aeroplane had lost about 50 kt since the autopilot disconnection and the beginning of the climb. The speed displayed on the left side was incorrect for 29 seconds. At 2 h 10 min 47, the thrust controls were pulled back slightly to 2/3 of the IDLE/CLB notch (85% of N1). Two seconds later, the pitch attitude came back to a little above 6°, the roll was controlled and the angle of attack was slightly less than 5°. The aeroplane’s pitch attitude increased progressively beyond 10 degrees and the plane started to climb. From 2 h 10 min 50, the PNF called the Captain several times. At 2 h 10 min 51, the stall warning triggered again, in a continuous manner. The thrust levers were positioned in the TO/GA detent and the PF made nose-up inputs. The recorded angle of attack, of around 6 degrees at the triggering of the stall warning, continued to increase. The trimmable horizontal stabilizer (THS) began a nose-up movement and moved from 3 to 13 degrees pitch-up in about 1 minute and remained in the latter position until the end of the flight. Around fifteen seconds later, the ADR3 being selected on the right side PFD, the speed on the PF side became valid again at the same time as that displayed on the ISIS. It was then at 185kt and the three displayed airspeeds were consistent. The PF continued to make nose-up inputs. The aeroplane’s altitude reached its maximum of about 38,000 ft; its pitch attitude and angle of attack were 16 degrees. At 2 h 11 min 37, the PNF said “controls to the left”, took over priority without any callout and continued to handle the aeroplane. The PF almost immediately took back priority without any callout and continued piloting. At around 2 h 11 min 42, the Captain re-entered the cockpit. During the following seconds, all of the recorded speeds became invalid and the stall warning stopped, after having sounded continuously for 54 seconds. The altitude was then about 35,000 ft, the angle of attack exceeded 40 degrees and the vertical speed was about -10,000 ft/min. The aeroplane’s pitch attitude did not exceed 15 degrees and the engines’ N1’s were close to 100%. The aeroplane was subject to roll oscillations to the right that sometimes reached 40 degrees. The PF made an input on the side-stick to the left stop and nose-up, which lasted about 30 seconds. At 2 h 12 min 02, the PF said, “I have no more displays”, and the PNF “we have no valid indications”. At that moment, the thrust levers were in the IDLE detent and the engines’ N1’s were at 55%. Around fifteen seconds later, the PF made pitch-down inputs. In the following moments, the angle of attack decreased, the speeds became valid again and the stall warning triggered again. At 2 h 13 min 32, the PF said, “[we’re going to arrive] at level one hundred”. About fifteen seconds later, simultaneous inputs by both pilots on the side-sticks were recorded and the PF said, “go ahead you have the controls”. The angle of attack, when it was valid, always remained above 35 degrees. From 2 h 14 min 17, the Ground Proximity Warning System (GPWS) “sink rate” and then “pull up” warnings sounded. The recordings stopped at 2 h 14 min 28. The last recorded values were a vertical speed of -10,912 ft/min, a ground speed of 107 kt, pitch attitude of 16.2 degrees nose-up, roll angle of 5.3 degrees left and a magnetic heading of 270 degrees. No emergency message was transmitted by the crew. The wreckage was found at a depth of 3,900 metres on 2 April 2011 at about 6.5 NM on the radial 019 from the last position transmitted by the aeroplane. Both CVR and DFDR were found 23 months after the accident, in May 2011 at a depth of 3,900 metres. The final report was published in July 2012.
Probable cause:
The obstruction of the Pitot probes by ice crystals during cruise was a phenomenon that was known but misunderstood by the aviation community at the time of the accident. From an operational perspective, the total loss of airspeed information that resulted from this was a failure that was classified in the safety model. After initial reactions that depend upon basic airmanship, it was expected that it would be rapidly diagnosed by pilots and managed where necessary by precautionary measures on the pitch attitude and the thrust, as indicated in the associated procedure. The occurrence of the failure in the context of flight in cruise completely surprised the pilots of flight AF 447. The apparent difficulties with aeroplane handling at high altitude in turbulence led to excessive handling inputs in roll and a sharp nose-up input by the PF. The destabilization that resulted from the climbing flight path and the evolution in the pitch attitude and vertical speed was added to the erroneous airspeed indications and ECAM messages, which did not help with the diagnosis. The crew, progressively becoming de-structured, likely never understood that it was faced with a 'simple' loss of three sources of airspeed information. In the minute that followed the autopilot disconnection, the failure of the attempts to understand the situation and the de-structuring of crew cooperation fed on each other until the total loss of cognitive control of the situation. The underlying behavioral hypotheses in classifying the loss of airspeed information as 'major' were not validated in the context of this accident. Confirmation of this classification thus supposes additional work on operational feedback that would enable improvements, where required, in crew training, the ergonomics of information supplied to them and the design of procedures. The aeroplane went into a sustained stall, signaled by the stall warning and strong buffet. Despite these persistent symptoms, the crew never understood that they were stalling and consequently never applied a recovery manoeuvre. The combination of the ergonomics of the warning design, the conditions in which airline pilots are trained and exposed to stalls during their professional training and the process of recurrent training does not generate the expected behavior in any acceptable reliable way. In its current form, recognizing the stall warning, even associated with buffet, supposes that the crew accords a minimum level of 'legitimacy' to it. This then supposes sufficient previous experience of stalls, a minimum of cognitive availability and understanding of the situation, knowledge of the aeroplane (and its protection modes) and its flight physics. An examination of the current training for airline pilots does not, in general, provide convincing indications of the building and maintenance of the associated skills. More generally, the double failure of the planned procedural responses shows the limits of the current safety model. When crew action is expected, it is always supposed that they will be capable of initial control of the flight path and of a rapid diagnosis that will allow them to identify the correct entry in the dictionary of procedures. A crew can be faced with an unexpected situation leading to a momentary but profound loss of comprehension. If, in this case, the supposed capacity for initial mastery and then diagnosis is lost, the safety model is then in 'common failure mode'. During this event, the initial inability to master the flight path also made it impossible to understand the situation and to access the planned solution.
Thus, the accident resulted from the following succession of events:
- Temporary inconsistency between the airspeed measurements, likely following the obstruction of the Pitot probes by ice crystals that, in particular, caused the autopilot disconnection and the reconfiguration to alternate law;
- Inappropriate control inputs that destabilized the flight path;
- The lack of any link by the crew between the loss of indicated speeds called out and the appropriate procedure;
- The late identification by the PNF of the deviation from the flight path and the insufficient correction applied by the PF;
- The crew not identifying the approach to stall, their lack of immediate response and the exit from the flight envelope;
- The crew’s failure to diagnose the stall situation and consequently a lack of inputs that would have made it possible to recover from it.
These events can be explained by a combination of the following factors:
- The feedback mechanisms on the part of all those involved that made it impossible:
* To identify the repeated non-application of the loss of airspeed information procedure and to remedy this,
* To ensure that the risk model for crews in cruise included icing of the Pitot probes and its consequences;
- The absence of any training, at high altitude, in manual aeroplane handling and in the procedure for 'Vol avec IAS douteuse';
- Task-sharing that was weakened by:
* Incomprehension of the situation when the autopilot disconnection occurred,
* Poor management of the startle effect that generated a highly charged emotional factor for the two copilots;
- The lack of a clear display in the cockpit of the airspeed inconsistencies identified by the computers;
- The crew not taking into account the stall warning, which could have been due to:
* A failure to identify the aural warning, due to low exposure time in training to stall phenomena, stall warnings and buffet,
* The appearance at the beginning of the event of transient warnings that could be considered as spurious,
* The absence of any visual information to confirm the approach-to-stall after the loss of the limit speeds,
* The possible confusion with an overspeed situation in which buffet is also considered as a symptom,
* Flight Director indications that may led the crew to believe that their actions were appropriate, even though they were not,
* The difficulty in recognizing and understanding the implications of a reconfiguration in alternate law with no angle of attack protection.
Final Report:

Crash of a Boeing 737-2K9 in Guadalajara

Date & Time: Apr 27, 2009 at 1800 LT
Type of aircraft:
Operator:
Registration:
XA-MAF
Survivors:
Yes
Schedule:
Cancún – Guadalajara
MSN:
22505/815
YOM:
1981
Flight number:
GMT585
Country:
Crew on board:
8
Crew fatalities:
Pax on board:
108
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On approach to Guadalajara-Miguel Hidalgo y Costilla Airport, the pilots encountered technical problems with the landing gear and elected to perform a low pass in front of the tower. ATC confirmed that the landing gear were not fully deployed and locked. The captain decided to perform a wheels up landing. After touchdown on runway 28, the aircraft slid for few dozen metres before coming to rest. The left engine was destroyed by fire and the aircraft was damaged beyond repair. All 116 occupants escaped uninjured.

Crash of a McDonnell Douglas MD-90-30 in Jakarta

Date & Time: Mar 9, 2009 at 1535 LT
Type of aircraft:
Operator:
Registration:
PK-LIL
Survivors:
Yes
Schedule:
Ujung Pandang - Jakarta
MSN:
53573/2182
YOM:
1997
Flight number:
LNI793
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
166
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
25000
Captain / Total hours on type:
5000.00
Copilot / Total flying hours:
5000
Copilot / Total hours on type:
800
Aircraft flight hours:
18695
Aircraft flight cycles:
14507
Circumstances:
Lion Mentari Airline (Lion Air) as flight number LNI-793, departed from Sultan Hasanuddin Airport (WAAA), Makassar, Ujung Pandang, Sulawesi at 0636 UTC for Soekarno-Hatta International Airport (WIII), Jakarta. The estimated flight hour from Makassar to Jakarta was 2 hours. The crew consisted of two pilots and four flight attendants. There were 166 adult passengers. The copilot was the pilot flying for the sector, and the pilot in command (PIC) was the support/monitoring pilot. During the approach to runway 25L at Jakarta, the weather at the airport was reported as wind direction 200 degrees, wind speed 20 knots, visibility 1,000 meters, and rain. The PIC reported that he decided to take over control from the copilot. The PIC later reported that he had the runway in sight passing through 1,000 feet on descent, and he disengaged the autopilot at 400 feet. At about 50 feet the aircraft drifted to the right and the PIC initiated corrective action to regain the centreline. The aircraft touched down to the left of the runway 25L centerline and then commenced to drift to the right. The PIC reported that he immediately commenced corrective action by using thrust reverser, but the aircraft increasingly crabbed along the runway with the tail to the right of runway heading. The investigation subsequently found that the right thrust reverser was deployed, but left thrust reverser was not deployed. The aircraft stopped at 0835 on the right side of the runway 25L, 1,095 meters from the departure end of the runway on a heading of 152 degrees; 90 degrees to the runway 25L track. The main landing gear wheels collapsed, and still attached to the aircraft, were on the shoulder of the runway and the nose wheel was on the runway. The passengers and crew disembarked via the front right escape slide and right emergency exit windows. None of the occupants were injured
Probable cause:
The aircraft was not stabilized approach at 100 feet above the runway.
Final Report:

Crash of a Boeing 737-8F2 in Amsterdam: 9 killed

Date & Time: Feb 25, 2009 at 1026 LT
Type of aircraft:
Operator:
Registration:
TC-JGE
Survivors:
Yes
Schedule:
Istanbul - Amsterdam
MSN:
29789/1065
YOM:
2002
Flight number:
TK1951
Country:
Region:
Crew on board:
7
Crew fatalities:
Pax on board:
128
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total flying hours:
17000
Captain / Total hours on type:
10885.00
Copilot / Total flying hours:
4146
Copilot / Total hours on type:
44
Circumstances:
Turkish Airlines Flight 1951, a Boeing 737-800, departed Istanbul-Atatürk International Airport (IST) for a flight to Amsterdam-Schiphol International Airport (AMS), The Netherlands. The flight crew consisted of three pilots: a line training captain who occupied the left seat, a first officer under line training in the right seat and an additional first officer who occupied the flight deck jump seat. The first officer under line training was the pilot flying. The en route part of the flight was uneventful. The flight was descending for Schiphol and passed overhead Flevoland at about 8500 ft. At that time the aural landing gear warning sounded. The aircraft continued and was then directed by Air Traffic Control towards runway 18R for an ILS approach and landing. The standard procedure for runway 18R prescribes that the aircraft is lined up at least 8 NM from the runway threshold at an altitude of 2000 feet. The glidepath is then approached and intercepted from below. Lining up at a distance between 5 and 8 NM is allowed when permitted by ATC. Flight 1951 was vectored for a line up at approximately 6 NM at an altitude of 2000 feet. The glide slope was now approached from above. The crew performed the approach with one of the two autopilot and autothrottle engaged. The landing gear was selected down and flaps 15 were set. While descending through 1950 feet, the radio altimeter value suddenly changed to -8 feet. And again the aural landing gear warning sounded. This could be seen on the captain’s (left-hand) primary flight display. The first officer’s (right-hand) primary flight display, by contrast, indicated the correct height, as provided by the right-hand system. The left hand radio altimeter system, however, categorised the erroneous altitude reading as a correct one, and did not record any error. In turn, this meant that it was the erroneous altitude reading that was used by various aircraft systems, including the autothrottle. The crew were unaware of this, and could not have known about it. The manuals for use during the flight did not contain any procedures for errors in the radio altimeter system. In addition, the training that the pilots had undergone did not include any detailed system information that would have allowed them to understand the significance of the problem. When the aircraft started to follow the glidepath because of the incorrect altitude reading, the autothrottle moved into the ‘retard flare’ mode. This mode is normally only activated in the final phase of the landing, below 27 feet. This was possible because the other preconditions had also been met, including flaps at (minimum) position 15. The thrust from both engines was accordingly reduced to a minimum value (approach idle). This mode was shown on the primary flight displays as ‘RETARD’. However, the right-hand autopilot, which was activated, was receiving the correct altitude from the right-hand radio altimeter system. Thus the autopilot attempted to keep the aircraft flying on the glide path for as long as possible. This meant that the aircraft’s nose continued to rise, creating an increasing angle of attack of the wings. This was necessary in order to maintain the same lift as the airspeed reduced. In the first instance, the pilots’ only indication that the autothrottle would no longer maintain the pre-selected speed of 144 knots was the RETARD display. When the speed fell below this value at a height of 750 feet, they would have been able to see this on the airspeed indicator on the primary flight displays. When subsequently, the airspeed reached 126 knots, the frame of the airspeed indicator also changed colour and started to flash. The artificial horizon also showed that the nose attitude of the aircraft was becoming far too high. The cockpit crew did not respond to these indications and warnings. The reduction in speed and excessively high pitch attitude of the aircraft were not recognised until the approach to stall warning (stick shaker) went off at an altitude of 460 feet. The first officer responded immediately to the stick shaker by pushing the control column forward and also pushing the throttle levers forward. The captain however, also responded to the stick shaker commencing by taking over control. Assumingly the result of this was that the first officer’s selection of thrust was interrupted. The result of this was that the autothrottle, which was not yet switched off, immediately pulled the throttle levers back again to the position where the engines were not providing any significant thrust. Once the captain had taken over control, the autothrottle was disconnected, but no thrust was selected at that point. Nine seconds after the commencement of the first approach to stall warning, the throttle levers were pushed fully forward, but at that point the aircraft had already stalled and the height remaining, of about 350 feet, was insufficient for a recovery. According to the last recorded data of the digital flight data recorder the aircraft was in a 22° ANU and 10° Left Wing Down (LWD) position at the moment of impact. The airplane impacted farmland. The horizontal stabilizer and both main landing gear legs were separated from the aircraft and located near the initial impact point. The left and right engines had detached from the aircraft. The aft fuselage, with vertical stabilizer, was broken circumferentially forward of the aft passenger doors and had sustained significant damage. The fuselage had ruptured at the right side forward of the wings. The forward fuselage section, which contained the cockpit and seat rows 1 to 7, had been significantly disrupted. The rear fuselage section was broken circumferentially around row 28.
Probable cause:
During the accident flight, while executing the approach by means of the instrument landing system with the right autopilot engaged, the left radio altimeter system showed an incorrect height of -8 feet on the left primary flight display. This incorrect value of -8 feet resulted in activation of the ‘retard flare’ mode of the auto-throttle, whereby the thrust of both engines was reduced to a minimal value (approach idle) in preparation for the last phase of the landing. Due to the approach heading and altitude provided to the crew by air traffic control, the localiser signal was intercepted at 5.5 NM from the runway threshold with the result that the glide slope had to be intercepted from above. This obscured the fact that the auto-throttle had entered the retard flare mode. In addition, it increased the crew’s workload. When the aircraft passed 1000 feet height, the approach was not stabilized so the crew should have initiated a go around. The right autopilot (using data from the right radio altimeter) followed the glide slope signal. As the airspeed continued to drop, the aircraft’s pitch attitude kept increasing. The crew failed to recognize the airspeed decay and the pitch increase until the moment the stick shaker was activated. Subsequently the approach to stall recovery procedure was not executed properly, causing the aircraft to stall and crash.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in Nome

Date & Time: Feb 19, 2009 at 1812 LT
Operator:
Registration:
N41185
Survivors:
Yes
Schedule:
Brevig Mission – Nome
MSN:
31-8553001
YOM:
1985
Flight number:
FTA8218
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
24850
Captain / Total hours on type:
7500.00
Aircraft flight hours:
10928
Circumstances:
The scheduled commuter flight was about 10 miles north of the destination airport, operating under a special visual-flight-rules clearance, and descending for landing in instrument meteorological conditions. According to the pilot he started a gradual descent over an area of featureless, snow-covered, down-sloping terrain in whiteout and flat light conditions. During the descent a localized snow shower momentarily reduced the pilot’s forward visibility and he was unable to discern any terrain features. The airplane collided with terrain in an all-white snow/ice field and sustained substantial damage. At the time of the accident the destination airport was reporting visibility of 1.5 statute miles in light snow and mist, broken layers at 900 and 1,600 feet, and 3,200 feet overcast, with a temperature and dew point of 25 degrees Fahrenheit. The pilot reported that there were no pre accident mechanical problems with the airplane and that the accident could have been avoided if the flight had been operated under an instrument-flight-rules flight plan.
Probable cause:
The pilot's continued flight into adverse weather and his failure to maintain clearance from terrain while on approach in flat light conditions.
Final Report:

Crash of an Avro RJ100 in London-City

Date & Time: Feb 13, 2009 at 2040 LT
Type of aircraft:
Operator:
Registration:
G-BXAR
Survivors:
Yes
Schedule:
Amsterdam - London-City
MSN:
E3298
YOM:
1997
Flight number:
BA8456
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
67
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4730
Captain / Total hours on type:
2402.00
Circumstances:
Following a normal touchdown, the fracture of the nose landing gear main fitting allowed the nose gear to collapse rearwards and penetrate the lower fuselage, causing significant damage to the equipment bay and the battery to become disconnected. The penetration of the fuselage allowed smoke and fumes produced by the consequent release of hydraulic fluid to enter the cockpit and passenger cabin. With the battery disconnected and after the engines were shut down, all power to the aircraft PA systems was lost and the remote cockpit door release mechanism became inoperative. No pre-accident defects were identified with the manual cockpit door release mechanism or the PA system.
Probable cause:
The nose landing gear main fitting failed following the formation of multiple fatigue cracks within the upper section of the inner bore, originating at the base of machining grooves in the bore surface. These had formed because the improved surface finish, introduced by SB 146-32-150, had not been properly embodied at previous overhaul by Messier Services Inc, despite their overhaul records showing its incorporation. The operator had been in full compliance with the Service Bulletin relating to regular inspection of the main fitting, and embodiment of SB 146-32-150 at overhaul removed the requirement for these inspections by the operator.
Final Report:

Crash of a De Havilland Dash-8-Q402 in Buffalo: 50 killed

Date & Time: Feb 12, 2009 at 2217 LT
Operator:
Registration:
N200WQ
Survivors:
No
Site:
Schedule:
Newark - Buffalo
MSN:
4200
YOM:
2008
Flight number:
CO3407
Crew on board:
4
Crew fatalities:
Pax on board:
45
Pax fatalities:
Other fatalities:
Total fatalities:
50
Captain / Total flying hours:
3379
Captain / Total hours on type:
111.00
Copilot / Total flying hours:
2244
Copilot / Total hours on type:
774
Aircraft flight hours:
1819
Aircraft flight cycles:
1809
Circumstances:
On February 12, 2009, about 2217 eastern standard time, a Colgan Air, Inc., Bombardier DHC-8-400, N200WQ, operating as Continental Connection flight 3407, was on an instrument approach to Buffalo-Niagara International Airport, Buffalo, New York, when it crashed into a residence in Clarence Center, New York, about 5 nautical miles northeast of the airport. The 2 pilots, 2 flight attendants, and 45 passengers aboard the airplane were killed, one person on the ground was killed, and the airplane was destroyed by impact forces and a post crash fire. The flight was operating under the provisions of 14 Code of Federal Regulations Part 121. Night visual meteorological conditions prevailed at the time of the accident.
Probable cause:
The captain’s inappropriate response to the activation of the stick shaker, which led to an aerodynamic stall from which the airplane did not recover.
Contributing to the accident were:
1) The flight crew’s failure to monitor airspeed in relation to the rising position of the low speed cue,
2) The flight crew’s failure to adhere to sterile cockpit procedures,
3) The captain’s failure to effectively manage the flight,
4) Colgan Air’s inadequate procedures for airspeed selection and management during approaches in icing conditions.
Final Report:

Crash of a BAe 3201 Jetstream 31 in Heraklion

Date & Time: Feb 12, 2009 at 1723 LT
Type of aircraft:
Operator:
Registration:
SX-SKY
Survivors:
Yes
Schedule:
Rhodes – Heraklion
MSN:
829
YOM:
1988
Flight number:
SEH103
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
15
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
24000
Captain / Total hours on type:
570.00
Copilot / Total flying hours:
1800
Copilot / Total hours on type:
250
Aircraft flight hours:
13222
Aircraft flight cycles:
15349
Circumstances:
Flight SEH102/103 of 12 February 2009 was a scheduled passenger carrying flight performing the route Heraklion – Rhodes – Heraklion. The crew that was going to perform the flight reported for duty at 16:00 h. The aircraft had earlier on the same day performed, with a different flight crew, four routes (Heraklion – Rhodes – Heraklion and Heraklion – Samos – Heraklion), without any problems being reported. Nothing had been observed during the pre-flight check. The aircraft departed Heraklion at 16:55 h and landed at Rhodes at 17:35 h without incident. At 18:30 h the aircraft departed Rhodes for Heraklion, carrying three crew members and 15 passengers. The pilot flying (PF) this particular sector was the Pilot in Command (PIC). At a distance of 30 nm from Heraklion and at a altitude of 7700 ft on its descent to 3000 ft, the crew informed the Air Traffic Control that it had the runway in sight and requested and was granted clearance to perform a visual approach. The aircraft, fully configured for landing from a distance of 7nm, approached the airport for landing at runway 27. The wind information provided by the Air Traffic Control was 18 kt – 25 kt, from 210°. While approaching the runway, the PF asked the First Officer (FO) to check the angle of descent based on the APAPIs’ of the runway. The FO confirmed the correct angle of descent, saying “one white, one red”. The aircraft crossed the threshold with a speed of 112 kt and after flaring the PF reduced speed to Flight Idle and touched down with a speed of 86 kt. As the speed was being gradually reduced, the PF had difficulty with controlling the aircraft along its longitudinal axis and noticing that the aircraft was leaning somewhat to the right, reported to the FO that “the gear has broken”. Immediately afterwards, the blades of the right propeller of the aircraft struck the runway. As the aircraft continued to move with the left main landing gear wheel operating normally and the collapsed right main landing gear, folded backwards under the wing, being dragged along the runway, the crew stopped the engines, reported to the Airport Control Tower that the right landing gear had broken and requested evacuation. The aircraft stopped in the runway with its nose wheel at 4.6 m to the right of the center line, at a distance of 930 m from the point of the propeller’s first contact with the runway. Immediately afterwards the PF ordered the cabin crew to open the cabin door and evacuated the aircraft, and the FO, who observed some fuel leaking from the right engine, switched off the electrical systems and requested through the Airport Control Tower that the fire trucks, which were on their way, to throw foam on the right wing to prevent any fire being started. The passengers disembarked from the left aft door without any problems with the assistance of the cabin crew, while the fire trucks covered the right wing with foam as a preventive measure. The airport, applying the standing procedures, removed the aircraft and released the runway for operation at 22:30 h. During the period of time that runway 09/27 remained out of operation, two flights approaching the airport for landing were diverted to Chania Airport, and the departures of another three flights were delayed.
Probable cause:
CONCLUSIONS
Findings:
- The flight crew met all the requirements for the performance of the flight.
- The aircraft was airworthy.
- The aircraft’s landing gears have a life of 50,000 cycles (landings) and the interval between two overhauls is six years or 10,000 cycles, whichever comes sooner.
- The fractured landing gear had completed 23,940 cycles since new and had been subjected to an overhaul on 17.09.08. Since then and as of the date of the accident it had completed 148 cycles.
- The aircraft manufacturer had issued an SB, and the UK Civil Aviation Authority an AD, asking for tests and inspection applicable to Region “A” of the main landing gear cylinders.
- Said AD had been carried out without findings in the course of the landing gear overhaul of 17.09.08 by an EASA-Part 145 approved maintenance organization.
- On 02.01.09 a visual inspection of Region “A” of the main landing gear cylinders was carried out by the aircraft operator’s maintenance organization, in accordance with Part B of the SB, again without findings.
- On 07.02.09 and in the morning of 12.02.09 the aircraft made ‘heavy’ landings considering that vertical acceleration values of 2.8 g and 2.5 g, respectively, had been recorded. None of these landings had been recorded in the aircraft’s log in order to trigger the inspection prescribed in the aircraft’s maintenance manual after a ‘heavy’ landing.
- According to the technical examination of the fractured parts, the first crack developed in Region “A” (fracture surface “A2-B2”) increasing the loading upon the cylinder material surrounding the threaded fasteners, sites of stress concentration. The second and third cracks then initiated at the site of stress concentration and propagated within the cylinder to form fracture surfaces “A1” - “B1” in the region surrounding the threaded fasteners. The cracks and the fracture resulted from the ductile overload of the undercarriage cylinder which is likely to have resulted from a ‘heavy’ landing made by the aircraft.
Probable Causes:
Landing gear cylinder failure because of ductile overload resulting from a ‘heavy’ landing made by the aircraft.
Final Report:

Crash of a Fokker 100 in Tehran

Date & Time: Jan 19, 2009 at 1701 LT
Type of aircraft:
Operator:
Registration:
EP-CFN
Survivors:
Yes
Schedule:
Ardabil - Tehran
MSN:
11423
YOM:
1993
Country:
Region:
Crew on board:
8
Crew fatalities:
Pax on board:
106
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
After landing on runway 29L at Tehran-Mehrabad Airport, the right main gear collapsed. The aircraft veered off runway to the right and came to rest. All 114 occupants were uninjured and the aircraft was damaged beyond repair.
Probable cause:
Failure of the right main gear upon landing for unknown reasons.