Crash of a Boeing 737-8BK in Georgetown

Date & Time: Jul 30, 2011 at 0132 LT
Type of aircraft:
Operator:
Registration:
9Y-PBM
Survivors:
Yes
Schedule:
New York - Port of Spain - Georgetown
MSN:
29635/2326
YOM:
2007
Flight number:
BW523
Country:
Crew on board:
6
Crew fatalities:
Pax on board:
157
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
9600
Captain / Total hours on type:
5000.00
Copilot / Total flying hours:
1400
Copilot / Total hours on type:
350
Aircraft flight hours:
14861
Circumstances:
The flight originated in New York as BW 523, and made a passenger and fuel stop in Port-of-Spain, Trinidad where there was also a change of crew comprising two pilots and four flight attendants before proceeding to Georgetown, Guyana. The flight departed Piarco at 04:36UTC. The aircraft proceeded to Georgetown from Port of Spain at Flight Level (FL) 330, was given descent clearance and was cleared for an RNAV (GPS) approach to RWY 06, landing at 05:32 UTC. There were no reported anomalies in the en-route profile, although during the transition from cruise to approach to RWY 06 the aircraft deviated to avoid some thunderstorm cells north and east of the Airport. The reported visibility was 9,000m. Light rain was encountered during the approach. The pilot reported that after visual contact was made and after crossing the Final Approach Fix (FAF), he disengaged the auto pilot and configured the aircraft for landing. The Flight Data Recorder (FDR) indicated that the flight was normal until the aircraft was approaching the runway. Even before the aircraft was over the threshold, the captain commented that he was not landing here. As the flight continued over the runway, comments on the Cockpit Voice Recorder (CVR), revealed that the captain indicated to the First Officer (FO) that the aircraft was not touching down. A go-around call was made by the Captain and acknowledged by the First Officer, however three seconds elapsed and the aircraft subsequently touched down approximately 4700ft from the threshold of RWY06, leaving just over 2700 feet of runway surface remaining. Upon touchdown, brake pressure was gradually increased and maximum brake pressure of 3000psi was not achieved until the aircraft was 250ft from the end of the runway or 450ft from the end of the paved area. The ground spoilers were extended on touchdown. The thrust reversers were partially deployed after touchdown. The aircraft did not stop and overran the runway. It then assumed a downward trajectory followed by a loud impact.
Probable cause:
The probable cause of the accident was that the aircraft touched down approximately 4,700 feet beyond the runway threshold, some 2,700 feet from the end of the runway, as a result of the Captain maintaining excess power during the flare, and upon touching down, failure to utilize the aircraft’s full deceleration capability, resulted in the aircraft overrunning the remaining runway and fracturing the fuselage.
Contributory Factors:
The Flight Crew’s indecision as to the execution of a go-around, failure to execute a go-around after the aircraft floated some distance down the runway and their diminished situational awareness contributed to the accident.
Final Report:

Ground fire of a Boeing 777-266ER in Cairo

Date & Time: Jul 29, 2011 at 0911 LT
Type of aircraft:
Operator:
Registration:
SU-GBP
Flight Phase:
Survivors:
Yes
Schedule:
Cairo - Jeddah
MSN:
28423/71
YOM:
1997
Flight number:
MS667
Country:
Region:
Crew on board:
10
Crew fatalities:
Pax on board:
307
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
16982
Captain / Total hours on type:
5314.00
Copilot / Total flying hours:
2247
Copilot / Total hours on type:
198
Aircraft flight hours:
48281
Aircraft flight cycles:
11448
Circumstances:
On July 29, 2011, the said Boeing 777-200, Egyptian registration SU-GBP, operated by EgyptAir, arrived from Madina, Saudi Arabia (Flight No 678) and stopped at Gate F7, terminal 3, Cairo international airport almost at 0500 UTC time. Necessary maintenance actions (After Landing Check ALC, Transit Check) have been performed by EgyptAir engineers and technicians, to prepare the aircraft for the following scheduled flight (Cairo/Jeddah, scheduled at 0730 UTC, same day 29 July 2011, flight number 667). The cockpit crew (Captain and F/O) for the event flight (Cairo/Jeddah), started the cockpit preparation including checking the cockpit crew oxygen system as per normal procedures. The F/O reported that the oxygen pressure was within normal range (730 psi). At almost 0711 UTC, and while waiting for the last passengers to board the aircraft, the F/O officer reported that a pop, hissing sound originating from the right side of his seat was heard, associated with fire and smoke coming from the right side console area below F/O window #3 (right hand lower portion of the cockpit area) [The aircraft was still preparing for departure at Gate F7, Terminal 3 at Cairo Airport at the time the crew detected the fire]. The Captain requested the F/O to leave the cockpit immediately and notify for cockpit fire. The captain used the cockpit fire extinguisher bottle located behind his seat in attempt to fight and extinguish the fire. The attempt was unsuccessful, the fire continued in the cockpit. The F/O left the cockpit, he asked the cabin crew to deplane all the passengers and crew from the aircraft, based on captain’s order. He moved to the stairs and then underneath the aircraft in attempt to find anyone with a radio unit but he could not. He returned to the service road in front of the aircraft and stopped one car and asked the person in the car to notify the fire department that the aircraft is burning on the stand F7 using his radio unit. The cabin crew deplaned the passengers using the two doors 1L and 2L. The passenger bridge was still connected to the entry doors that were used for deplaning. The first fire brigade arrived to the aircraft after three minutes. The fire was extinguished. Extinguishing actions and cooling of the aircraft were terminated at 0845 UTC (1045 Cairo local time). The aircraft experienced major damage resulting from the fire and smoke. Passengers deplaned safely, some (passengers, employees) suffered mild asphyxia caused by smoke inhalation. Passengers and crew were as follows: Passengers 307, Cockpit Crew 2, Cabin Crew 8.
Probable cause:
Probable causes for the accident can be reached through:
- Accurate and thorough reviewing of the factual information and the analysis sections
- Excluding the irrelevant probable causes included in the analysis section
Examination of the aircraft revealed that the fire originated near the first officer's oxygen mask supply tubing, which is located underneath the side console below the no. 3 right hand flight deck window. Oxygen from the flight crew oxygen system is suspected to have contributed to the fire's intensity and speed.
The cause of the fire could not be conclusively determined. It is not yet known whether the oxygen system breach occurred first, providing a flammable environment or whether the oxygen system breach occurred as a result of the fire.
Accident could be related to the following probable causes:
1. Electrical fault or short circuit resulted in electrical heating of flexible hoses in the flight crew oxygen system. (Electrical Short Circuits; contact between aircraft wiring and oxygen system components may be possible if multiple wire clamps are missing or fractured or if wires are incorrectly installed).
2. Exposure to Electrical Current
Final Report:

Crash of an ATR72-212 in Shannon

Date & Time: Jul 17, 2011 at 1021 LT
Type of aircraft:
Operator:
Registration:
EI-SLM
Survivors:
Yes
Schedule:
Manchester - Shannon
MSN:
413
YOM:
1994
Flight number:
EI3601
Location:
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
21
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2882
Captain / Total hours on type:
2444.00
Copilot / Total flying hours:
1678
Copilot / Total hours on type:
1351
Aircraft flight hours:
32617
Aircraft flight cycles:
37149
Circumstances:
The aircraft and crew commenced operations in EINN that morning, departing at 05.52 hrs and arriving at EGCC at 07.13 hrs. During the turnaround, fuel was uplifted and 21 passengers boarded. Using the flight number and call sign EI-3601 the scheduled passenger service departed EGCC at 07.47 hrs for EINN with an estimated flight time of one hour and nine minutes. En-route operations were normal and, in consultation with ATC, the aircraft descended and was cleared to self-position to DERAG2 for an Instrument Landing System (ILS) approach to RWY 24. At 09.08 hrs the aircraft commenced an approach to RWY 24 in strong and gusty crosswind conditions. Following a turbulent approach difficulty was experienced in landing the aircraft, which contacted the runway in a nose-down attitude and bounced. A go-around was performed and the aircraft was vectored for a second approach. During this second approach landing turbulence was again experienced. Following bounces the aircraft pitched nose down and contacted the runway heavily in a nose down attitude. The nose gear collapsed and the aircraft nose descended onto the runway. The aircraft sustained damage with directional control being lost. The aircraft came to rest at the junction of the runway and a taxiway. Following engine shutdown the forward Cabin Crew Member (CCM) advised the cockpit that there was no smoke and that the doors could be opened following which, an evacuation was commenced. Airport fire crews arrived on scene promptly and assisted passengers disembarking the aircraft. There were no injuries.
Probable cause:
Probable Cause:
1. Excessive approach speed and inadequate control of aircraft pitch during a crosswind landing in very blustery conditions.
Contributory Factors:
1. Confusing wording in the FCOM that led the crew to compute an excessive wind factor in the determination of Vapp.
2. Incorrect power handling technique while landing.
3. Inexperience of the pilot in command.
4. Inadequate information provided to flight crew regarding crosswind landing techniques.
Final Report:

Ground collision of an ATR72-202 in Warsaw

Date & Time: Jul 14, 2011 at 2230 LT
Type of aircraft:
Operator:
Registration:
SP-LFH
Flight Phase:
Survivors:
Yes
Schedule:
Wrocław – Warsaw
MSN:
478
YOM:
1995
Flight number:
ELO3850
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
33
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On 14 July, 2011 ATR 72 flight crew after landing at EPWA aerodrome received the clearance for taxiing to parking stand 41 via taxiways: "S", "O" and "M". When the airplane was on taxiway "M2", "Mulag" type tractor was moving by the service road, passing perpendicularly to taxiway “M2”. The tractor driver did not give the right of way to ATR 72 and the tractor collided with the airplane. As a result, the airplane and the tractor sustained substantial damages. The flight crew stopped the airplane and shut down the engines. Airport Fire Brigade and an ambulance were called. The tractor operator suffered some injuries and was taken to hospital. the airplane passengers and the flight crew did not suffer any injuries. The impact caused a fuel leakage from the airplane of 200 m2 in area, which was removed along with other elements of the damaged aircraft by the Airport Fire Brigade. The airplane and the "Mulag" tractor were withdrawn from the further service. During the accident there were adverse weather conditions at the airport - heavy rain and lightning which caused reduction in visibility.
Probable cause:
Inadequate observation of the Ground Movement Area by the “Mulag” tractor operator.
Contributing factors:
1. Heavy rain and lightning.
2. Light reflections on the aerodrome surface which hindered observation from the tractor cab.
3. Construction of the "Mulag” tractor cab, left side of which could partially or completely obscure silhouette of the airplane.
4. Short distance between a service road and taxiway "O2".
Final Report:

Crash of a Let L-410UVP-E20 in Recife: 16 killed

Date & Time: Jul 13, 2011 at 0654 LT
Type of aircraft:
Operator:
Registration:
PR-NOB
Flight Phase:
Survivors:
No
Schedule:
Recife - Natal - Mossoró
MSN:
92 27 22
YOM:
1992
Flight number:
NRA4896
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
14
Pax fatalities:
Other fatalities:
Total fatalities:
16
Captain / Total flying hours:
15457
Captain / Total hours on type:
957.00
Copilot / Total flying hours:
2404
Copilot / Total hours on type:
404
Aircraft flight hours:
2126
Aircraft flight cycles:
3033
Circumstances:
At 0650 local time, the aircraft departed from Recife-Guararapes Airport runway 18, destined for Natal, carrying 14passengers and two crewmembers on a regular public transportation flight. During the takeoff, after the aircraft passed over the departure end of the runway, the copilot informed that they would return for landing, preferably on runway 36, and requested a clear runway. The aircraft made a deviation to the left, out of the trajectory, passed over the coastline, and, then, at an altitude of approximately 400ft, started a turn to the right over the sea. After about 90º of turn, upon getting close to the coast line, the aircraft reverted the turn to the left, going farther away from the coast line. After a turn of approximately 270º, it leveled the wings and headed for the airport area. The copilot informed, while the aircraft was still over the sea, that they would make an emergency landing on the beach. Witnesses reported that, as the aircraft was crossing over the coast line, the left propeller seemed to be feathered and turning loosely. At 0654 local time, the aircraft crashed into the ground in an area without buildings, between Boa Viagem Avenue and Visconde de Jequitinhonha Avenue, at a distance of 1,740 meters from the runway 36 threshold. A raging post-impact fire occurred and all 16 occupants were killed.
Probable cause:
Human Factors
Medical Aspect
- Anxiety
The perception of danger especially by the first officer affected the communication between the pilots and may have inhibited a more assertive attitude, which could have led to an emergency landing on the beach, minimizing the consequences of the accident.
Psychological Aspect
- Attitude
Operational decisions during the emergency may have resulted from the high confidence level, that the captain had acquired in years of flying and experience in aviation, as well as the captain's resistance to accept opinions different to his own.
- Emotional state
According to CVR recordings there was a high level of anxiety and tension even before the abnormal situation. These components may have influenced the judgment of conditions affecting the operation of the aircraft.
- Decision making
The persistence to land on runway 36 during the emergency, even though the first officer recognized the conditions no longer permitted to reach the airport, reflects misjudgment of operational information present at the time.
- Signs of stress
The unexpected emergency at takeoff and the lack of preparation for dealing with it may have invoked a level of stress with the crew, that negatively affected the operational response.
Psychosocial Information
- Interpersonal relations
The historical differences between the two pilots possibly hindered the exchange of information and created a barrier to deal with the adverse situation.
- Dynamic team
The present diverging intentions of how to proceed clearly show cooperation and management issues in the cockpit. This prevented the choice of best alternative to achieve a safe emergency landing when there were no options left to reach the airport.
- Company Culture
The company was informally divided into two groups, whose interaction was impaired. It is possible that this problem of interaction continued into the cockpit management during the in flight emergency, with one pilot belonging to one and the other to the other group.
Organizational Information
- Education and Training
Deficiencies of training provided by the operator affected the performance of the crew, who had not been sufficiently prepared for the safe conduct of flight in case of emergency.
- Organizational culture
The actions taken by the company indicate informality, which resulted in incomplete operational training and attitudes that endangered the safety.
Operational Aspects
According to data from the flight recorder the rudder pedal inputs were inadequate to provide sufficient rudder deflection in order to compensate for asymmetric engine power.
The values of side slip reached as result of inadequate rudder pedal inputs penalized the performance of the aircraft preventing further climb or even maintaining altitude.
In the final phase of the flight, despite the airspeed decaying below Vmca, despite continuous stall warnings and despite calls by the first officer to not hold the nose up in order to not stall the captain continued pitch up control inputs until the aircraft reached 18 degrees nose up attitude and entered stall.
- Crew Coordination
The delay in retracting the landing gear after the first instruction by the captain, the instruction of the captain to feather the propeller when the propeller had already been feathered as well as the first officer's request the captain should initiate the turn back when the aircraft was already turning are indicative that the crew tasks and actions were not coordinated.
Emergency procedures provided in checklists were not executed and there was no consensus in the final moments of the flight, whether the best choice (least critical option) was to return to the runway or land on the beach.
- Oblivion
It is possible in response to the emergency and influenced by anxiety, that the crew may have forgotten to continue into the 3rd segment of the procedure provided for engine failure on takeoff at or above V1 while trying to return to the airfield shortly after completion of the 2nd segment while at 400ft.
- Pilot training
The lack of training of engine failures on takeoff at or above V1, similar as is recommended in the training program, led to an inadequate pilot response to the emergency. The pilots did not follow the recommended flight profile and did execute the checklist items to be carried out above 400 feet.
- Pilot decisions
The pilots assessed that the priority was to return to land in opposite direction of departure and began the turn back at 400 feet, which added to the difficulty of flying the aircraft. At 400 feet the aircraft maintained straight flight and a positive rate of climb requiring minor flight control inputs only, which would have favored the completion of the emergency check list items in accordance with recommendations by the training program.
After starting the turn the crew would needed to adjust all flight controls to maintain intended flight trajectory in addition to working the checklists, the turn thus increased workload. It is noteworthy that the remaining engine developed sufficient power to sustain flight.
- Supervision by Management
The supervision by management did not identify that the training program provided to pilots failed to address engine failure above V1 while still on the ground and airborne.
It was not identified that the software adopted by the company to dispatch aircraft used the maximum structural weight (6,600 kg) as maximum takeoff weight for departures from Recife.
On the day of the accident the aircraft was limited in takeoff weight due to ambient temperature. Due to the software error the aircraft took off with more than the maximum allowable takeoff weight degrading climb performance.
Mechanical Aspects
- Aircraft
Following the hypothesis that the fatigue process had already started when the turbine blade was still attached to the Russia made engine, the method used by the engine manufacturer for assessment to continue use of turbine blades was not able to ensure sufficient quality of the blade, that had been mounted into position 27 of the left hand engine's Gas Generator Turbine's disk.
- Aircraft Documentation
The documentation of the aircraft by the aircraft manufacturer translated into the English language did not support proper operation by having confusing texts with different content for the same items in separate documents as well as translation errors. This makes the documentation difficult to understand, which may have contributed to the failure to properly implement the engine failure checklists on takeoff after V1.
An especially concerning item is the "shutdown ABC (Auto Bank Control)", to be held at 200 feet height, the difference between handling instructed by the checklist and provided by the flight crew manual may have contributed to the non-performance by the pilots, aggravating performance of the aircraft.
Final Report:

Crash of an Antonov AN-24RV in Strezhevoy: 7 killed

Date & Time: Jul 11, 2011 at 1156 LT
Type of aircraft:
Operator:
Registration:
RA-47302
Survivors:
Yes
Schedule:
Tomsk - Surgut
MSN:
5 73 103 02
YOM:
1975
Flight number:
IK9007
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
33
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
4570
Captain / Total hours on type:
4064.00
Copilot / Total flying hours:
9476
Copilot / Total hours on type:
5100
Aircraft flight hours:
48489
Aircraft flight cycles:
32783
Circumstances:
The twin engine aircraft departed Tomsk Airport at 1010LT on a flight (callsign IK9007/SP5007) to Surgut, carrying 33 passengers and a crew of four. About an hour and 26 minutes into the flight, the left engine's 'chips in oil' warning light came on. About eight minutes later, a burning smell was noticed in the cockpit and the captain decided to divert to Nizhnevartovsk Airport. During the descent, the left engine caught fire. Its propeller was feathered and the crew decided to divert to Strezhevoy Airport. But as the fire could not be extinguished, the captain eventually attempted an emergency landing in the Ob River. Upon landing, the aircraft broke in two and came to rest in shallow water. Seven passengers were killed while all other occupants were rescued.
Probable cause:
The Interstate Aviation Committee (MAK) released their final report in Russian concluding the probable causes of the accident were:
The catastrophe of the AN-24 RA-47302 occurred when ditching became necessary due to a fire in the left hand engine's nacelle. The destruction of the aircraft and loss of life was caused by collision with underwater obstacles that the crew could not anticipate or avoid. The fire in the left hand engine nacelle was caused by the fracture of a centrifugal breather releasing an air-fuel emulsion into the engine compartment as well as a delayed reaction to shut the engine down by the crew following an magnetic chip detector indication together with indications of oil pressure fluctuations, a burning smell and a low oil pressure indication. A delay in indicating engine vibrations to the crew as result of degradation of the engine vibration sensoring equipment, most likely caused by changes of the rotor speed of the engine as result of the aft bearing failure of the compressor rotor and/or misalignment of the sensor, which probably influenced the decision of the crew to shut the engine down with a delay. Cause of the fracture of the centrifugal breather was the destruction of the impeller due to prolonged exposure to hot air-fuel emulsion due to the failure of the aft compressor rotor support bearing. It was not possible to determine the cause of the destruction of the aft compressor rotor support bearing due to significant secondary damage. Most likely the destruction was caused by misalignment such as:
- Incorrect assembly of support parts mating with the compressor rotor during on-condition engine repairs,
- Or deviations from required geometry of support parts mating with the compressor rotor.
Contributing factors were:
- Psychological unpreparedness of the captain to shut the engine down due to lack of experience with the aircraft on one engine inoperative
- Late detection of the fire and as a consequence late attempts to extinguish the fire, it was however not possible to establish why the fire was detected late due to lack of objective information about the performance of the fire alarm systems.
Final Report:

Crash of a Boeing 727-22 in Kisangani: 77 killed

Date & Time: Jul 8, 2011 at 1511 LT
Type of aircraft:
Operator:
Registration:
9Q-COP
Survivors:
Yes
Schedule:
Kinshasa - Kisangani - Goma
MSN:
18933/185
YOM:
1965
Flight number:
EO952
Region:
Crew on board:
7
Crew fatalities:
Pax on board:
108
Pax fatalities:
Other fatalities:
Total fatalities:
77
Captain / Total flying hours:
7000
Captain / Total hours on type:
5000.00
Aircraft flight hours:
52613
Circumstances:
Following an uneventful flight from Kinshasa, the crew started the descent to Kisangani-Bangoka Airport in poor weather conditions with low visibility due to heavy rain falls. On final approach, the pilot did not establish any visual contact with the runway but continued until the aircraft impacted ground some 1,000 metres short of runway 31. On impact, the aircraft went out of control, veered to the right, exploded and disintegrated in a wooded area located to the right of the approach path. The wreckage was found about 500 metres southeast from the runway 31 threshold. Five crew and 72 passengers were killed.
Probable cause:
In a preliminary report, DRC authorities pointed out the following factors:
- The flight crew misjudged weather conditions,
- The airline assigned unqualified/non-licensed crew to operate the Boeing 727-100 (the pilot's licence was not up to date),
- Tower controllers were not licensed (two ATC's did not have a proper licence and above legal age)
- Tower control staff was insufficient (six only for the complete roster),
- Tower controllers provided erroneous/false weather data to flying crew,
- The airport authority lacked security plans,
- Phonic records between tower control and crew were erased (destroyed) before the commission of inquiry can start any investigation.

Crash of a Cessna 208B Grand Caravan in Pukatawagan: 1 killed

Date & Time: Jul 4, 2011 at 1610 LT
Type of aircraft:
Operator:
Registration:
C-FMCB
Flight Phase:
Survivors:
Yes
Schedule:
Pukatawagan - The Pas
MSN:
208B-1114
YOM:
2005
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1900
Captain / Total hours on type:
400.00
Circumstances:
The Beaver Air Services Limited Partnership Cessna 208B (registration C-FMCB serial number 208B1114), operated by its general partner Missinippi Management Ltd (Missinippi Airways), was departing Pukatawagan, Manitoba, for The Pas/Grace Lake Airport, Manitoba. At approximately 1610 Central Daylight Time, the pilot began the takeoff roll from Runway 33. The aircraft did not become fully airborne, and the pilot rejected the takeoff. The pilot applied reverse propeller thrust and braking, but the aircraft departed the end of the runway and continued down an embankment into a ravine. A post-crash fire ensued. One of the passengers was fatally injured; the pilot and the 7 other passengers egressed from the aircraft with minor injuries. The aircraft was destroyed. The emergency locator transmitter did not activate.
Probable cause:
Findings as to Causes and Contributing Factors:
Runway conditions, the pilot's takeoff technique, and possible shifting wind conditions combined to reduce the rate of the aircraft's acceleration during the takeoff roll and prevented it from attaining takeoff airspeed. The pilot rejected the takeoff past the point from which a successful rejected takeoff could be completed within the available stopping distance. The steep drop-off and sharp slope reversal at the end of Runway 33 contributed to the occupant injuries and fuel system damage that in turn caused the fire. This complicated passenger evacuation and prevented the rescue of the injured passenger. The deceased passenger was not wearing the available shoulder harness. This contributed to the serious injuries received as a result of the impact when the aircraft reached the bottom of the ravine and ultimately to his death in the post-impact fire.
Findings as to Risk:
If pilots are not aware of the increased aerodynamic drag during takeoff while using soft-field takeoff techniques they may experience an unexpected reduction in takeoff performance. Incomplete passenger briefings or inattentive passengers increase the risk that they will be unable to carry out critical egress procedures during an aircraft evacuation. When data recordings are not available to an investigation, this may preclude the identification and communication of safety deficiencies to advance transportation safety. Although the runway at Pukatawagan and many other aerodromes are compliant with Aerodrome Standards and Recommended Practices (TP 312E), the topography of the terrain beyond the runway ends may increase the likelihood of damage to aircraft and injuries to crew and passengers in the event of an aircraft overrunning or landing short. TC's responses to TSB recommendations for action to reduce the risk of post-impact fires have been rated as Unsatisfactory. As a result, there is a continuing risk of post-impact fires in impact-survivable accidents involving these aircraft. The lack of accelerate stop distance information for aircraft impedes the crew's ability to plan the takeoff-reject point accurately.
Other finding:
Several anomalies were found in the engine's power control hardware. There was no indication that these anomalies contributed to the occurrence.
Final Report:

Crash of a Tupolev TU-134A-3 in Petrozavodsk: 47 killed

Date & Time: Jun 20, 2011 at 2340 LT
Type of aircraft:
Operator:
Registration:
RA-65691
Survivors:
Yes
Schedule:
Moscow - Petrozavodsk
MSN:
63195
YOM:
1980
Flight number:
CGI9605
Country:
Region:
Crew on board:
9
Crew fatalities:
Pax on board:
43
Pax fatalities:
Other fatalities:
Total fatalities:
47
Captain / Total flying hours:
8501
Captain / Total hours on type:
3158.00
Copilot / Total flying hours:
2846
Copilot / Total hours on type:
1099
Aircraft flight hours:
35591
Aircraft flight cycles:
20977
Circumstances:
Aircraft left Moscow-Domodedovo Airport in 2224LT for Petrozavodsk, Karelia. On final approach by night and fog reducing vertical visibility to 300 metres, crew descended too low without a visual contact was established with the runway lights. Aircraft descended below the MDA, hit an electric pole, crashed on a road and came to rest in a garden, 570 metres short of runway 02. Eight people were rescued as all other 44 occupants were killed. Flight was operated by RusAir on behalf of RusLine (flight 243). Russian FIFA's football referee Vladimir Pettaï was also killed in this accident. Two days later, a survivor died from his injuries. The weekend following the accident (five days and six days later), two survivors died from their injuries (burns).
Probable cause:
When the aircraft approached the airfield in weather below minimums for the aerodrome descending on autopilot at a fixed vertical speed, crew failed to decide to go around in absence of visual contact with approach lights and landmarks and permitted the aircraft to descend below minimum descent altitude, which led to impact with trees and the ground in controlled flight.
Following factors were considered as contirbutory:
- unsatisfactory crew resource management by the commander who effectively removed the first officer from the control loop in the final stages of the accident flight and who subordinated himself to the navigator showing increased activity however in the state of mild alcoholic intoxication.
- the navigator was in the state of mild alcoholic intoxication
- unjustified weather forecasts by height of cloud base, visibility and severe weather including fog as well as the non-conformity of weather data of Petrozavodsk Airport transmitted to the crew 30 and 10 minutes prior to estimated landing.
- Failure to use indications by the ADFs and other devices of the aircraft while using indications by an unapproved satellite navigation system KLN-90 in violation of flight manual supplements for the TU-134.
Final Report:

Crash of a Saab 340A near Prahuaniyeu: 22 killed

Date & Time: May 18, 2011 at 2050 LT
Type of aircraft:
Operator:
Registration:
LV-CEJ
Flight Phase:
Survivors:
No
Schedule:
Rosario – Córdoba – Mendoza – Neuquén – Comodoro Rivadavia
MSN:
25
YOM:
1985
Flight number:
OSL5428
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
19
Pax fatalities:
Other fatalities:
Total fatalities:
22
Captain / Total flying hours:
6133
Captain / Total hours on type:
2187.00
Copilot / Total flying hours:
1342
Copilot / Total hours on type:
288
Aircraft flight hours:
41422
Aircraft flight cycles:
44477
Circumstances:
On 18 May 2011, the pilot in command (PIC) and the crew - composed of the copilot (COP) and cabin crew members (CCM) - initiated the flight OSL5428 from Rosario International Airport (ROS) in the province of Santa Fe at 20:35, the final destination being the Comodoro Rivadavia International Airport (CRD), in the province of Chubut. The flight had scheduled intermediate stopovers at Córdoba International Airport (COR), Mendoza (MDZ), and Neuquén (NQN), according to the company's plans. The company designated aircraft Saab 340A, with registration number LV-CEJ, for the flight. After having made the intermediate stopovers in Córdoba (COR) and Mendoza (MDZ), the pilot landed the aircraft at the airport in Neuquén at 22:20. After refuelling and carrying out the planned dispatch, the crew and 19 passengers (18 adults and one minor) on board, prepared to make the last leg of the flight OSL5428, from Neuquén Airport (NQN) to the final destination: Comodoro Rivadavia International Airport (CRD). The flight took off at 23:05. After the take-off, the aircraft started to climb AWY T 105, to reach FL190, in accordance with the flight plan. After flying for 24 minutes, the pilot levelled the aircraft at 17,800 feet, and remained at this level for approximately 9 minutes. Due to the fact that the meteorological conditions at this level caused icing, the technical crew descended to FL (flight level) 140. Shifting to FL140 took five minutes. During this stage of the flight the icing conditions steadily worsened. By the time the aircraft had reached FL140, the icing conditions were severe. The aircraft flew for approximately two minutes with a straight and level flight attitude, increasing the accumulation of ice. Then the aircraft completely lost lift, which resulted in a loss of control, and the subsequent entry into abnormal flight attitude. The aircraft plunged towards the earth and impacted the ground, which resulted in a fire. Everyone on board perished and the aircraft was destroyed. The accident happened at night under IMC conditions.
Probable cause:
During a commercial, domestic passenger flight, while cruising, the crew lost control of the aircraft, which uncontrollably impacted the ground due to severe ice formation caused by the following factors:
- Entering an area with icing conditions without adequately monitoring the warning signals from the external environment (temperature, cloudiness, precipitation and ice accumulation) or the internal (speed, angle of attack), which allowed for prolonged operations in icing conditions to take place.
- Receiving a forecast for slight icing - given that the aircraft encountered sever icing conditions - which led to a lack of understanding regarding the specific meteorological danger.
- Inadequately evaluating the risks, which led to mitigating measures such as adequate briefing (distribution of tasks in the cockpit, review of the de-icing systems, limitations, use of power, use of autopilot, diversion strategy etc.) not being adopted.
- Levels of stress increasing, due to operations not having the expected effects, which led the crew to lose focus on other issues.
- Icing conditions that surpassed the aircraft's ice protection systems, which were certified for the aircraft (FAR 25 Appendix C).
- Inadequate use of speed, by maintaining the speed close to stall speed during flight in icing conditions.
- Inadequate use of the autopilot, by not selecting the IAS mode when flying in icing conditions.
- Partially carrying out the procedures established in the Flight Manual and the Operations Manual, when entering into areas with severe icing conditions.
- Realizing late that the aircraft had started to stall, because the buffeting that foretells a stall was confused with the vibrations that signify ice contamination on the propellers.
- Activation of the Stick Shaker and Stall Warning at a lower speed than expected in icing conditions.
- Using a stall recovery technique which prioritized the reduction of the angle of attack at the expense of altitude loss, and which was inappropriate for the flight conditions.
- The aileron flight controls reacting in an unusual manner when the aircraft lost control, probably due to the accumulation of ice in the surfaces of these, which made it impossible for the aircraft to recover. The increasingly stressful situation of the crew, which affected its operational decision-making.
Final Report: