Crash of a Cessna 411 in Fort Myers: 2 killed

Date & Time: Jan 25, 1977 at 1315 LT
Type of aircraft:
Registration:
N99JM
Flight Type:
Survivors:
No
Schedule:
Fort Myers - Fort Myers
MSN:
411-0093
YOM:
1965
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
6022
Captain / Total hours on type:
10.00
Circumstances:
The crew was completing a local training flight at Fort Myers Airport. During a simulated single engine approach, the crew initiated a steep turn when the airplane stalled and crashed close to the runway. The aircraft was destroyed by a post crash fire and both occupants were killed.
Probable cause:
Stall on final approach after the pilot failed to maintain flying speed. The following contributing factors were reported:
- Inadequate supervision of flight,
- Unfavorable wind conditions.
Final Report:

Crash of a Beechcraft C-45H Expeditor in Sonoma: 2 killed

Date & Time: Jan 16, 1977 at 0400 LT
Type of aircraft:
Registration:
N9497Z
Flight Type:
Survivors:
No
MSN:
AF-390
YOM:
1953
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1000
Circumstances:
While descending to Sonoma-Skypark by night and low clouds, the twin engine airplane stalled and crashed. Both occupants were killed. A witness at airport heard the aircraft flying low over hanger, turning south, engines surge then silence. At the time of the accident, the visibility was 2 miles or less.
Probable cause:
Stall during traffic pattern-circling after the pilot failed to maintain flying speed. The following contributing factors were reported:
- Attempted operation beyond experience/ability level,
- Exercised poor judgment,
- Low ceiling.
Final Report:

Crash of a Douglas DC-3-277C in Miami

Date & Time: Jan 15, 1977 at 1411 LT
Type of aircraft:
Operator:
Registration:
N73KW
Flight Phase:
Survivors:
Yes
Schedule:
Miami – Marathon – Key West
MSN:
2252
YOM:
1940
Flight number:
AAT220
Crew on board:
3
Crew fatalities:
Pax on board:
30
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
9250
Captain / Total hours on type:
2100.00
Circumstances:
After takeoff from Miami-Intl Airport, while climbing to a height of 100 feet, the left engine failed. The pilot stopped climbing and was attempting to land on the remaining wet runway when the airplane banked left, causing the left wing to drop and to struck the runway surface. Upon impact, the left main gear was torn off. The airplane went out of control, crash landed and came to rest. All 33 occupants were evacuated safely while the aircraft was damaged beyond repair.
Probable cause:
Engine failure during initial climb due to inadequate maintenance and inspection. The following contributing factors were reported:
- Failure of a cylinder assembly (disconnected),
- Failed to maintain flying speed,
- Delayed action in aborting takeoff,
- Improper emergency procedures,
- Low ceiling,
- Rain,
- Pilot stopped climbing and was attempting to land on the remaining wet runway.
Final Report:

Crash of a Douglas DC-8-62AF in Anchorage: 5 killed

Date & Time: Jan 13, 1977 at 0635 LT
Type of aircraft:
Operator:
Registration:
JA8054
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Moses Lake - Anchorage - Tokyo
MSN:
46148/553
YOM:
1971
Flight number:
JL8054
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
23252
Captain / Total hours on type:
4040.00
Copilot / Total flying hours:
1603
Copilot / Total hours on type:
1207
Aircraft flight hours:
19744
Circumstances:
On January 13, 1977, a Japan Air Line (JAL) McDonnell-Douglas DC-8-62F, JA 8054, operated as an international charter cargo flight from Moses Lake, Washington, U.S.A., to Tokyo, Japan. An en route stop and crew change were scheduled at Anchorage, Alaska. The aircraft arrived at Anchorage at 0503. The incoming flightcrew reported that the only weather they encountered en route was a layer of fog on the final approach at 800 feet, and that they did not encounter any precipitation or icing. The aircraft was serviced and a walk-around inspection was performed by JAL maintenance personnel and contract mechanics. The two contract mechanics stated that there was ice on the inlet guide vanes, the engine cowlings, and the engine bullet noses, but no ice was reported on the airfoil surfaces. The JAL personnel stated that they did not see any ice on the aircraft. One contract mechanic advised the JAL representative that the engine anti-icing system should be used by the next crew to clear the ice in the engine inlets. No maintenance was performed on the aircraft. The outbound flightcrew was wakened about 0330, left the hotel by taxi about 0430, and arrived at the JAL dispatch office about 0 0500. The taxicab driver who brought the outbound crew to the airport stated that he became concerned by the captain's actions in the taxi and called his dispatcher to report his impressions. He stated that the captain's movements were uncoordinated; that his face was flushed and his eyes were glazed; that his conversation was garbled and incoherent; that his movements were jerky and unstable; and that he had trouble getting out of the cab and had to steady himself on the car door. About 0450 the taxi dispatcher called the operations agent for the contract maintenance company and reported that one of her drivers had taken an "intoxicated" JAL captain to the airport. The operations agent stated that "...it seemed logical that JAL would detect anything unusual and act accordingly." He further stated that a 0620, he notified his line manager of the conversation with the taxi dispatcher and that "I felt that if the captain was intoxicated JAL OPS...or his first officer would have stopped the flight immediately." The JAL dispatch personnel and the inbound JAL crew stated that they noted nothing unusual about the outbound crew. The dispatch briefing proceeded smoothly and no significant questions were asked by the outbound crew. The outbound crew consisted of an American captain and a Japanese first officer and flight engineer. They went to the aircraft about 0515 and boarded the aircraft with the two cattle handlers. The driver of the crew car, a friend of the captain, stated that "...he was in good condition as far as way's I've seen him sometimes and I made that statement before I ever heard any rumors that he was supposedly drunk or had been partying or whatever." A review of the cockpit voice recorder (CVR) indicated that about 0603 the captain and first officer were checking the inputs to the inertial navigation system. They also checked the Automatic Terminal Information Service (ATIS) for local visibility, received their clearance, and began their prestart checklists about 0609. The weather on the ATIS report was in part: "...sky partially obscured, visibility one-quarter mile, fog...". The checklists were completed and the takeoff data reviewed. About 0615 the engines were started and the stickshaker (stall warning system) was tested. The after-start checklist was completed and the aircraft was cleared to taxi to runway 24L. During the taxi, the flight engineer requested and received permission from the captain to turn the engine anti-ice system on because of the ice on the inlet guide vanes. The flight controls and spoilers were checked while taxiing and the flaps were extended to 23°. The taxi checklist was completed and the takeoff data, the flap settings, and the trim settings were again reviewed. The captain, in response to the challenge "anti-ice, de-ice, and rain removal," said, "Ok, we will use engine anti-ice." The de-ice system was reported "off'' by the flight engineer. The captain briefed the crew on the takeoff and abort procedures he would use. He commented that the runway was slippery and he didn't think they would abort. The captain taxied the aircraft southeast on the ramp, past the terminal toward runway 24L. He stopped on the ramp after being instructed to hold short of runway 24R. After several communications with the controller, the aircraft taxied onto runway 24R, and reported ''...ready for takeoff." The tower advised the captain that he was on runway 24R which the captain contradicted. The controller then issued taxi instructions to get the aircraft to runway 24L. The captain made a 180° turn on runway 24R before he finally taxied to the taxiway which leads to the approach end of runway 24L. The crew again reported that they were ready for takeoff at 0633:37. Takeoff was initiated and at 0634:32 the captain called "maximum power". At 0634:50 the captain announced, "I have" and at 0634:52, "80" (knots) was called by the copilot. At 0635:10, "Vee one" was called by the copilot and at 0635:16 rotation was called and acknowledged by the captain. At 0635:19.5 the captain called "Ten degrees" and at 0635:21.4 the first officer called V2. At 0635:26.2 a sound similar to aircraft buffet was recorded. This sound became more frequent and continued until the sounds of impact. At 0635:32 the first officer called "Gear up" and at 0635:33 the flight engineer said "Too much speed (steep)".' At 0635: 38 the engineer called "stall" simultaneously the stickshaker sounded and continued until 0635:39.3, when impact was recorded. A witness near the departure end of the runway saw the aircraft climb to an estimated altitude of about 100 feet above the ground, veer to the left, and then slide '... out of the air." The aircraft was totally destroyed upon impact and all five occupants were killed as well as the 56 cows.
Probable cause:
The probable cause of the accident was a stall that resulted from the pilot's control inputs aggravated by airframe icing while the pilot was under the influence of alcohol. Contributing to the cause of this accident was the failure of the other flightcrew members to prevent the captain from attempting the flight.
Final Report:

Crash of a Mitsubishi MU-2B-10 Marquise in Rochester: 4 killed

Date & Time: Jan 7, 1977 at 1918 LT
Type of aircraft:
Operator:
Registration:
N854Q
Flight Phase:
Survivors:
No
Schedule:
Rochester - Lincoln
MSN:
107
YOM:
1968
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
8000
Captain / Total hours on type:
4000.00
Circumstances:
After a night takeoff from Rochester Airport in poor weather conditions, the airplane suffered an engine failure. The pilot lost control of the aircraft that crashed in flames past the runway end. The aircraft was destroyed and all four occupants were killed.
Probable cause:
Powerplant failure for undetermined reasons and stall spin during initial climb. The following contributing factors were reported:
- Improper operation of flight controls,
- Failed to maintain flying speed,
- Misused or failed to use flaps,
- Low ceiling,
- Snow and blowing snow,
- Visibility 1/2 mile or less,
- Flaps full down.
Final Report:

Crash of a Learjet 23 in Flint: 2 killed

Date & Time: Jan 6, 1977 at 1912 LT
Type of aircraft:
Operator:
Registration:
N332PC
Flight Type:
Survivors:
No
Schedule:
Detroit - Flint
MSN:
23-056
YOM:
1965
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
18320
Captain / Total hours on type:
1648.00
Circumstances:
The approach to Flint-Bishop Airport runway 27 was completed in poor weather conditions with limited visibility due to snow falls. On final, the airplane stalled then rolled to the right to an angle of 45° and crashed in flames. The aircraft was destroyed and both pilots were killed. They were completing a cargo flight from Detroit-Willow Run (Ypsilanti) Airport.
Probable cause:
Stall on final approach after the crew failed to maintain flying speed. The following contributing factors were reported:
- Failed to initiate go-around,
- Improper operation of flight controls,
- ATC issued improper or conflicting instructions,
- Lack of familiarity with aircraft,
- Poorly planned approach,
- Pilot had limited recent jet experience,
- Vectored and cleared for ILS back course 3NM southeast of middle marker.
Final Report:

Crash of a Learjet 24B near Palm Springs: 4 killed

Date & Time: Jan 6, 1977 at 1700 LT
Type of aircraft:
Operator:
Registration:
N12MK
Flight Phase:
Survivors:
No
Site:
Schedule:
Palm Springs - Las Vegas
MSN:
24-192
YOM:
1969
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
4150
Captain / Total hours on type:
532.00
Circumstances:
Shortly after takeoff from Palm Springs Airport, while climbing by night at an altitude of 9,700 feet, the airplane struck a mountain located in the San Gorgonio Wilderness of the San Bernardino Mountains, about 22 miles northwest of Palm Springs. Due to very poor weather conditions, rescuers were able to reach the crash site three days later only. The aircraft struck the ground at a speed of 325 knots and disintegrated on impact. All four occupants were killed.
Crew:
Donald J. Weier,
Jerald Wayne Foley.
Passengers:
Dolly Sinatra, Frank Sinatra's mother,
Ann Carbone.
Probable cause:
Controlled flight into terrain during climb to cruise after the crew misunderstood ATC instructions. The following contributing factors were reported:
- Lack of visibility,
- High obstructions,
- Crew misinterpreted IFR clearance and ATC instructions,
- ATC failed to detect deviation from route.
Final Report:

Crash of a Cessna 401 off Tampa

Date & Time: Dec 31, 1976 at 1156 LT
Type of aircraft:
Operator:
Registration:
N111TV
Flight Type:
Survivors:
Yes
Schedule:
Tampa - Tampa
MSN:
401-0158
YOM:
1968
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
437
Captain / Total hours on type:
129.00
Circumstances:
The twin engine airplane departed Tampa Airport in the morning for a local pleasure flight. On final approach to Tampa Airport, the pilot failed to extend the landing gear. Upon landing, the engine's propeller struck the runway surface. The pilot initiated a go-around but unable to maintain altitude, the aircraft lost height and crashed into Tampa Bay. All six occupants were rescued with minor injuries and the aircraft was lost.
Probable cause:
Wheels-up landing and controlled collision with water during go-around manoeuvre. The following contributing factors were reported:
- The pilot failed to extend landing gear on approach,
- Un maintain altitude during go-around due to prop damages.
Final Report:

Crash of a Cessna 411 in Berz-Macomb: 2 killed

Date & Time: Dec 29, 1976 at 1540 LT
Type of aircraft:
Operator:
Registration:
N411EF
Flight Type:
Survivors:
No
MSN:
411-0081
YOM:
1965
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
500
Circumstances:
While approaching Berz-Macomb Airport, the right engine failed. The pilot lost control of the airplane that entered an uncontrolled descent and crashed. Both occupants were killed.
Probable cause:
Engine failure and uncontrolled descent on final approach due to valve assemblies failure. The following contributing factors were reported:
- Material failure,
- Attempted operation beyond experience/ability level,
- Improper in-flight decisions,
- Failed to follow approved procedures,
- Improper emergency procedures,
- Partial loss of power on one engine,
- Forced landing off airport on land,
- 6th exhaust valve guide,
- Feathered engine capable of producing power,
- Not multi engine rated.
Final Report:

Crash of a Beechcraft D18 Mk. 3TM in Cairo

Date & Time: Dec 28, 1976 at 0206 LT
Type of aircraft:
Registration:
N3128B
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Cairo - Cleveland
MSN:
A-776
YOM:
1952
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8700
Captain / Total hours on type:
1500.00
Circumstances:
While taking off by night from Cairo Airport, the twin engine airplane stalled and crash landed on the runway. It went out of control, veered off runway and came to rest. The aircraft was damaged beyond repair and the pilot, sole on board, was seriously injured.
Probable cause:
The aircraft stall during initial climb after the pilot failed to maintain flying speed.
Final Report: