Crash of a Boeing B-50A-5-BO Superfortress off McDill AFB: 7 killed

Date & Time:
Type of aircraft:
Operator:
Registration:
46-009
Flight Type:
Survivors:
Yes
Schedule:
Chatham - McDill
MSN:
15729
YOM:
1947
Crew on board:
12
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
7
Circumstances:
On approach to McDill AFB, the aircraft caught fire. Five crew members were able to bail out before the aircraft crashed into the Tampa Bay. Seven other crew members were killed.

Crash of a Fairchild C-119B Flying Boxcar in Decatur

Date & Time:
Operator:
Registration:
48-0338
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
10320
YOM:
1948
Location:
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
En route, the right engine failed, forcing the crew to attempt an emergency landing. The aircraft crash landed in a field in Decatur and was damaged beyond repair. There were no injuries among the five occupants.
Probable cause:
In flight failure of the right engine.

Crash of a Fairchild C-119C-13-FA Flying Boxcar in Hendersonville: 4 killed

Date & Time:
Operator:
Registration:
49-0134
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Fort Campbell - Fort Campbell
MSN:
10371
YOM:
1949
Crew on board:
4
Crew fatalities:
Pax on board:
26
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
The aircraft left Fort Campbell AFB in the evening with 31 other similar aircraft to participate to a combined night parachuting exercice. En route, the right engine caught fire. All 26 paratroopers abandoned the aircraft and bailed out. The crew elected to return to Fort Campbell when the aircraft crashed in a field. All four crew members were killed while 26 paratroopers were later found alive.
Probable cause:
Engine fire.

Crash of a Douglas DC-4 into Lake Michigan: 58 killed

Date & Time:
Type of aircraft:
Operator:
Registration:
N95425
Flight Phase:
Survivors:
No
Schedule:
New York – Minneapolis – Spokane – Seattle
MSN:
10270
YOM:
1943
Flight number:
NW2501
Crew on board:
3
Crew fatalities:
Pax on board:
55
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
8662
Captain / Total hours on type:
1968.00
Copilot / Total flying hours:
8821
Copilot / Total hours on type:
400
Aircraft flight hours:
15902
Circumstances:
The flight 2501, was scheduled to operate between the terminal points of New York, N. Y., and Seattle, Wash, via intermediate points of Minneapolis, Minn., and Spokane, Wash. At approximately 1931 the flight departed from LaGuardia Airport for Minneapolis with a crew consisting of Robert C. Lind, captain, Verne F. Wolfe, first officer, and Bonnie A. Feldman, stewardess. On board were 55 passengers, 2, 500 gallons of fuel, 80 gallons of oil, and 490 pounds of express, which resulted in an aircraft weight of 71, 342 pounds for takeoff. This was 58 pounds below the maximum permissible takeoff weight, and the load was distributed so that the center of gravity was within approved limits. The flight plan filed with ARTC (Air Route Traffic Control) specified a cruising altitude of 6 000 feet to Minneapolis. An altitude of 4,000 feet had been originally requested because of forecast en route thunderstorms, but denied by ARTC because other traffic was assigned at that level. At 2149, when over Cleveland, Ohio, a cruising altitude of 4,000 feet was again requested by the flight and this time approved by ARTC. Forty minutes later the flight was requested by ARTC to descend to 3, 500 feet because there was an eastbound flight at 5,000 feet over Lake Michigan which was experiencing severe turbulence and difficulty in maintaining its assigned altitude. ARTC estimated that the two flights would pass each other in the vicinity of Battle Creek, Mich., and that the standard separation of 1,000 feet would not be sufficient because of the turbulence. At 2251, Flight 2501 reported that it was over Battle Creek at 3,500 feet, and that it would be over Milwaukee at 2337. When in the vicinity of Benton Harbor, at 2313, the flight requested a cruising altitude of 2,500 feet, however, no reason was given for the request. ARTC was unable to approve this altitude because of other traffic. Acknowledgement that ARTC could not approve descent to 2,500 feet was received at 2315, and this was the last communication received from the flight. At 2337, Northwest Radio at Milwaukee advised the company at LaGuardia and Minneapolis, and ARTC at Chicago, that the flight was ten minutes overdue since they had incorrectly copied the 2251 flight report as 2327. At 2345 Northwest Radio at Milwaukee transmitted to the flight instructions to circle the range station at Madison, Wis., if its radio transmitter was inoperative. During the same period, all CAA (Civil Aeronautics Administration) radio stations in the Chicago-Minneapolis area tried to contact the flight on all frequencies. At 2358, Chicago ARTC, at the request of Northwest Airlines, alerted air-sea rescue facilities in the area, which included the Air Force, Navy, Coast Guard, and the state police of Illinois, Michigan, Wisconsin, and Indiana. The missing aircraft was assumed to have been involved in an accident at 0530 since the fuel supply at that time would have been exhausted. An intensive search of the Lake Michigan area was commenced at daylight June 24. On the following day, at 1830, the United States Coast Guard cutter Woodbine found an oil slick, aircraft debris, and the aircraft log book in Lake Michigan approximately 18 miles north-northwest of Benton Harbor. At 0530, June 25, underwater search operations were conducted with divers and sonar equipment. Divers descended at the points where strong sonar contacts were made. At those locations, the lake bottom was 150 feet below the surface of the water and was covered by a layer of silt and mud estimated to be 30 to 40 feet deep. Visibility was less than eight inches. The possibility of locating anything was slight, and movement was severely restricted. In addition to diving operations, the entire area was dragged with grapnel but without results. After two days of operation, the Navy suspended their search because of the difficult conditions, and because nothing had been found which would indicate that the aircraft could be recovered. Since then, the Coast Guard and aircraft flying in that area have maintained a sea and air surveillance. The only parts of the aircraft that were recovered were those with sufficient buoyancy to float a fuel tank float, foam rubber cushions, arm rests, clothing, blankets, pillows, pieces of luggage, cabin lining, plywood flooring and other wooden parts. The cushions and arm rests, shredded from impact forces and cutting edges of the fuselage, indicated that the aircraft struck the water at high speed. A plywood oxygen bottle support bracket, which had been installed in the forward left side of the fuselage, showed that the inertia forces acted in a forward, downward, and to the left direction. There was no sign of fire found on any parts recovered. All 58 occupants have been killed.
Probable cause:
The Board determines that there is not sufficient evidence upon which to make a determination of probable cause. At the approximate time of the accident a squall line was located in the area where the aircraft crashed. Despite an intensive surface and underwater search, the aircraft was not located with the exception of a few fragments.
Final Report:

Crash of a Douglas C-47B-5-DK in Tinker AFB: 1 killed

Date & Time:
Operator:
Registration:
43-48885
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
14701/26146
YOM:
1944
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
Just after liftoff, while in initial climb, the aircraft stalled and crashed. A pilot was killed and the second occupant was injured.

Crash of a Douglas C-47D in Tulsa: 1 killed

Date & Time:
Operator:
Registration:
43-48477
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
14293/25738
YOM:
1944
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
16
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
During the takeoff roll, the pilot in command started the rotation when an engine failed. The aircraft went out of control, veered off runway and collided with a building housing the school of army cadets. The aircraft was damaged beyond repair and all 18 occupants were slightly injured. In the building, three guys were injured while a fourth was killed.
Probable cause:
Engine failure.

Crash of a Lockheed P2V-2 Neptune in Quonset Point NAS: 9 killed

Date & Time:
Type of aircraft:
Operator:
Registration:
122454
Flight Type:
Survivors:
Yes
Schedule:
Jacksonville – Argentia
Crew on board:
12
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
9
Circumstances:
En route from Jacksonville NAS to Argentia in Newfoundland, the crew encountered an unexpected situation and the captain decided to divert to Quonset Point NAS for a safe landing. But on final approach, the aircraft went out of control and crashed in flames few miles short of runway threshold. Three crew members were rescued while nine others were killed.

Crash of a Curtiss C-46F-1-CU Commando in Teterboro: 1 killed

Date & Time:
Type of aircraft:
Operator:
Registration:
N9406H
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Teterboro – Fort Wayne – Detroit
MSN:
22582
YOM:
1945
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3200
Captain / Total hours on type:
200.00
Copilot / Total flying hours:
2800
Copilot / Total hours on type:
160
Circumstances:
At 1727 the aircraft was cleared to Runway 19 for takeoff toward the south. The engines were run up to a manifold pressure of 15 inches of mercury and ignition was checked on both magnetos of each engine. Takeoff was then started and the manifold pressure was increased to 52 inches of mercury. Ground witnesses estimated that the takeoff run as somewhat longer than usual for this model aircraft. Tower personnel and several ground witnesses saw puffs of black smoke coming from the left engine immediately after the takeoff. At an altitude estimated as 200-300 feet, the left engine started to misfire. The landing gear had been raised and was checked for position. The left engine continued misfiring and shortly became worse. The left propeller as feathered. Ahead, the terrain as flat, unobstructed and marshy. Full power was maintained on the right engine and a left turn was started as if to return to the airport. At this point the altitude was estimated to be 400-500 feet. During the turn the air speed fell to 85-90 1 PH and the aircraft settled. This turning and settling continued until the aircraft neared the ground, when it was leveled laterally. It struck while about level, both laterally and longitudinally, and slid along the omen ground in a generally northeasterly direction for some 620 feet where it struck some large trees and turned to the left about 180 degrees. Both captain and copilot were thrown clear of the wreckage. The captain later died from his injuries. The weather was good and was not a factor in the accident.
Probable cause:
The Board determines that the probable cause of the accident was overloading of the aircraft due to faulty loading end dispatch procedures coupled with engine malfunctioning due to inadequate maintenance.
The following factors were noted:
- The aircraft's was leaded above its maximum gross weight by approximately 5,000 pounds,
- The aircraft had been flown in excess of its 80-hour inspection period,
- Both engines were inadequately maintained,
- The ignition systems of both engines were found to be defective,
- The left engine malfunctioned and its propeller was feathered shortly after takeoff at an air speed of 130-135 miles per hour,
- A left turn was made and the air speed fell sharply to 85-90 miles per hour,
- The aircraft settled to the ground in a near stalled condition.
Final Report:

Crash of a Boeing 247D in Walla Walla: 2 killed

Date & Time:
Type of aircraft:
Operator:
Registration:
NR13352
Flight Phase:
Survivors:
No
Schedule:
Walla Walla - Walla Walla
MSN:
1734
YOM:
1933
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The crew was engaged in an agricultural mission and while flying at low height, the twin engine aircraft hit tree tops and crashed in flames in a wooded area. Both crew members were killed.

Crash of a Grumman G-73 Mallard in Charlotte: 1 killed

Date & Time:
Type of aircraft:
Operator:
Registration:
N2941
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
J-3
YOM:
1946
Crew on board:
4
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
Shortly after takeoff from Charlotte-Douglas Airport, while in initial climb, the seaplane stalled and crashed in flames. A crew member was killed.