Crash of an ATR42-500 in Coari

Date & Time: May 30, 2014 at 2055 LT
Type of aircraft:
Operator:
Registration:
PR-TKB
Flight Phase:
Survivors:
Yes
Schedule:
Coari - Manaus
MSN:
610
YOM:
2000
Location:
Country:
Crew on board:
4
Crew fatalities:
Pax on board:
45
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total hours on type:
2601.00
Copilot / Total flying hours:
5898
Copilot / Total hours on type:
548
Circumstances:
During the takeoff roll from Coari-Urucu Airport by night, the aircraft collided with a tapir that struck the right main gear. The crew continued the takeoff procedure and the flight to Manaus. After two hours and burning fuel, the aircraft landed at Manaus-Eduardo Gomes Airport. Upon touchdown, the right main gear collapsed and the aircraft veered to the right and came to rest. All 49 occupants evacuated safely while the aircraft was damaged beyond repair.
Probable cause:
Collision with a tapir during takeoff, causing severe damages to the right main gear.
The following findings were identified:
- The lack of isolation of the operational area allowed the land animal to enter the runway for landings and takeoffs, contributing to the accident.
- The crew did not notice the presence of the land animal on the runway early enough to abort the takeoff without extrapolating the runway limits and avoiding collision.
- The presence of the land animal (Tapirus terrestris) interfered with the operation and led to the collision of the right main landing gear.
Final Report:

Crash of a Fokker 100 in Brasília

Date & Time: Mar 28, 2014 at 1742 LT
Type of aircraft:
Operator:
Registration:
PR-OAF
Survivors:
Yes
Schedule:
Petrolina – Brasília
MSN:
11415
YOM:
1992
Flight number:
OC6393
Country:
Crew on board:
5
Crew fatalities:
Pax on board:
44
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4993
Captain / Total hours on type:
3060.00
Copilot / Total flying hours:
3357
Copilot / Total hours on type:
2844
Aircraft flight hours:
44449
Aircraft flight cycles:
32602
Circumstances:
The aircraft took off from the Senador Nilo Coelho Aerodrome (SBPL), Petrolina - PE, to Presidente Juscelino Kubitschek International Airport (SBBR), Brasilia - DF, at 1752 (UTC), in order to complete the scheduled cargo and personnel flight O6 6393, with 5 crewmembers and 44 passengers on board. During the level flight, thirty minutes after takeoff, the aircraft presented low level in the hydraulic system 1. The crew performed the planned operational procedures and continued the flight to Brasilia, with the hydraulic system degraded. During the SBBR landing procedures, the crew used the alternative system for lowering the landing gears. The main landing gears lowered and locked, the nose landing gear unlocked, but did not lower. After coordination with the air traffic control, the aircraft was instructed to land on SBBR runway 11R. The landing took place at 2042 (UTC). After the touchdown, the aircraft covered a total distance of 900 meters until its full stop. The initial 750 meters were with the aircraft supported only by the main landing gears and the last 150 meters were with the aircraft supported by the main landing gears and by the lower part of the front fuselage. The aircraft stopped on the runway. Substantial damage to structural elements of the aircraft occurred near the nose section. The evacuation of the crewmembers and passengers was safe and orderly. The copilot suffered fractures in the thoracic spine. The other crewmembers and passengers left unharmed.
Probable cause:
The following findings were identified:
- It was found that there was a restriction on the articulation movement of the right nose landing gear door and that the weight of this landing gear was not sufficient to overcome such restriction.
Upon inspecting the hinges, it was found that there were no signs of recent lubrication, allowing the hypothesis of occurrence of any deviation or non-adherence to the inspection and lubrication requirements established by the manufacturer leading to a the scenario favorable to the right door movement restriction. The issue of the maintenance could also be related to some deviation, or nonadherence to the requirements established for the service of widening the holes of the hinges concerning the coating and corrosion protection of the worked surface. As a result, the area could have been more susceptible to corrosive processes.
- The maintenance program, established by the manufacturer, may have contributed to the occurrence by not establishing adequate preventive maintenance parameters for the landing gear doors that were modified by reworking the hinges, incorporating larger radial pins and widening the lobe holes.
- It was not possible to determine the causal root of the EDP1 gasket extrusion, which caused the leakage of hydraulic oil that caused the hydraulic system 1 to fail.
Final Report:

Crash of a Britten Norman BN-2A-3 Islander in Aldeia Pikany: 5 killed

Date & Time: Dec 4, 2013 at 1130 LT
Type of aircraft:
Operator:
Registration:
PT-WMY
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Aldeia Pikany – Novo Progresso
MSN:
314
YOM:
1974
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
530
Captain / Total hours on type:
58.00
Circumstances:
Shortly after takeoff from The Pikany Indian Reserve Airfield, while in initial climb, the twin engine aircraft lost height, collided with trees and crashed in a wooded area located on km from the airstrip. The aircraft was destroyed and all five occupants were killed, among them Indian Kayapo who were flying to Novo Progresso to have urgent care.
Probable cause:
The following factors were identified:
- The utilization of an aircraft not included in the Operating Specifications and of a runway neither registered nor approved, with a pilot who did not have the amount of hours necessary nor specific training, disclose a culture based on informal practices, which led to operation below the minimum safety requirements.
- It is possible that the pilot forgot to verify the quantity of fuel in the tanks of the aircraft before takeoff.
- The lack of specific training for the pilot and for the coordinator who, possibly, assumed the function of instructor may have compromised their operational performance during the preparation and conduction of the flight, since they were not effectively prepared for the activity.
- It is possible that the pilot failed to comply with the prescriptions of the legislation relatively to the minimum amount of fuel required for the flight leg. The operation of the aircraft by a pilot with expired qualifications and without the required training goes against the prescriptions at the time, but it was not determined whether this pilot (coordinator) was in the aircraft controls at the moment of the accident. The transport of a cylinder onboard the aircraft also configures flight indiscipline, since it goes against the legislation which prohibits the transport of such material.
- The lack of training of the differences may have contributed to the forgetting to verify the fuel tanks, a procedure that is prescribed in the aircraft manual. Likewise, lack of training may have deprived the pilots from acquiring proficiency for the operation of the aircraft in a single engine condition.
- The fact of conducting a flight to provide assistance in an emergency situation may have contributed to the pilot having forgotten to check safety parameters, such as the amount of fuel necessary.
- The pilot’s intention to earn his operational promotion may have stimulated him excessively, to the point of disregarding the minimum safety requirements for the operation. In addition, the emergency nature of the flight request possibly added to the motivation of the pilot and the coordinator.
- It is possible that, due to having little total experience either both of flight and in the aircraft, the pilot lost control of the aircraft when faced with the situation of in-flight engine failure after the takeoff.
- It is possible that the pilot and the coordinator prioritized the emergency requirement of the situation, failing to evaluate other aspects relevant for the safety of the flight, such as planning, for example.
- The lack of control on the part of the company’s management in relation to the flights operating outside of the main base allowed the pilot and the base manager to conduct a flight without the operating sector authorization. The lack of supervision of the air transport service provision by the contracting organizations allowed the company to provide services without the minimum conditions required by the legislation. Such conditions exposed the passengers to the risks of an irregular operation.
Final Report:

Crash of a Comp Air CA-8 in Sorocaba: 2 killed

Date & Time: May 29, 2013 at 1540 LT
Type of aircraft:
Operator:
Registration:
PP-XLR
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Sorocaba - Jundiaí
MSN:
0204CA8
YOM:
2006
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
Shortly after take off from Sorocaba Airport, while climbing, the pilot encountered technical problems and elected to return. While trying to land in a wasteland, the single engine aircraft crashed in a street and was destroyed by impact forces and a post impact fire. Both occupants were killed as a house was also destroyed.

Crash of an Embraer EMB-820C Carajá in Almeirim: 10 killed

Date & Time: Mar 12, 2013 at 2030 LT
Operator:
Registration:
PT-VAQ
Survivors:
No
Schedule:
Belém - Almeirim
MSN:
820-140
YOM:
1986
Location:
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
10
Captain / Total flying hours:
1300
Captain / Total hours on type:
70.00
Circumstances:
The twin engine aircraft departed Belém-Val de Cans-Júlio Cezar Ribeiro Airport at 1907LT on a flight to Almeirim, carrying one pilot and nine employees of a company taking part to the construction of a hydro-electric station in the area. Following an eventful flight at FL85, the pilot started the descent to Almeirim and contacted ground at 2023LT. On final approach by night, the aircraft descended too low, impacted ground and crashed 5 km short of runway, bursting into flames. The aircraft was destroyed and all 10 occupants were killed.
Probable cause:
The following findings were identified:
- The pilot took the risks inherent to that flight when he accepted to be the only crewmember on a night-time flight with an aircraft in which he lacked enough experience. It is therefore considered that the pilot was complacent when he accepted to fly the aircraft under those circumstances, taking the risks associated with the operation.
- The fact that the pilot made a phone call to his father, to tell that he was feeling insecure for conducting the flight, may be considered an indication that he was not confident, and this condition may have influenced negatively his operational performance during the descent procedure.
- It is possible that the motivation of the pilot in making a fast progress in his career contributed to his acceptance of the challenge to operate the flight, even if he was not feeling fully confident.
- It is possible that the characteristics related to the type of flight, regions, time of the day, in addition to the fact that the pilot was flying the aircraft alone for the first time, contributed to an unclear perception of the relevant elements around him, leading him to a mistaken comprehension, which resulted in the deterioration of his ability to foresee the events.
- The operational progress of the pilot in the company was expedited and, therefore, it is possible that for this reason he did not gather the necessary experience for conducting that type of flight.
- It is possible that the way the work was organized within the company, with designation of pilots not readapted in the aircraft for night-time flights without artificial horizon, and for takeoffs with an aircraft weight above the one prescribed in the manual contributed to the event that resulted in the accident.
- It is possible that the prioritization of the financial sector, in detriment of operational safety, contributed to the designation of a single pilot with short experience for transporting nine passengers.
- It is probable that the pilot, during the preparation of the aircraft for landing, allowed the its speed and power to drop to a value below the minima required for maintenance of level flight on the downwind leg.
- It is possible that the location of the runway in an isolated area of the Amazonian jungle region, without visual references in a night-time flight, contributed to the pilot’s difficulty maintaining a sustained flight.
- It is possible that the training done by the pilot in a shortened manner deprived him from the knowledge and other technical abilities necessary for flying the aircraft.
- The decisions of the company operation sector to designate a short-experienced pilot without a copilot for a night flight destined for an aerodrome located in a jungle region without visual reference with the terrain increased the risk of the operation. Therefore, the risk management process was probably inappropriate.
- It was the first time the pilot was flying the aircraft on a night-time flight without a copilot. Since he had only little experience in the aircraft, it is possible that his operational performance was hindered in the management of tasks, weakening his situational awareness.
- It was not possible to determine whether the company chose to dispense with the copilot on account of the need to transport a ninth passenger and, thus, did not consider in a conservative manner the prescription contained in the aircraft airworthiness certificate by designating just one pilot for the flight.
Final Report:

Crash of a Beechcraft King Air C90A in Cândido Mota: 5 killed

Date & Time: Feb 3, 2013 at 2030 LT
Type of aircraft:
Registration:
PP-AJV
Flight Phase:
Survivors:
No
Schedule:
Maringá – São Paulo
MSN:
LJ-1647
YOM:
2001
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total hours on type:
441.00
Aircraft flight hours:
3137
Circumstances:
The twin engine aircraft departed Maringá Airport at 1837LT on a flight to São Paulo, carrying four passengers and one pilot. 35 minutes into the flight, about five minutes after he reached its assigned altitude of 21,000 feet, the aircraft stalled and entered an uncontrolled descent. The pilot was unable to regain control, the aircraft partially disintegrated in the air and eventually crashed in a flat attitude in a field. The aircraft was destroyed and all five occupants were killed.
Probable cause:
The following findings were identified:
- The lack of a prompt identification of the aircraft stall by the captain may have deprived him of handling the controls in accordance with the prescriptions of the aircraft emergency procedures, contributing to the aircraft entry in an abnormal attitude.
- The captain’s attention was focused on the passengers sitting in the rear seats, in detriment of the flight conditions under which the aircraft was flying. This had a direct influence on the maintenance of a poor situational awareness, which may have made it difficult for the captain to immediately identify that the aircraft was stalling.
- There was complacency when the copilot functions were assumed by a person lacking due professional formation and qualification for such. Even under an adverse condition, the prescribed procedure was not performed, namely, the use of the aircraft checklist.
- The fact that the aircraft was flying under icing conditions was confirmed by a statement of the female passenger in the cockpit (CVR). The FL210 (selected and maintained by the captain) gave rise to conditions favorable to severe icing on the aircraft structure. If the prevailing weather conditions are correlated with reduction of speed (attested by the radar rerun), the connection between loss of control in flight and degraded aircraft performance is duly established.
- The rotation of the aircraft after stalling may have contributed to the loss of references of the captain’s balance organs (vestibular system), making it impossible for him to associate the side of the turn made by the aircraft with the necessary corrective actions.
- The non-adherence to the aircraft checklists on the part of the captain, in addition to the deliberate adoption of non-prescribed procedures (disarmament of the starter and “seven killers”) raised doubts on the quality of the instruction delivered by the captain.
- The captain made an inappropriate flight level selection for his flight destined for São Paulo. Even after a higher flight level was offered to him, he decided to maintain FL 210. Also, after being informed about icing on the aircraft, he did not activate the Ice Protection System, as is expressly determined by the flight manual.
- The captain had the habit of making use of a checklist not prescribed for the aircraft, and this may have influenced his actions in response to the situation he was experiencing in flight.
- His recently earned technical qualification in the aircraft type; his inattention and distraction in flight; his attitude of non-compliance with operations and procedures prescribed in manuals; all of this contributed to the captain’s poor situational awareness.
- The flight plan was submitted via telephone. Therefore, it was not possible to determine the captain’s level of awareness of the real conditions along the route, since he did not report to the AIS office in SBMG. In any event, the selection of a freezing level for the flight, considering that the front was moving along the same proposed route, was indication of inappropriate planning.
- The investigation could neither determine the whole experience of the aircraft captain, nor whether his IFR flight experience was sufficient for conducting the proposed flight, since he made decisions which went against the best practices, such as, for example, selecting a flight level with known icing.
- With a compromised situational awareness, the pilot failed to correctly interpret the information available in the aircraft, as well as the information provided by the female passenger sitting in the cockpit, and he chose to maintain the flight level under inadequate weather conditions.
- The lack of monitoring/supervision of the activities performed by the captain allowed that behaviors and attitudes contrary to flight safety could be adopted in flight, as can be observed in this occurrence.
- Apparently, there was lack of an effective managerial supervision on the part of the aircraft operator, with regard to both the actions performed by the captain and the correction of the aircraft problems.
Final Report:

Crash of a Cessna 525B Citation CJ3 in São Paulo

Date & Time: Nov 11, 2012 at 1721 LT
Type of aircraft:
Operator:
Registration:
PR-MRG
Survivors:
Yes
Schedule:
Florianópolis – São Paulo
MSN:
525B-0187
YOM:
2008
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4048
Captain / Total hours on type:
521.00
Copilot / Total flying hours:
648
Copilot / Total hours on type:
189
Circumstances:
Following an uneventful flight from Florianópolis, the crew started the approach to São Paulo-Congonhas Airport Runway 35R. After touchdown, the airplane was unable to stop within the remaining distance. It overran, went down an embankment and came to rest against a fence, broken in two. The passenger and the copilot were slightly injured and captain was seriously injured. The aircraft was destroyed.
Probable cause:
The following findings were identified:
- The commander was overconfident in himself and the aircraft which led him to lose the critical capacity to discern the risks involved in the procedure that was adopting. Corroborating was the fact that the pilot judged he had much knowledge in this operation and knew exactly how the aircraft responded. It can be inferred there was complacency by the copilot on the actions of the commander, during the approach at high speed, because even feeling uncomfortable, he did not make an incisive interference because he believed in the idea that the commander had done this kind of approach, with high speed, and so knowing what he was doing.
- The pilot failed to identify the location of touch down during landing and not knowing how much runway was remaining, he decided he should not rush, thus demonstrating low situational awareness and lack of awareness, impacting the proper reaction time for the situation (Rush), which was not performed , leading the occurrence in question.
- The crew failed to properly assess the information available like speed and the runway length for the realization of a safe landing, which led to a poor judgment of the situation at hand, making the decision not to adopt the missed approach procedure.
- The distance between the crew, caused unconsciously by the commander's position with excess knowledge in the operation and the aircraft, and the insecurity of the copilot in considering new and inexperienced, resulted in a lack of assertiveness of the copilot to inform, with little emphasis, the commander of his perception of excessive airspeed.
- The crew did not adopt good crew resource management, failing to communicate with assertiveness and share critical information in time prior to landing, allowing the speeding remained present until the touchdown.
- Despite having adequate experience and training, the commander did not use the resources available, such as speed brakes to reduce the aircraft approach speed.
- The variable wind direction and predominantly tail intensity equal to or greater than 10 knots, allowed excessive speed during landing.
- The crew did not adopt good crew resource management, allowing the high speed to remain present until the touchdown.
- The commander thought he would be able to perform the approach and landing with the speed above the expected.
Final Report:

Crash of a Piper PA-31T2 Cheyenne II XL in Curitiba: 4 killed

Date & Time: Nov 6, 2012 at 1725 LT
Type of aircraft:
Operator:
Registration:
PT-MFW
Survivors:
No
Schedule:
Dourados – Curitiba
MSN:
31-8166067
YOM:
1981
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
11088
Captain / Total hours on type:
618.00
Copilot / Total flying hours:
771
Copilot / Total hours on type:
16
Circumstances:
The twin engine aircraft departed Dourados-Francisco de Matos Pereira Airport on an on-demand flight to Curitiba, carrying two passengers, two pilots and a load consisting of valuables. On final approach to Curitiba-Bacacheri Airport, both engines failed simultaneously. The crew attempted an emergency landing when the aircraft crashed in a field and came to rest near trees. A passenger was seriously injured while three other occupants were killed. The following day, the only survivor died from his injuries.
Probable cause:
The following findings were identified:
- Fatigue is likely to have occurred, since there are reports of high workload, capable of affecting the perception, judgment, and decision making of the crew.
- In view of the fact that the captain displayed an attitude of gratefulness toward the company which hired him, working for consecutive hours and many times more than was prescribed for his daily routine, it is possible that such high motivation may have been present in the accident flight, harming his capacity to evaluate the conditions required for a safe flight.
- The crew neither gathered nor properly evaluated the available pieces of information for the correct refueling of the aircraft, something that led to their decision of not refueling the aircraft in SBDO.
- The company crews did not usually keep fuel records, and made approximate calculations based on the fuel remaining from previous flights, whose control parameters were not dependable. Such attitudes reflected a work-group culture that became apparent in this accident.
- The pilots were presumably undergoing a condition of stress on account of the company flight routine, in which they flew every day, with little time dedicated to rest or even holidays. Under such condition, the pilots may have had their cognitive processes affected, weakening their performance in flight.
- The flights had the objective of transporting valuables, causing concern in relation to security issues involving the aircraft on the ground. Thus, it is suspected that decisions made by the pilots may have been affected by this complexity, such as, for example, deciding not to refuel the aircraft on certain locations.
- The way the work was structured in the company was giving rise to overload due to the routine of many flights and few periods of rest or holidays. This situation may have affected the crew’s performance, interfering in the analysis of the conditions necessary for a safe flight.
- The company did not monitor the performance of its pilots for the identification of contingent deviations from standard procedures, such as non-compliance with the MGO.
- Failures in the application of operational norms, as well as in the communication between the crew members, may have occurred on account of inadequate management of tasks by each individual, such as, for example, the use of the checklist and the filling out of control forms relative to fuel consumption contained in the company MGO.
- The crew judged that the amount of fuel existing in the aircraft was sufficient for the flight in question.
- The fact that the fuel gauges were not indicating the correct quantity of fuel had direct influence on the flight outcome, since the planning factors and the pilots’ situational awareness were affected.
- The crew did not analyze appropriately the amount of fuel necessary for the flight leg between SBDO and SBBI. The Mission Order did not establish the minimum amount of fuel necessary for the flight legs, and the crew had to take responsibility for the decision.
- The company was not rigorous with the filling out of aircraft logbooks and cargo manifestos, resulting that it did not have control over the operational procedures performed by the crews, and this may have contributed to the aircraft taking off with an amount of fuel that was insufficient for the flight. Although the MGO had parameters established for calculating the endurance necessary for VFR/IFR flights, the company did not define the fuel necessary in the Mission Orders, transferring the responsibility for the decision to the aircraft captain.
Final Report:

Crash of a McDonnell Douglas MD-11F in Campinas

Date & Time: Oct 13, 2012 at 1852 LT
Type of aircraft:
Operator:
Registration:
N988AR
Flight Type:
Survivors:
Yes
Schedule:
Miami - Campinas
MSN:
48434/476
YOM:
1991
Flight number:
CWC425
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
12900
Copilot / Total flying hours:
5198
Copilot / Total hours on type:
1368
Circumstances:
The airplane took off from Miami International Airport (KMIA), destined for Viracopos Airport (SBKP), with two pilots and a mechanic on board, on a non-regular cargo transport flight. The flight was uneventful up to the moment its landing in SBKP. On the approach for landing on runway 15, the crew performed the IFR ILS Z procedure. The weather conditions were VMC, with the wind coming from 140º at 19kt. When the aircraft was granted clearance to land, the wind strength was 20kt, gusting up to 29kt. The copilot was the Pilot Flying (PF), and the captain was the Pilot Monitoring (PM) at the moment of landing. When the aircraft touched down on the runway after the flare, the left main landing gear collapsed, causing the aircraft to skid on the runway for approximately 800 meters before stopping. There was substantial damage to the left main gear assembly, to the left wing, and left engine. The aircraft stopped within the runway limits. All three crew members were uninjured.
Probable cause:
It was determined that the “the landing gear failed due to overload in the cylinder structure”. The fracture started in the rear section of the cylinder in a connection hole which served as a tension concentration point, and ended in the front part of the cylinder with its breakage into two parts. Following a failure of the right main gear upon landing in Montevideo on 20 October 2009, the right main landing gear was replaced by VARIG Engineering & Maintenance (VEM), but the organization responsible for the research of damage, the specification of the services necessary for the restoration of airworthiness, and the provision of the services that enabled the restoration of the aircraft to an airworthy condition was not identified. The same aircraft parts were subjected to metallurgical analysis at the Boeing Long Beach Materials, Processing and Physics [MP&P] Laboratories, in Huntington Beach, California, USA; and the technical report issued by Boeing highlighted that in one of the points of origin of the failure, the analysis had identified characteristics similar to a pre-crack point, which would have begun earlier, probably due to overload. In the tasks that led to the restoration of the aircraft airworthiness after the accident in Uruguay in 2009 (Hard-Landing), and also in subsequent periodic inspections, the existence of pre-crack traces resulting from a previous overload condition may not have been identified, something that could have resulted in a point of stress concentration.
Final Report:

Crash of a Piper PA-46R-350T Matrix off Jacarepaguá: 2 killed

Date & Time: Aug 21, 2012 at 1935 LT
Registration:
PT-FEM
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Jacarepaguá – Campo de Marte
MSN:
46-92158
YOM:
2010
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
Shortly after a night takeoff from Jacarepaguá Airport, the single engine aircraft entered an uncontrolled descent and crashed in the sea. Few debris were found several days later. The pilot's body was found on September 4 on a beach in Barra de Tijuca. The wreckage and the copilot's body were never found. It was reported that the crew did not activate the transponder after takeoff and did not contact ATC for unknown reasons.