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Crash of a Boeing EC-135N in Walkersville: 21 killed

Date & Time: May 6, 1981 at 1050 LT
Type of aircraft:
Operator:
Registration:
61-0328
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Wright-Patterson - Wright Patterson
MSN:
18235/C13
YOM:
1961
Flight number:
AGAR23
Crew on board:
17
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
21
Aircraft flight hours:
13471
Circumstances:
On 6 May 1981, EC-135N, Serial Number 61-0328, call sign AGAR 23, departed Wright Patterson AFB, Ohio, at 1005 Eastern Daylight Savings Time (EDT) on a routine training mission. On board the aircraft were 17 crewmembers and four authorized passengers. The flight proceeded uneventfully as planned for approximately 45 minutes. Then in a few brief moments, a sequence of very rapid events resulted in a crash with the loss of all onboard. At 1049:48 EDT, The Federal Aviation Administration (FAA) lost radar contact with AGAR 23. The aircraft was cruising at Flight Level 290, at .78 Mach while performing a navigational training leg. The aircraft commander, Capt Emilio, occupied the right pilot seat and a passenger, Mrs. Emilio, occupied the left pilot seat. Also in the crew compartment were the 2 navigators, Lt Col Frederick and Capt Fonke, and 2 passengers, Mrs. Fonke and SSgt Brundige. For undetermined reasons, the aircraft pitch trim moved to the full nose-down position. The aircraft then a rapidly pitched over, most likely upon release of the autopilot, and induced sufficient negative "G" forces to cause the generators to trip off line, resulting in the loss of all AC electrical power. The pitch trim could not then be moved electrically. This condition, while unusual, can be controlled if prompt corrective action is taken; however, if corrective action is delayed approximately 8 seconds, the aircraft pitch angle will be greater than 30 degrees nose-down in the airspeed in excess of 350 knots indicated airspeed. Under these conditions, the aircraft cannot be controlled until the pitch trim is moved toward neutral. While it is evident that recovery was delayed, the reason for the delay is unknown. The aircraft became uncontrollable and entered a steep descent. During the rapid descent, an explosion occurred at approximately 1300 feet above ground level followed immediately by catastrophic failure, and complete break-up of the aircraft. The wreckage was found north of Walkersville and all 21 occupants were killed.
Probable cause:
At 1049:48 EDT, FAA lost radar contact with the aircraft. The aircraft was cruising at flight level 290 at .78 Mach and was performing a navigational training leg. Navigational legs are normally flown on autopilot, and FAA altitude readouts showed the aircraft was within 100 feet of assigned altitude, characteristic of autopilot flight. The aircraft commander, Capt Joseph Emilio, occupied the right pilot seat and a passenger, Mrs. Peggy Emilio, occupied the left pilot seat. Also in the crew compartment were the 2 navigators, Lt Col Benjamin B. Frederick and Capt Donald V. Fonke, and 2 passengers, Mrs. Linda Fonke and SSgt Joseph T. Brundige. This phase of flight, the navigational leg, was the least demanding on the pilot and was the logical time for the passengers to come forward to view the cockpit area. There is no evidence that the presence of the passengers in the crew compartment contributed to, or caused, the accident. For undetermined reasons, the aircraft pitch trim moved to the full nose-down position. The autopilot can overcome the trim until near full nose-down. The aircraft then rapidly pitched over, most likely upon release of the autopilot, and induced sufficient negative "G" forces to cause the generators to trip off line and loss of all AC electrical power. The pitch trim could not then be moved electrically. This condition, while unusual, can be easily controlled if prompt corrective action is taken; however if corrective action is delayed approximately 8 seconds, the aircraft pitch angle will be greater than 30° nose-down in the airspeed in excess of 350 KIAS. Under these conditions, the aircraft cannot be controlled until the pitch trim is moved toward neutral. While it is clear that recovery was delayed, the reason for the delay is unknown. The aircraft became uncontrollable and entered a steep descent. The aircraft emerged from the clouds at 2,000 feet above ground level (AGL) and was intact. Airspeed was in excess of 400 KTAS and die to angle was 20 to 30 degrees. Engine power was above 2.0 engine pressure ratio (EPR). At approximately 1,500 feet mean sea level (MSL) an explosion occurred inside the pressurized compartment of the fuselage and weakened the aircraft structure to the extent that catastrophic failure of the aircraft followed immediately. Cause of this explosion is undetermined; however, the aircraft was in an unrecoverable condition at the time of the explosion and a crash was already inevitable.

Crash of a Boeing B-52H-135-BW Stratofortress at Wright-Patterson AFB

Date & Time: May 30, 1974
Type of aircraft:
Operator:
Registration:
60-0006
Flight Type:
Survivors:
Yes
Schedule:
Wright-Patterson - Wright-Patterson
MSN:
464372
YOM:
1960
Crew on board:
7
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was completing a local training flight at Wright-Patterson AFB. On final approach, the airplane went out of control and crashed in a field. All seven crew members were rescued while the aircraft was destroyed.
Probable cause:
Loss of control on final approach after rudder and elevators failed.

Crash of a Lockheed L-382B-10C Hercules at McGuire AFB: 3 killed

Date & Time: Oct 10, 1970 at 2130 LT
Type of aircraft:
Operator:
Registration:
N9248R
Flight Type:
Survivors:
No
Schedule:
Wright Patterson – McGuire – Dover
MSN:
4221
YOM:
1967
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
16586
Captain / Total hours on type:
11735.00
Circumstances:
The crew was completing a cargo flight from Wright Patterson AFB, Ohio, to Dover AFB, Delaware, with an intermediate stop at McGuire AFB, New Jersey, on behalf of the US Air Force. On final approach, the crew encountered low visibility due to fog. While transiting from IFR to VFR on short final, the airplane went out of control, struck the ground and crashed 5,470 feet short of runway. The aircraft was destroyed and all three crew members were killed.
Probable cause:
Improper IFR operation on part of the pilot-in-command who suffered a spatial disorientation on final approach. The following factors were reported:
- Low ceiling,
- Fog,
- Instruments-misread or failed to read,
- Company dispatch,
- Weather slightly worse than forecast,
- The crew was disoriented by lite glare,
- Fog during transition from IFR to VFR.
Final Report:

Crash of an Armstrong Whitworth AW.650 Argosy 101 in Piqua

Date & Time: Oct 14, 1965 at 1743 LT
Operator:
Registration:
N601Z
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Madison - Wright-Patterson
MSN:
6659
YOM:
1960
Location:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5616
Captain / Total hours on type:
146.00
Circumstances:
The crew departed Madison-Truax Field at 1610LT on a cargo flight to Wright-Patterson AFB on behalf of the US Air Force. While descending to the airbase, north of Dayton, all four engines stopped simultaneously. The crew attempted an immediate emergency landing in a field. The aircraft slid on the ground and eventually collided with a bridge pile and several vehicles before coming to rest. All three crew members were slightly injured while no one on the ground was hurt. The aircraft was damaged beyond repair.
Probable cause:
Engine failure caused by a fuel exhaustion. Inadequate preflight preparation and miscalculated fuel consumption on part of the flying crew.
Final Report:

Crash of a Boeing KC-135A-BN Stratotanker in Hanscom Field: 3 killed

Date & Time: Aug 8, 1962
Type of aircraft:
Operator:
Registration:
55-3144
Flight Type:
Survivors:
No
Schedule:
Wright-Patterson - Hanscom Field
MSN:
17260
YOM:
1957
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
On final approach to Bedford-Hanscom Field Airport, the pilot-in-command did not realize his altitude was insufficient. The four engine aircraft struck telephone poles, stalled and crashed in a boulder located 2,657 feet short of runway threshold. The aircraft was destroyed and all three crew members were killed.

Crash of a Douglas A-26 Invader in East Dayton: 4 killed

Date & Time: Sep 24, 1957 at 1659 LT
Type of aircraft:
Operator:
Flight Type:
Survivors:
No
Site:
Schedule:
Wright Patterson - Wright Patterson
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
The crew was performing a local training flight and departed Wright-Patterson AFB in the day. On approach, the twin engine aircraft went out of control and crashed in flames into several houses located in 1843 Tuttle Avenue, East Dayton. At least four houses were destroyed. Both pilots as well as two people on the ground were killed.
Crew:
Maj James Melancon, pilot,
Cpt Wilho R. Heikkinen, copilot.
Both civilians killed were Mildred VanZant and Walter Geisler.
Probable cause:
An investigation determined that a loose engine cowling moved forward into the propeller.

Crash of a Boeing B-50D-80-BO Superfortress in Wilmington Pike: 11 killed

Date & Time: Feb 27, 1956
Type of aircraft:
Operator:
Registration:
48-072
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Wright-Patterson - Wright-Patterson
MSN:
15881
YOM:
1948
Location:
Crew on board:
11
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
11
Circumstances:
While conducting a training mission out from Wright-Patterson AFB, the airplane crashed in unknown circumstances in Wilmington Pike, southeast of Dayton. All 11 occupants were killed.

Crash of a North American TB-25N Mitchell at Mitchel AFB: 6 killed

Date & Time: Sep 13, 1955 at 0830 LT
Operator:
Registration:
45-8822
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Mitchel – Wright-Patterson
MSN:
108-47673
YOM:
1945
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
Shortly after takeoff from Mitchel AFB, while climbing to a height of about 300 feet, the crew informed ground about the failure of the right engine. The crew elected to make an emergency landing when the aircraft crashed in a cemetery in Uniondale, bursting into flames. All six occupants were killed.
Crew:
Maj James D. Judy, pilot,
Cpt Richard E. Hall.
Passengers:
Lt Col Morris I. Fass,
S/Sgt John I. Jackson Jr.,
Lee Rogow,
Larry J. Rubrecht.
Probable cause:
Failure of the right engine for unknown reasons.

Crash of a Beechcraft C-45B Expeditor in Fort McCoy: 4 killed

Date & Time: Jul 6, 1953
Type of aircraft:
Operator:
Registration:
43-35565
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
La Crosse – Fort McCoy – Wright-Patterson
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
The aircraft was on a cross-country flight. Following an overnight stop in La Crosse, Wisconsin, due to poor weather, the aircraft departed the next morning for nearby Fort McCoy, to refuel. After refueling, the airplane departed Fort McCoy for Wright-Patterson AFB but during initial climb, the left engine lost power. The pilot-in-command elected to return and completed a turn to the left when the aircraft stalled and crashed. The aircraft was destroyed and all four occupants were killed.
Crew:
Lcdr LeWayne N. Felts,
Cpt Phillip M. Clinton,
1st Lt Rory G. Jahn,
Cwo Kenneth Ziegler.
Probable cause:
Failure of the left engine shortly after liftoff.

Crash of a Boeing B-29A-60-BN Superfortress into the Peconic Bay: 6 killed

Date & Time: Apr 24, 1953
Type of aircraft:
Operator:
Registration:
44-62093
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Wright-Patterson - Wright-Patterson
MSN:
11570
YOM:
1944
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
A coupling and fully-towed flight was accomplished using the right-handed EF-84B, but no electrical power was received from the B-29. The right hand fighter uncoupled and the left hand fighter coupled with the B-29 and was retracted in the fully-locked towing position. The cockpit panel light indicated that electrical power was available from the B-29, and as soon as everything was trimmed and stabilized and the automatic flight control system was activated momentarily from the fighter. This resulted in a violent pitching motion of the EF-84B causing it to flip up and inward into the B-29. The B-29 outer wing panel crumpled and struck the main B-29 wing spar, shearing off the F-84 nose section before the two aircraft separated. As Bud Anderson flew in formation on the right side of the Superfortress, John Davis brought the left-hand EF-84D into position and linked wingtips with the EB-29A. He transmitted, "Autopilot coming on" and then switched the autopilot on. It commanded hard nose-up elevator. Davis' Thunderjet rolled rapidly to the right onto the outer wing panel of the Superfortress. As the fighter rotated about the wing tip of the bomber, the explosive bolts fired to jettison the Thunderjet, but not in time to prevent the collision between the planes. The left wing of the EB-29A failed outboard of the engines. The nose of the EF-84D broke away from the rest of the airplane.
B-29 went into steep spiral and crashed into Peconic Bay, Long Island and the F-84 crashed shortly thereafter. John Davis and five crew members aboard the EB-29A were killed in the accident. The other fighter, having unhooked, presumably landed safely. The project 'Tip Tow' was immediately cancelled.
Source:
http://www.air-and-space.com/Wing Tip Coupling B-29 F-84.htm
http://www.joebaugher.com/usaf_serials/1944_4.html