Crash of a Piper PA-31-350 Navajo Chieftain off Pompano Beach

Date & Time: Oct 21, 2004 at 1748 LT
Operator:
Registration:
N61518
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Moss Town – Fort Lauderdale
MSN:
31-7552022
YOM:
1975
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4500
Aircraft flight hours:
19269
Circumstances:
Before the start of the trip, the pilot was reportedly given $500.00 cash by the operator to purchase fuel. The pilot stated that the first leg of the flight from KFLL to MYEF departed with the main fuel tanks full and approximately 10 gallons in each of the auxiliary fuel tanks. There were no deviations en-route, and the uneventful flight lasted a reported 1 hour 40 minutes. After landing in Exuma International Airport, the main fuel tanks contained slightly more than 1/2 fuel capacity. Ten gallons of fuel were added to each of the two auxiliary fuel tanks at MYEF, no additional fuel was purchased. The flight departed for KFLL, and during the climb to 10,000 feet, he leaned the fuel/air mixture. During the cruise portion of the flight, the fuel in the auxiliary fuel tanks was consumed then he switched to the main fuel tanks to supply fuel to the engines. The flight crossed the DEKAL intersection at 4,000 feet, which is about 31 nautical miles southeast of KFLL, continued, and the right engine manifold pressure decreased, the cylinder head temperature reached red line indication, and the engine sputtered. He declared an emergency with air traffic control and the controller provided vectors to KFLL which he verbally acknowledged but did not comply with. While operating single engine, with the engine operating at full power, he reported no discrepancies with the left engine. He reported he could reach KFLL but was concerned about flying over a populated area at a low altitude, and was losing altitude. Contrary to the statement made by the pilot that he was not able to maintain altitude while flying single-engine, the airplane was capable of a rate of climb greater than 170 feet-per-minute if flown properly. He elected to ditch the airplane in the Atlantic Ocean; the airplane was not recovered. The operator was asked repeatedly by NTSB for historical fuel receipts and flight hours for N61518 but did not comply. NTSB review of fuel consumption calculations performed by the Federal Aviation Administration (FAA) Inspector-In-Charge revealed the aircraft would have experienced fuel exhaustion at the approximate location and time when the pilot declared an emergency with ATC following failure of the right engine. The NTSB did not receive the NTSB requested detailed, signed, dated statement from the pilot.
Probable cause:
The pilot's inadequate in-flight planning/decision, which resulted in fuel exhaustion and the loss of engine power in one engine. Contributing factors were the pilot's inadequate handling of the aircraft following failure of the right engine for his failure to extract maximum single engine performance, and his failure to properly refuel the aircraft.
Final Report:

Crash of a Rockwell Aero Commander 700 in Pompano Beach: 2 killed

Date & Time: Oct 12, 1987 at 1437 LT
Registration:
N26574
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Pompano Beach – Melbourne
MSN:
700-06
YOM:
1978
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
5380
Aircraft flight hours:
1565
Circumstances:
Witnesses stated that just after takeoff, the left engine started to leave a trail of white smoke, the aircraft then turned left back towards the airport and crashed into the street. Post crash examination revealed one of the left engine crankshaft counterweights failed causing the #6 cylinder connecting rod to break and puncture a hole in the upper engine case. Both propellers were found in feather. Both occupants were killed.
Probable cause:
Occurrence #1: loss of engine power (total) - mech failure/malf
Phase of operation: takeoff - initial climb
Findings
1. 1 engine
2. (c) eng assembly, crankshaft counterweights/vib damper - failure, total
3. Propeller feathering - performed - pilot in command
----------
Occurrence #2: loss of engine power (total) - nonmechanical
Phase of operation: takeoff - initial climb
Findings
4. All engines
5. (c) wrong propeller feathered - inadvertent - pilot in command
6. (f) in-flight planning/decision - poor - pilot in command
----------
Occurrence #3: loss of control - in flight
Phase of operation: takeoff - initial climb
Findings
7. (c) airspeed - not maintained - pilot in command
----------
Occurrence #4: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report:

Crash of a Beechcraft 60 Duke off Pompano Beach

Date & Time: Aug 27, 1980 at 0917 LT
Type of aircraft:
Operator:
Registration:
N354D
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Fort Lauderdale – Freeport
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1826
Captain / Total hours on type:
109.00
Circumstances:
Few minutes after takeoff from Fort Lauderdale-Executive Airport, while climbing, both engines failed. The pilot elected to ditch the aircraft off Pompano Beach. Both occupants were rescued while the aircraft was damaged beyond repair.
Probable cause:
Powerplant failure for undetermined reasons. The following contributing factors were reported:
- Forced landing off airport on water,
- Complete failure both engines.
Final Report:

Crash of a Cessna 411 off Pompano Beach

Date & Time: Jul 7, 1980 at 1502 LT
Type of aircraft:
Registration:
N3CC
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
411-0033
YOM:
1964
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1500
Circumstances:
After takeoff from Pompano Beach Airport, while climbing, the right engine surged. The airplane stalled and crashed into the sea close to the shore. All three occupants were injured and the aircraft was written off.
Probable cause:
Engine failure and subsequent stall and crash due to improper operation of powerplant and powerplant controls. The following contributing factors were reported:
- Unqualified person operated aircraft,
- The pilot failed to maintain flying speed,
- Aircraft came to rest in water,
- Partial loss of power on the right engine,
- Pilot not multi-engine rated,
- Stall warning horn on during attempt to stabilize surging right engine,
- Stayed on until impact.
Final Report:

Crash of a Piper PA-61 Aerostar (Ted Smith 601) into the Gulf of Mexico: 1 killed

Date & Time: Apr 27, 1978
Operator:
Registration:
N555BU
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Pompano Beach – Panama City
MSN:
61-0001
YOM:
1968
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
950
Captain / Total hours on type:
36.00
Circumstances:
En route from Pompano Beach to Panama City, Florida, the airplane crashed under unknown circumstances into the Gulf of Mexico. SAR operations were initiated but no trace of the aircraft nor the pilot was ever found.
Probable cause:
Due to lack of evidences, the exact cause of the accident could not be determined. However, it was reported that the pilot-in-command attempted operation with known deficiencies in equipment as the altimeters seemed to be defective since a certain time.
Final Report:

Crash of a Cessna 401 off West Palm Beach

Date & Time: Dec 16, 1977 at 1523 LT
Type of aircraft:
Operator:
Registration:
N80BW
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Washington DC - Pompano Beach
MSN:
401-0111
YOM:
1968
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3454
Captain / Total hours on type:
16.00
Circumstances:
While in cruising altitude along the east coast of Florida, one of the engine failed. The pilot reduced his altitude and ditched the airplane off West Palm Beach. He was seriously injured while the aircraft was lost.
Probable cause:
Engine failure in normal cruise due to inadequate preflight preparation. The following contributing factors were reported:
- Lack of familiarity with aircraft,
- Mismanagement of fuel,
- Fuel exhaustion,
- Aircraft came to rest in water,
- Forced landing off airport on water.
Final Report:

Crash of a Lockheed 18-56 LodeStar in Pompano Beach: 3 killed

Date & Time: Jan 14, 1974 at 2000 LT
Type of aircraft:
Operator:
Registration:
N2375
Flight Type:
Survivors:
No
MSN:
2455
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
5000
Circumstances:
The crew was completing an illegal flight to the US with a load of more than 4,000 pounds of marijuana on board. While flying over Florida, the right engine failed and the crew decided to divert to Pompano Beach Airport for an emergency landing. On final approach, the airplane went out of control and crashed in flames. The aircraft was destroyed and all three occupants were killed.
Probable cause:
Engine malfunction on final approach caused by the failure of a cylinder assembly. The following factors were reported:
- Material failure,
- Failed to follow the approved procedures,
- Improper emergency procedures,
- Failed to maintain flying speed,
- Exercised poor judgment,
- Improperly loaded aircraft and CofG,
- Improper in-flight decisions,
- Low ceiling,
- Obstructions to vision,
- Complete engine failure,
- Failure of n°9 exhaust valve on right engine,
- Propeller not feathered,
- Stalled on turn to airport,
- Over gross weight,
- Illegal flight with about 4,000 pounds of marijuana on board.
Final Report:

Crash of a Rockwell Turbo Commander 680T off Pompano Beach

Date & Time: Oct 3, 1970 at 0705 LT
Registration:
N541W
Flight Phase:
Survivors:
Yes
Schedule:
Pompano Beach – Fort Lauderdale
MSN:
680-1554-13
YOM:
1965
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2200
Captain / Total hours on type:
50.00
Circumstances:
After takeoff from Pompano Beach Airport, while in initial climb, the airplane went out of control, lost height and crashed into the sea few hundred yards off shore. The pilot was seriously injured while the aircraft sank and was lost.
Probable cause:
Failure of both engines during initial climb for undetermined reason.
Final Report: