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Crash of a Mitsubishi MU-2B-60 Marquise in Elyria: 4 killed

Date & Time: Jan 18, 2010 at 1405 LT
Type of aircraft:
Registration:
N80HH
Flight Type:
Survivors:
No
Schedule:
Gainesville - Elyria
MSN:
732
YOM:
1978
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
2010
Captain / Total hours on type:
1250.00
Copilot / Total flying hours:
190
Aircraft flight hours:
6799
Circumstances:
On his first Instrument Landing System (ILS) approach, the pilot initially flew through the localizer course. The pilot then reestablished the airplane on the final approach course, but the airplane’s altitude at the decision height was about 500 feet too high. He executed a missed approach and received radar vectors for another approach. The airplane was flying inbound on the second ILS approach when a witness reported that he saw the airplane about 150 feet above the ground in about a 60-degree nose-low attitude with about an 80-degree right bank angle. The initial ground impact point was about 2,150 feet west of the runway threshold and about 720 feet north (left) of the extended centerline. The cloud tops were about 3,000 feet with light rime or mixed icing. The flap jack screws and flap indicator were found in the 5-degree flap position. The inspection of the airplane revealed no preimpact anomalies to the airframe, engines, or propellers. A radar study performed on the flight indicated that the calibrated airspeed was about 130 knots on the final approach, but subsequently decreased to about 95–100 knots during the 20-second period prior to loss of radar contact. According to the airplane’s flight manual, the wings-level power-off stall speed at the accident aircraft’s weight is about 91 knots. The ILS approach flight profile indicates that 20 degrees of flaps should be used at the glide slope intercept while maintaining 120 knots minimum airspeed. At least 20 degrees of flaps should be maintained until touchdown. The “No Flap” or “5 Degrees Flap Landing” flight profile indicates that the NO FLAP Vref airspeed is 115 knots calibrated airspeed minimum.
Probable cause:
The pilot's failure to maintain adequate airspeed during the instrument approach, which resulted in an aerodynamic stall and impact with terrain.
Final Report:

Crash of a Learjet 25 in Saint Augustine

Date & Time: Jul 21, 2007 at 1410 LT
Type of aircraft:
Operator:
Registration:
N70SK
Flight Type:
Survivors:
Yes
Schedule:
Gainesville - Saint Augustine
MSN:
25-49
YOM:
1970
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4620
Captain / Total hours on type:
250.00
Copilot / Total flying hours:
2453
Copilot / Total hours on type:
368
Aircraft flight hours:
15812
Circumstances:
About 5 miles from the destination airport, the flight was cleared by air traffic control to descend from its cruise altitude of 5,000 feet for a visual approach. As the first officer reduced engine power, both engines "quit." The captain attempted to restart both engines without success. He then took control of the airplane, and instructed the first officer to contact air traffic control and advise them that the airplane had experienced a "dual flameout." The captain configured the airplane by extending the landing gear and flaps and subsequently landed the airplane on the runway "hard," resulting in substantial damage to the airframe. Both engines were test run following the accident at full and idle power with no anomalies noted. Examination of the airplane revealed that it was equipped with an aftermarket throttle
quadrant, and that the power lever locking mechanism pins as well as the throttle quadrant idle stops for both engines were worn. The power lever locking mechanism internal springs for both the left and right power levers were worn and broken. Additionally, it was possible to repeatedly move the left engine's power lever directly into cutoff without first releasing its power lever locking mechanism; however, the right engine's power lever could not be moved to the cut off position without first releasing its associated locking mechanism. The right throttle thrust reverser solenoid installed on the airplane was found to be non-functional, but it is not believed that this component contributed to the accident. No explicit inspection or repair instructions were available for the throttle quadrant assembly. Other than the throttle quadrant issues, no other issues were identified with either the engines or airframe that could be contributed to both engines losing power simultaneously.
Probable cause:
A loss of power on both engines for an undetermined reason.
Final Report:

Crash of a Mitsubishi MU-2B-36 Marquise in West Memphis: 1 killed

Date & Time: Sep 22, 2005 at 1958 LT
Type of aircraft:
Operator:
Registration:
N103RC
Flight Type:
Survivors:
No
Schedule:
West Memphis - Gainesville
MSN:
673
YOM:
1975
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
12600
Captain / Total hours on type:
1900.00
Aircraft flight hours:
10892
Circumstances:
The twin-engine airplane was destroyed when it impacted an earthmoving scraper and terrain in a field about 2.5 miles north of the departure airport in night visual meteorological conditions. Witnesses reported that the pilot had aborted an earlier flight when he returned to the airport and told the mechanic that he had a right engine fire warning light. The discrepancy could not be duplicated during maintenance, and the airplane departed. About 23 minutes after departure, the pilot reported to air traffic control that he needed to return to the airport to have something checked out. The pilot did not report to anyone why he decided to return to the departure airport, and he flew over four airports when he returned to the departure airport. Radar track data indicated that the airplane flew over the departure end of runway 35 at an altitude of about 1,600 feet agl, and made a descending left turn. The airplane's altitude was about 800 feet agl when it crossed the final approach course for runway 35. The airplane continued the descending left turn, but instead of landing on runway 35, the airplane flew a course that paralleled the runway, about 0.8 nm to the right of runway 35. The airplane continued to fly a northerly heading and continued to descend. The radar track data indicated that the airplane's airspeed was decreasing from about 130 kts to about 110 kts during the last one minute and fifty seconds of flight. The last reinforced beacon return indicated that the airplane's altitude was about 200 feet agl, and the airspeed was about 107 kts. The airplane impacted terrain about 0.75 nm from the last radar contact on a 338-degree magnetic heading. A witness reported that the airplane was going slow and was "extremely low." He reported that the airplane disappeared, and then there was an explosion and a fireball that went up about 1,000 feet. Inspection of the airplane revealed that it impacted the earthmover in about a wings level attitude. The landing gear handle was found to be in the landing gear UP position. The inspection of the left engine and propeller revealed damage indicative of engine operation at the time of impact. Inspection of the right engine revealed damage indicative of the engine not operating at the time of impact, consistent with an engine shutdown and a feathered propeller. No pre-existing conditions were found in either engine that would have interfered with normal operation. The inspection of the right engine fire detection loop revealed that the connector had surface contamination. When tested, an intermittent signal was produced which could give a fire alarm indication to the pilot. After the surface contamination was removed, the fire warning detection loop operated normally.
Probable cause:
The pilot's improper in-flight decision not to land at the departure runway or other available airports during the emergency descent, and his failure to maintain clearance from a vehicle and terrain. Contributing factors were a false engine fire warning light, inadequate maintenance by company personnel, a contaminated fire warning detection loop, and night conditions.
Final Report:

Crash of a Learjet 24A in Gainesville

Date & Time: Sep 26, 1999 at 0935 LT
Type of aircraft:
Operator:
Registration:
N224SC
Flight Type:
Survivors:
Yes
Schedule:
Sarasota - Gainesville
MSN:
24-100
YOM:
1966
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4830
Captain / Total hours on type:
580.00
Aircraft flight hours:
12869
Circumstances:
The pilots stated that approach and landing were normal. During landing rollout, about 2,000 feet down the runway, the brakes became ineffective. The aircraft continued to roll off the end of the runway, down an embankment, across a 4 lane road, and came to rest in a drainage ditch. Post-crash examination of the main landing gear brakes showed that 3 out of the 4 brake assemblies were worn beyond allowable limits and all 4 antiskid wheel generators were not producing voltage within the allowable limits. The outboard right main tire had failed during landing roll do to the antiskid becoming inoperative due to the low voltage of the wheel generator. The airplane had received an A-1 through A-6 inspection 2 days before the accident and this was the first flight since the inspection. The A-5 inspection requires inspection of the landing gear brake assemblies for wear, cracks, hydraulic leaks, and release.
Probable cause:
The inadequate inspection of the main landing gear brake assemblies, which lead to operation of the aircraft with worn brakes that failed during the landing roll. Contributing factors were the descending terrain, roadway and ditch.
Final Report:

Crash of a Cessna 208B Grand Caravan in Gainesville: 2 killed

Date & Time: Mar 3, 1995 at 1943 LT
Type of aircraft:
Registration:
N227DM
Survivors:
No
Schedule:
Savannah - Gainesville
MSN:
208B-0364
YOM:
1993
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
2005
Captain / Total hours on type:
201.00
Circumstances:
The flight was executing the non-precision NDB runway 04 approach, had reported procedure turn inbound, and was cleared to change to advisory frequency. Witnesses observed the airplane descend out of the base of the overcast clouds in a 10° nose down, 45° left wing down attitude. The airplane impacted terrain about 3/4 mile south-southeast of the airport. Witnesses in the area reported that the weather was ceilings of about 100 feet and visibility of about 500 feet in light rain and fog. The minimum descent altitude for the approach is 465 feet agl. Both pilots were killed.
Probable cause:
The pilots failure to maintain the minimum descent altitude during the approach. The weather and dark night light condition were factors.
Final Report:

Crash of a Cessna 441 Conquest in Gainesville

Date & Time: Aug 10, 1992 at 1750 LT
Type of aircraft:
Registration:
N920C
Flight Phase:
Survivors:
Yes
Schedule:
Gainesville - Nashville
MSN:
441-0020
YOM:
1978
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8000
Captain / Total hours on type:
305.00
Circumstances:
The pilot reported that immediately after takeoff, he had a collision with a flight of birds. He stated that the right engine immediately had a partial loss of power. He stated that he did not attempt to raise the landing gear nor the flaps following the loss of engine power, and the aircraft would not maintain altitude. Examination of the aircraft engines revealed that there was rotational scratching of the turbine housings on the right engine, and no rotational scratching on the turbine housing of the left engine.
Probable cause:
The poor inflight decision by the pilot in command in that after a partial loss of power, he shut down the wrong engine, did not follow the emergency checklist, did not raise the flaps, and did not retract the landing gear. A factor in the accident was the inflight collision with birds during the takeoff climb.
Final Report:

Crash of a Cessna 401 in New Port Richey: 1 killed

Date & Time: Apr 23, 1992 at 1606 LT
Type of aircraft:
Registration:
N3271Q
Flight Type:
Survivors:
No
Schedule:
New Port Richey - Gainesville
MSN:
401-0071
YOM:
1967
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
12600
Circumstances:
The pic departed on a ferry flight in VFR conditions without a ferry permit. Witnesses stated they observed the airplane returning to the airport at about 150 to 500 feet. The airplane was observed to begin a left turn with the landing gear extended. A fire was observed in the vicinity of the left engine exhaust. The airplane continued in a steep descending left turn before it disappeared below the tree line and collided with the terrain. The airplane was destroyed and the pilot was fatally injured.
Probable cause:
The pilot-in-command's failure to maintain airspeed (vs) while maneuvering for a forced landing following an in flight left engine fire for undetermined reasons. Contributing to the accident was the pilot in command's inadvertent shutdown of the wrong engine.
Final Report:

Crash of a Piper PA-61 Aerostar (Ted Smith 601P) in Cockeysville: 2 killed

Date & Time: Apr 28, 1984 at 1507 LT
Registration:
N6079R
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Lancaster – Gainesville
MSN:
61P-0735-8063359
YOM:
1980
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
2500
Captain / Total hours on type:
105.00
Circumstances:
On the day of departure the pilot had received a 30 minutes familiarization flight upon completion of the superstar conversion. Emphasis was directed to engine gages, fuel flow and counter, and power settings. The flight was flown at 5,500 feet. The pilot then obtained a weather briefing and filed a flight plan. About 15 minutes after departure, while climbing thru FL170, the pilot radioed that he had lost both engines. The aircraft was subsequently observed descending uncontrolled out of the overcast. At about 1,000 feet agl the right aileron separated. The fuel boost pumps were found in the 'off' position. The AFM states that the boost pumps should be on during climb above 10,000 feet. The pilot had been enrolled in an Aerostar transition school the previous month during which a 2-hr combined demonstration/flight evaluation flight was conducted. The instructor pilot recommended further multi-engine training. Both occupants were killed.
Probable cause:
Occurrence #1: loss of engine power (total) - nonmechanical
Phase of operation: climb - to cruise
Findings
1. (c) flight manuals - not followed - pilot in command
2. (c) fluid, fuel - starvation
3. (c) fuel boost pump selector position - improper - pilot in command
4. (f) lack of total experience in type of aircraft - pilot in command
----------
Occurrence #2: loss of control - in flight
Phase of operation: climb - to cruise
Findings
5. (f) aircraft performance, two or more engines - inoperative
6. (c) aircraft handling - uncontrolled - pilot in command
7. (c) spatial disorientation - pilot in command
8. (f) inadequate recurrent training - pilot in command
----------
Occurrence #3: airframe/component/system failure/malfunction
Phase of operation: descent - uncontrolled
Findings
9. (c) flight control, aileron - overload
10. (c) design stress limits of aircraft - exceeded - pilot in command
11. Flight control, aileron - separation
----------
Occurrence #4: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report:

Crash of a Cessna 411A in Gainesville

Date & Time: Jan 12, 1984 at 1830 LT
Type of aircraft:
Registration:
N4500Q
Flight Type:
Survivors:
Yes
Schedule:
Conroe - Gainesville
MSN:
411-0300
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft crashed while on an ILS approach to the Gainsville Airport. Investigation revealed that the pilot had advised approach control that he was 'low on fuel.' After two missed approaches the pilot radioed that he was 'out of fuel.' The pilot did not have charts or approach plates aboard the aircraft, however ATC was not aware of this factor. Attempts to acquire additional information from the pilot have been unsuccessful. All three occupants escaped with minor injuries.
Probable cause:
Occurrence #1: loss of engine power(total) - nonmechanical
Phase of operation: approach - faf/outer marker to threshold (IFR)
Findings
1. (f) fluid,fuel - exhaustion
2. (c) preflight planning/preparation - improper - pilot in command
3. (c) fuel system - inadequate - pilot in command
4. (c) in-flight planning/decision - improper - pilot in command
----------
Occurrence #2: forced landing
Phase of operation: landing - flare/touchdown
Final Report:

Crash of a Cessna 401B in Gainesville

Date & Time: May 12, 1980 at 1936 LT
Type of aircraft:
Registration:
N7931Q
Survivors:
Yes
Schedule:
Jacksonville - Gainesville
MSN:
401B-0031
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5000
Captain / Total hours on type:
3.00
Circumstances:
On final approach to Gainesville Airport, both engines failed simultaneously. The airplane lost height, struck trees and crashed in high vegetation. Both occupants were seriously injured.
Probable cause:
Double engine failure on final approach due to inadequate preflight preparation. The following contributing factors were reported:
- Lack of familiarity with aircraft,
- Mismanagement of fuel,
- Inattentive to fuel supply,
- Fuel starvation,
- Fuel selector positioned between tanks,
- High vegetation,
_ Complete failure of both engines,
- Forced landing off airport on land,
- Auxiliary fuel tanks and left main empty,
- Right main fuel tank 10-15 gallons,
- Left engine fuel selector on left main tank,
- Right engine fuel selector between left main and right auxiliary tank.
Final Report: