Crash of a Douglas DC-10-10 in Sioux City: 111 killed

Date & Time: Jul 19, 1989 at 1600 LT
Type of aircraft:
Operator:
Registration:
N1819U
Survivors:
Yes
Schedule:
Denver - Chicago - Philadelphia
MSN:
46618
YOM:
1971
Flight number:
UA232
Crew on board:
11
Crew fatalities:
Pax on board:
285
Pax fatalities:
Other fatalities:
Total fatalities:
111
Captain / Total flying hours:
29967
Captain / Total hours on type:
7190.00
Copilot / Total flying hours:
20000
Copilot / Total hours on type:
665
Aircraft flight hours:
43401
Aircraft flight cycles:
16997
Circumstances:
United Flight 232 departed Denver-Stapleton International Airport, Colorado, USA at 14:09 CDT for a domestic flight to Chicago-O'Hare, Illinois and Philadelphia, Pennsylvania. There were 285 passengers and 11 crew members on board. The takeoff and the en route climb to the planned cruising altitude of FL370 were uneventful. The first officer was the flying pilot. About 1 hour and 7 minutes after takeoff, at 15:16, the flightcrew heard a loud bang or an explosion, followed by vibration and a shuddering of the airframe. After checking the engine instruments, the flightcrew determined that the No. 2 aft (tail-mounted) engine had failed. The captain called for the engine shutdown checklist. While performing the engine shutdown checklist, the flight engineer observed that the airplane's normal systems hydraulic pressure and quantity gauges indicated zero. The first officer advised that he could not control the airplane as it entered a right descending turn. The captain took control of the airplane and confirmed that it did not respond to flight control inputs. The captain reduced thrust on the No. 1 engine, and the airplane began to roll to a wings-level attitude. The flightcrew deployed the air driven generator (ADG), which powers the No. 1 auxiliary hydraulic pump, and the hydraulic pump was selected "on." This action did not restore hydraulic power. At 15:20, the flightcrew radioed the Minneapolis Air Route Traffic Control Center (ARTCC) and requested emergency assistance and vectors to the nearest airport. Initially, Des Moines International Airport was suggested by ARTCC. At 15:22, the air traffic controller informed the flightcrew that they were proceeding in the direction of Sioux City; the controller asked the flightcrew if they would prefer to go to Sioux City. The flightcrew responded, "affirmative." They were then given vectors to the Sioux Gateway Airport (SUX) at Sioux City, Iowa. A UAL DC-10 training check airman, who was off duty and seated in a first class passenger seat, volunteered his assistance and was invited to the cockpit at about 15:29. At the request of the captain, the check airman entered the passenger cabin and performed a visual inspection of the airplane's wings. Upon his return, he reported that the inboard ailerons were slightly up, not damaged, and that the spoilers were locked down. There was no movement of the primary flight control surfaces. The captain then directed the check airman to take control of the throttles to free the captain and first officer to manipulate the flight controls. The check airman attempted to use engine power to control pitch and roll. He said that the airplane had a continuous tendency to turn right, making it difficult to maintain a stable pitch attitude. He also advised that the No. 1 and No. 3 engine thrust levers could not be used symmetrically, so he used two hands to manipulate the two throttles. About 15:42, the flight engineer was sent to the passenger cabin to inspect the empennage visually. Upon his return, he reported that he observed damage to the right and left horizontal stabilizers. Fuel was jettisoned to the level of the automatic system cutoff, leaving 33,500 pounds. About 11 minutes before landing, the landing gear was extended by means of the alternate gear extension procedure. The flightcrew said that they made visual contact with the airport about 9 miles out. ATC had intended for flight 232 to attempt to land on runway 31, which was 8,999 feet long. However, ATC advised that the airplane was on approach to runway 22, which was closed, and that the length of this runway was 6,600 feet. Given the airplane's position and the difficulty in making left turns, the captain elected to continue the approach to runway 22 rather than to attempt maneuvering to runway 31. The check airman said that he believed the airplane was lined up and on a normal glidepath to the field. The flaps and slats remained retracted. During the final approach, the captain recalled getting a high sink rate alarm from the ground proximity warning system (GPWS). In the last 20 seconds before touchdown, the airspeed averaged 215 KIAS, and the sink rate was 1,620 feet per minute. Smooth oscillations in pitch and roll continued until just before touchdown when the right wing dropped rapidly. The captain stated that about 100 feet above the ground the nose of the airplane began to pitch downward. He also felt the right wing drop down about the same time. Both the captain and the first officer called for reduced power on short final approach. The check airman said that based on experience with no flap/no slat approaches he knew that power would have to be used to control the airplane's descent. He used the first officer's airspeed indicator and visual cues to determine the flightpath and the need for power changes. He thought that the airplane was fairly well aligned with the runway during the latter stages of the approach and that they would reach the runway. Soon thereafter, he observed that the airplane was positioned to the left of the desired landing area and descending at a high rate. He also observed that the right wing began to drop. He continued to manipulate the No. 1 and No. 3 engine throttles until the airplane contacted the ground. He said that no steady application of power was used on the approach and that the power was constantly changing. He believed that he added power just before contacting the ground. The airplane touched down on the threshold slightly to the left of the centerline on runway 22 at 16:00. First ground contact was made by the right wing tip followed by the right main landing gear. The airplane skidded to the right of the runway and rolled to an inverted position. Witnesses observed the airplane ignite and cartwheel, coming to rest after crossing runway 17/35. Firefighting and rescue operations began immediately, but the airplane was destroyed by impact and fire. The accident resulted in 111 fatal, 47 serious, and 125 minor injuries. The remaining 13 occupants were not injured.
Probable cause:
Inadequate consideration given to human factors limitations in the inspection and quality control procedures used by United Airlines' engine overhaul facility which resulted in the failure to detect a fatigue crack originating from a previously undetected metallurgical defect located in a critical area of the stage 1 fan disk that was manufactured by General Electric Aircraft Engines. The subsequent catastrophic disintegration of the disk resulted in the liberation of debris in a pattern of distribution and with energy levels that exceeded the level of protection provided by design features of the hydraulic systems that operate the DC-10's flight controls.
Final Report:

Crash of a Douglas DC-10-30 in Dallas

Date & Time: May 21, 1988 at 1612 LT
Type of aircraft:
Operator:
Registration:
N136AA
Flight Phase:
Survivors:
Yes
Schedule:
Dallas - Frankfurt
MSN:
47846
YOM:
1972
Flight number:
AA070
Crew on board:
14
Crew fatalities:
Pax on board:
240
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
15660
Captain / Total hours on type:
2025.00
Aircraft flight hours:
61322
Aircraft flight cycles:
12864
Circumstances:
A rejected takeoff was attempted when the slat disagree light illuminated and the takeoff warning horn sounded at 166 knots (V1). The pilot aborted the takeoff, but the aircraft accelerated to 178 knots ground speed before it began to decelerate. The deceleration was normal until 130 knots where an unexpected rapid decay in the deceleration occurred. The aircraft ran off the end of the runway at 95 knots, the nose gear collapsed, and the aircraft came to a stop 1,100 feet beyond the end of the runway. Eight of the ten brake sets failed. Post-accident exam of the brakes revealed that excessive brake wear occurred during the rejected takeoff. Testing showed that dc-10 worn brakes have a much greater wear rate during an rto. The faa does not require worn brake testing. Douglas did not use brake wear data from rto certification tests to set more conservative brake wear replacement limits. New brakes were used for those tests. All 254 occupants were evacuated, among them eight were injured, two seriously. The aircraft was damaged beyond repair.
Probable cause:
Occurrence #1: airframe/component/system failure/malfunction
Phase of operation: takeoff
Findings
1. (f) flt control syst, wing slat system - false indication
----------
Occurrence #2: airframe/component/system failure/malfunction
Phase of operation: takeoff - aborted
Findings
2. Aborted takeoff - attempted
3. Airspeed (v1) - exceeded
4. (c) landing gear, normal brake system - inadequate
5. (c) acft/equip, inadequate aircraft component - manufacturer
6. (c) inadequate substantiation process - manufacturer
7. (c) inadequate certification/approval, aircraft - faa (organization)
8. Landing gear, normal brake system - worn
9. (c) landing gear, normal brake system - failure, total
----------
Occurrence #3: overrun
Phase of operation: takeoff - aborted
Findings
10. Terrain condition - soft
11. Object - approach light/navaid
----------
Occurrence #4: nose gear collapsed
Phase of operation: takeoff - aborted
Final Report:

Crash of a Douglas DC-10-30 in Ilorin

Date & Time: Jan 10, 1987 at 1350 LT
Type of aircraft:
Operator:
Registration:
5N-ANR
Flight Type:
Survivors:
Yes
Schedule:
Lagos - Ilorin
MSN:
46968
YOM:
1977
Location:
Country:
Region:
Crew on board:
9
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Aircraft flight hours:
29487
Aircraft flight cycles:
8748
Circumstances:
The flight originated from Lagos, Nigeria, at 1320LT hours local time as a training flight. The training flight commenced from Lagos with the trainee Captain on the left seat as the Pilot Flying while the Instructor Captain was on the right seat as Pilot-in-Command. The point of intended landing and subsequent trainings was Ilorin Airport. Flight preparation was completed by the crew and ground dispatchers with 60.3 metric tonnes of fuel up-lift giving an estimated endurance of 8 hours. The flight was normal up till the altitude of 3,000 feet when the aircraft was inside the control zone of Ilorin Control Tower which had cleared the aircraft for a touch and go on runway 05. At 1,000 feet agl the aircraft had its landing gears in the down position and landing flaps set at 35°. At 400 feet agl the autopilot was disconnected and later at 80 feet the autothrottles were also disconnected. The aircraft was fully established on the ILS. As the trainee captain was on his very first flight on the aircraft type, the Nigeria Airways DC-10 flight transition syllabus item 9 has it that the sequence of training at this point in time should be '3 engine or single land demonstration-Full stop'. As the aircraft had already requested and cleared for a touch and go and established on ILS, it was clear that item 9 had been skipped and item 10 '3 engine Flight Director ILS approach -Touch and Go' was in progress. The trainee captain crossed the 05 threshold rather high at about 60 feet or more and a long time, interspersed with instructions by the instructor captain, was spent before the aircraft had its main landing gears on the ground at about 2,913 feet (888 m) from the threshold. Runway 05 had a Landing Distance Available if 3,100 meters. It appeared that the trainee captain did not recede the throttles fully back for the touchdown and the Instructor had to assist in doing so. The trainee captain then appeared to be holding the nosewheel off the ground and again the Instructor had to push the control column down. On nosewheel touchdown, the trainee immediately requested for takeoff power. The Instructor went into the aircraft reconfiguration procedure after the landing and was still busy on the required settings when the trainee Pilot raised an alarm as the runway threshold was approaching. The Instructor looked out into the 900m of slight haze visibility, felt that the aircraft would not takeoff with the limited runway available and immediately reached out to deploy the spoilers at the same time stepped on the brakes. Abort takeoff was not announced. At this point in time the engine throttles had already been advanced for takeoff. The aircraft was on heavy braking from about 1,390 feet (424 meters) before runway end as it overran the runway. The aircraft made significant impacts with the ILS antenna bars, electrical switch posts and the approach light support structures of runway 23 all located on the runway 05 clearway before it came to a halt. The location of the accident site was 44 meters to the left of the centreline and 649 meters along the extended centreline. A fire erupted and consumed the fuselage. All nine crew members escaped uninjured.
Probable cause:
The probable cause of the accident is primarily the amount of runway consumed in effecting the landing coupled with the lack of knowledge, with certainty of the position of the throttle levers by both the instructor and the trainee pilot in a crucial moment of deciding either to continue the takeoff or abort. The breakdown of communication and coordination between the instructor, the trainee pilot and the trainee flight engineer led to the subsequent overrun.
The following contributing factors were reported:
- The absence of uniform flight standards especially on procedures, within the Nigeria Airways Ltd. in that simulator trainings are not a progressive and logical sequence to flying the live aircraft.
- The extent of the accident was aggravated by the repeated collisions with solidly constructed approach light supporting structures which caused the fire and the shoddy performance of the airport fire services.
- The visibility was too close to the minima for a training flight.

Crash of a Douglas DC-10-30CF in Anchorage

Date & Time: Dec 23, 1983 at 1406 LT
Type of aircraft:
Operator:
Registration:
HL7339
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Seoul - Anchorage - Los Angeles
MSN:
46960
YOM:
1977
Flight number:
KE084
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
12562
Captain / Total hours on type:
6471.00
Copilot / Total flying hours:
8157
Copilot / Total hours on type:
2995
Circumstances:
While taxiing out in fog, the KAL crew became disoriented and ended up on the wrong runway. During the takeoff run, the aircraft collided head-on with South Central Air Flight 59, a Piper PA-31 which was taking off from runway 06L-24R for a flight to Kenai. The 9 occupants of N35206 were injured. The DC-10 overran the runway by 1434 feet and came to rest 40 feet right of the extended centreline.
Probable cause:
The failure of the pilot of Korean Air Lines Flight 084 to follow accepted procedures during taxi, which caused him to become disoriented while selecting the runway; the failure of the pilot to use the compass to confirm his position; and the decision of the pilot to take off when he was unsure that the aircraft was positioned on the correct runway. Contributing to the accident was the fog, which reduced visibility to a point that the pilot could not ascertain his position visually and the control tower personnel could not assist the pilot. Also contributing to the accident was a lack of legible taxiway and runway signs at several intersections passed by Flight 084 while it was taxiing.
Final Report:

Crash of a Douglas DC-10-30CF in Málaga: 50 killed

Date & Time: Sep 13, 1982 at 1200 LT
Type of aircraft:
Operator:
Registration:
EC-DEG
Flight Phase:
Survivors:
Yes
Schedule:
Madrid – Málaga – New York
MSN:
46962
YOM:
1977
Flight number:
BX995
Country:
Region:
Crew on board:
13
Crew fatalities:
Pax on board:
381
Pax fatalities:
Other fatalities:
Total fatalities:
50
Captain / Total flying hours:
16129
Captain / Total hours on type:
2119.00
Copilot / Total flying hours:
6840
Copilot / Total hours on type:
2165
Aircraft flight hours:
15364
Aircraft flight cycles:
4008
Circumstances:
Takeoff acceleration was normal, failure was not detected on engines, systems or structures. The crew registered a strong vibration at or close to V1. The captain felt how this vibration was highly increased as he began rotation, consequently rejecting the takeoff at a speed between VR and V2. Physical evidence shows how detachment of the tread of a tire of the nose gear, retreated, began before the aircraft had reached V1. The reject of takeoff began where there were another 1,295 meters (4,250 feet) of runway left. The aircraft crossed the runway end at a speed slightly over 110 knots, colliding with an ILS concrete building, breaking the metal fencing of the airport, crossing a highway, causing damage to three vehicles on the same, colliding then with farming construction. Engine number three detached after impact with the ILS building. Approximately three quarters of the right wing as well as the right horizontal stabilizer were detached as a result of the impact with the afore mentioned farming construction. The fuselage also ran over the construction with which the right wing collided. The aircraft stopped 450 meters (1,475 feet) away from the end of runway 14, and approximately 40 meters (130 feet) off to the left from the centerline. Neither the passenger department nor the cockpit showed damage that could impede survival when the aircraft stopped. Fuel was spilled off the right wing, from the time it collided with the farming construction, and the fire began in the rear of the fuselage. The fire destroyed the aircraft completely. There were 381 passengers and 13 crew members on board. 333 passengers and 10 crew survived, and as a result of the fire subsequent to the impact, 47 passengers and three assistant crew members died.
Probable cause:
The Commission determines the cause of the accident to be the fractional detachment of the retread of the right wheel of the nose gear, originating a strong vibration which could not be identified by the captain, leading him into the belief that the aircraft would become uncontrollable in flight, and thus deciding to abandon the take-off over VR. The decision of aborting the take-off, though not in accordance with the standard operation procedure, is in this case considered reasonable, on the base of the irregular circumstances that the crew had to face, the short period of time available to take the decision, the lack of training in case of wheel failure and the absence of take-off procedures when failure other than that of the engines occurs.
Final Report:

Crash of a Douglas DC-10-30CF in Boston: 2 killed

Date & Time: Jan 23, 1982 at 1936 LT
Type of aircraft:
Operator:
Registration:
N113WA
Survivors:
Yes
Schedule:
Oakland - Newark - Boston
MSN:
47821/320
YOM:
1980
Flight number:
WO30H
Crew on board:
12
Crew fatalities:
Pax on board:
200
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
18091
Captain / Total hours on type:
1969.00
Copilot / Total flying hours:
8600
Aircraft flight hours:
6327
Circumstances:
Following a non-precision instrument approach to runway 15R at Boston-Logan International Airport, the airplane touched down about 2,800 feet beyond the displaced threshold of the 9,191-foot usable part of the runway. About 1936:40, the airplane veered to avoid the approach light pier at the departure end of the runway and slid into the shallow water of Boston Harbor. The nose section separated from the fuselage in the impact after the airplane dropped from the shore embankment. Of the 212 persons on board, 2 persons are missing and presumed dead. The other persons onboard evacuated the airplane safely, some with injuries.
Probable cause:
The minimal braking effectiveness on the ice-covered runway; the failure of the Boston-Logan International Airport management to exercise maximum efforts to assess the condition of the runway to assure continued safety of landing operations; the failure of air traffic control to transmit the most recent pilot reports of braking action to the pilot of Flight 30H; and the captain's decision to accept and maintain an excessive airspeed derived from the auto throttle speed control system during the landing approach which caused the aircraft to land about 2,800 feet beyond the runway's displaced threshold. Contributing to the accident were the inadequacy of the present system of reports to convey reliable braking effectiveness information and the absence of provisions in the Federal Aviation Regulations to require:
- Airport management to measure the slipperiness of the runways using standardized procedures and to use standardized criteria in evaluating and reporting braking effectiveness and in making decisions to close runways.
- Operators to provide flight crews and other personnel with information necessary to correlate braking effectiveness on contaminated runways with aircraft stopping distances, and
- Extended minimum runway lengths for landing on runways which adequately take into consideration the reduction of braking effectiveness due to ice and snow.
Final Report:

Crash of a Douglas DC-10-30 on Ross Island: 257 killed

Date & Time: Nov 28, 1979 at 1250 LT
Type of aircraft:
Operator:
Registration:
ZK-NZP
Flight Phase:
Survivors:
No
Site:
Schedule:
Auckland - Christchurch
MSN:
46910/182
YOM:
1974
Flight number:
NZ901
Country:
Region:
Crew on board:
20
Crew fatalities:
Pax on board:
237
Pax fatalities:
Other fatalities:
Total fatalities:
257
Captain / Total flying hours:
11151
Captain / Total hours on type:
2872.00
Copilot / Total flying hours:
7934
Copilot / Total hours on type:
1361
Aircraft flight hours:
20763
Circumstances:
In preparation for Flight TE901 two of the pilots attended a route qualification briefing. This briefing consisted of an audio visual presentation, a review of a printed briefing sheet and a subsequent 45 minute flight in a DC 10 flight simulator for each pilot to familiarise him with the grid navigation procedures applicable to the portion of the flight south of 60o south latitude and the visual meteorological conditions (VMC) letdown procedure at McMurdo. This briefing was completed 19 days prior to the scheduled departure date. The briefing gave details of the instrument flight rules (IFR) route to McMurdo which passed almost directly over Mt Erebus, a 12450 ft high active volcano, some 20 nm prior to the most southerly turning point, Williams Field. It also stated that the minimum instrument meteorological conditions (IMC) altitude was 16000 ft and the minimum altitude after passing overhead McMurdo was 6000 ft providing conditions were better than certain specified minima well in excess of the standard VMC in New Zealand. On the day of the flight the crew participated in a normal pre-flight dispatch planning. At 1917 hours (Z) on 27 November 1979 Air New Zealand Flight TE 901, a DC10-30 (ZKNZP) departed from Auckland Airport on a non-scheduled domestic scenic flight which was planned to proceed via South Island New Zealand, Auckland Islands, Baleny Island, and Cape Hallett to McMurdo, Antarctica then returning via Cape Hallett and Campbell Island to Christchurch its first intended landing point. The flight was dispatched on an IFR computer stored flight plan route. The flight deck crew consisted of the captain, two first officers and two flight engineers. Beside the fifteen cabin crew there was an official flight commentator on the flight who was experienced in Antarctic exploration. The passenger load was reduced by 21 from the normal passenger seating capacity as a deliberate policy to facilitate movement about the cabin to allow passengers to view the Antarctic scenery. In a discussion with the McMurdo meteorological office at 0018 hours (Z) the aircraft crew was advised that Ross Island was under a low overcast with a base of 2000 ft and with some light snow and a visibility of 40 miles and clear areas approximately 75 to 100 nm northwest of McMurdo. At approximately 0043 hours (Z) Scott Base advised the aircraft that the dry valley area was clear and that area would be a better prospect for sightseeing than Ross Island. In response to the message that the area over the Wright and Taylor Valleys was clear the captain asked the commentator if he could guide them over that way. The commentator said that would be no trouble and asked if the captain wished to head for that area at the time. The captain replied he “would prefer here first”. The US Navy Air Traffic Control Centre (ATCC) “Mac Centre” suggested that the aircraft crew take advantage of the surveillance radar to let down to 1500 feet during the aircraft’s approach to McMurdo and the crew indicated their acceptance of this offer. In the event however the aircraft was not located by the radar equipment prior to initiating its descent (or at any other time). The aircraft crew also experienced difficulty in their attempts to make contact on the very high frequency (VHF) radio telephone (R/T)and the distance measuring equipment (DME) did not lock onto the McMurdo Tactical Air Navigation System (TACAN) for any useful period. The aircraft was relying primarily on high frequency (HF) R/T during the latter part of its flight for communication with the ATCC. The area which was approved by the operator for VMC descents below 16000 feet was obscured by cloud while ZK-NZP was approaching the area, and the crew elected to descend in a clear area to the north of Ross Island in two descending orbits the first to the right and the second to the left. Although they requested and were granted a clearance from “Mac Centre” to descend from 10000 to 2000 feet VMC, on a heading of 180 grid (013oT) and proceed “visually” to McMurdo, the aircraft only descended to 8600 feet before it completed a 180° left turn to 375°G (190°T) during which it descended to 5,700 feet. The aircraft’s descent was then continued to 1500 feet on the flight planned track back toward Ross Island. Shortly after the completion of the final descent the aircraft collided with Ross Island. The aircraft’s ground proximity warning system (GWPS) operated correctly prior to impact and the crew responded to this equipment’s warning by the engineer calling off two heights above ground level, 500 and 400 feet, and the captain calling for “go round power”. The aircraft’s engines were at a high power setting and the aircraft had rotated upwards in pitch immediately prior to impact. The aircraft collided with an ice slope on Ross Island and immediately started to break up. A fire was initiated on impact and a persistent fire raged in the fuselage cabin area after that section came to rest. The accident occurred in daylight at 0050 hours (Z) at a position of 77° 25’30” S and 167° 27’30” E and at an elevation of 1467 feet AMSL. The cockpit voice recorder (CVR) and digital flight data recorder (DFDR) established that the aircraft was operating satisfactorily and the crew were not incapacitated prior to the accident.
Probable cause:
The probable cause of this accident was the decision of the captain to continue the flight at low level toward an area of poor surface and horizon definition when the crew was not certain of their position and the subsequent inability to detect the rising terrain which intercepted the aircraft’s flight path. The following findings were reported:
- The flight planned route entered in the company’s base computer was varied after the crew’s briefing in that the position for McMurdo on the computer printout used at the briefing was incorrect by over 2 degrees of longitude and was subsequently corrected prior to this flight.
- The system of checking the detailed flight plan entries into the base computer was inadequate in that an error of 2° of longitude persisted in a flight plan for some 14 months,
- Some diagrams and maps issued at the route qualification briefing could have been misleading in that they depicted a track which passed to the true west of Ross Island over a sea level ice shelf, whereas the flight planned track passed to the east over high ground reaching to 12,450 feet AMSL,
- The briefing conducted by Air New Zealand Limited contained omissions and inaccuracies which had not been detected by either earlier participating aircrews or the supervising Airline Inspectors,
- The crew were not aware of the VHF R/T callsigns in use in the area and these are not published in the briefing notes, the NZAIP, or the US Department of Defence documents which were available to the crew. They were however specified in US Navy instruction CNSFA INST 3722.1, a copy of which was held by Operation Deep Freeze Headquarters,
- The question of making a landing near McMurdo on either the ice runway or the skiways at Williams Field and the type of emergencies which might require such a diversion was not discussed at the company’s briefing,
- The Civil Aviation Division Airline Inspectors had formally approved the audio visual stage of the route qualification briefing for the flight and one had witnessed a typical audio visual segment of the briefing for an Antarctic flight, twice, without requiring any amendments or detecting the errors contained in the briefing. They had also confirmed that it was no longer necessary for captains to carry out a supervised flight as required in the Operations Specifications in view of these briefings and the flight simulator detail,
- Civil Aviation Regulation 77 1(a) had not been complied with,
- The operator departed from the stated undertaking to carry two captains on each flight and substituted an additional first officer in lieu of the second captain,
- Of the flight deck crew only one engineer had flown to the Antarctic previously,
- The crew were not monitoring their actual position in relation to the topography adequately even though a continuous readout of the aircraft’s latitude and longitude and distance to run to the next waypoint was continuously available to them from the AINS,
-The crew did not observe the transition level in use in the McMurdo air traffic control area for resetting this aircraft’s altimeters and this procedure was not published in either the briefing notes or the US Department of Defence documents which were made available to the crew. The procedure used was that prescribed in US Federal Aviation Regulation 91.81 which required the QNH to be set basically at FL 180 during descent but this was modified in low pressure areas,
- The captain’s altimeter was not set to the correct QNH until the aircraft reached 3,500 feet,
- The captain initiated a descent to an altitude below both the IMC (16000 feet) and VMC (6000 feet) minima for the area in a cloud free area but in contravention of the operator’s briefing and outside the sector approved for the descent to 6000 feet by the DCA and the Company,
- The co-pilot was devoting a significant proportion of his time in an endeavour to establish VHF contact with the McMurdo ground stations and did not monitor the decisions of the pilot in command adequately in that he did not offer any criticism of the intention to descend below MSA in contravention of company restrictions and basic good airmanship,
- The descent was intentionally continued below the VMC limit specified by CAD and Air New Zealand Limited, of 6000 feet to an indicated 1500 feet,
- The crew were distracted but not preoccupied by their failure to raise the Ice Tower or any local ground station on VHF, the failure of the DME to lock on to the TACAN and the lack of any identification of the aircraft on radar,
- The company deleted an earlier requirement for VMC descents to be monitored by radar and substituted the alternative procedure of contacting the radar controller for co-ordination of the descent,
- The failure of the aircraft’s systems to establish satisfactory VHF contactor to “lock on” to the McMurdo TACAN was probably due to the aircraft’s low altitude in conjunction with significant high ground between the aircraft and the ground equipment,
- The flight engineers endeavoured to monitor the progress of the flight and expressed their dissatisfaction with the descent toward a cloud covered area,
- Although the route selected by Air New Zealand for the approach to McMurdo crossed almost directly over a 12450 ft active volcano just 20 miles from destination in preference to the normal approach path of military aircraft which was across the sea level ice shelf the Air New Zealand route was safe provided the crew observed the minimum altitudes stipulated for the flight and no extraordinary activity occurred in the volcano,
- Despite the shortcomings of some aspects of the route qualification briefing, this flight and Antarctic flights in general were not unacceptably hazardous, if they had been conducted strictly in accordance with the route qualification briefing as presented,
- The CAD procedure of reapproving Antarctic flights each season on the condition that they complied with the constraints of the previous season’s flights led to some items being discontinued without formal notification or agreement, e.g. the carriage of 2 captains on each flight, and the requirement for a briefing by ODF Headquarters,
- The on board navigation and flight guidance system operated normally during the latter stages of the flight,
- The aircraft’s GPWS operated in accordance with its design specifications,
- CAD had not implemented effectively the section of the ICAO standard detailed in Annex 6 of the convention which requires appropriate life-sustaining equipment to be carried on flights across land areas which have been designated by the State concerned as areas in which search and rescue would be especially difficult. Although the Commander of the USN Antarctic Support Force stated that “limited SAR capability existed over land and very little over water”, this may not constitute “designation of the area” as being especially difficult for search and rescue activities by the State concerned,
- Although some notes on Antarctic survival were given to the Chief Purser immediately before this flight no additional life-sustaining equipment was carried or training given to the crew members to facilitate survival following an emergency landing on the ice or in the polar waters of Antarctica,
- Neither the passengers nor the crew were expecting the collision and all received fatal injuries on impact with the ice,
- The search and rescue organisation was mobilised and co-ordinated in a competent manner despite the difficult environment and the aircraft was located as soon as practicable, (11 hours) after the collision occurred,
- The aircraft was not fitted with a self activated ELT but such equipment is not at present required,
- The aircraft’s CVR and DFDR operated as intended and provided an excellent record for the investigators of this accident. The CVR system however could be significantly improved as discussed in recommendation 8.
- The aircraft’s radar would have depicted the mountainous terrain ahead.
Final Report:

Crash of a Douglas DC-10-10 in Mexico City: 73 killed

Date & Time: Oct 31, 1979 at 0542 LT
Type of aircraft:
Operator:
Registration:
N903WA
Survivors:
Yes
Schedule:
Los Angeles - Mexico City
MSN:
46929/107
YOM:
1973
Flight number:
WA2605
Country:
Crew on board:
11
Crew fatalities:
Pax on board:
77
Pax fatalities:
Other fatalities:
Total fatalities:
73
Captain / Total flying hours:
31500
Captain / Total hours on type:
2248.00
Copilot / Total hours on type:
354
Aircraft flight hours:
24614
Aircraft flight cycles:
7345
Circumstances:
The airplane had taken off from Los Angeles International Airport, California, for Mexico City, at 0140LT on 31 October 1979. The Mexico centre had cleared the crew to approach Mexico City via Tepexpan, subsequently instructing the aircraft crew to change frequency to the control tower. The tower operator informed the crew that the runway in use was 23 Right and provided the crew with information on the weather conditions prevailing at Mexico City International Airport, and landing data. When the aircraft was on final approach, the control tower operator repeated that the runway in use was 23 Right and drew the attention of the pilot to the fact that he was left of the flight path he should be following to land on the runway in use. The pilot acknowledged the information and the fact that he was slightly to the left. The transcription of the magnetic tape which contains the communications between the control tower operator and the crew of aircraft N-903WA reveals that et one point the control tower operator asked the pilot whether he could see the approach lights on his left, to which the pilot replied "negative". The data obtained from the aircraft's flight recorder shows that the crew was making an instrument approach. The instrument landing procedure authorized in the aeronautical information publication (AIP) for Runway 23 Left with transition to 23 Right specifies that if the pilot does not have the runway in sight at 600 ft during an instrument landing approach, he must break off the approach and climb to 8 500 ft. In this case the crew continued with the landing procedure, ignoring the requirement to call out the altitude values and the decision minimum, and descended until the landing gear touched down off-centre of Runway 23 Left, which was closed to all operations. On the transcription of the cockpit voice recorder the pilot-in-command is heard to have said that he was on the flight path to Runway 23 Left, just before the left landing gear wheels touched down on the grass to the left of Runway 23 Left and the right landing gear wheels on the runway shoulder. The aircraft did not enter the runway until it had travelled some 100 m. According to the flight recorder data and the wheel traces at the site of the accident, the crew re-applied power for the go-around procedure and lifted the aircraft nose by 100-210. Now airborne, the aircraft's right landing gear collided with a truck located on the left shoulder of the runway which was closed for repairs. The impact left a distinct mark in the left-hand side of the vehicle's bonnet corresponding exactly to the shape and size of the aircraft's wheel. The collision with the truck, which was loaded with 10 tonnes of earth, removed the right landing gear leg with part or sections of the main gear beam to which it is attached, bursting three of the four tires. The two front tires came off the wheels, whose hubs disintegrated, scattering pieces away from the aircraft. The horizontal shaft which carries the two front wheels and the associated brake units also broke off and were projected forward over a distance of over 400 m. After breaking off, the right landing gear leg struck the right tailplane and elevator, severing the two almost completely. This caused the landing gear leg complete with the two rear tires, wheels and brake units to be thrown about 70 m beyond the point of collision with the truck. The left side panel of the truck's dumper body, the only part to break off, was thrown to the left of the runway; this panel bore traces of tires about halfway along its top edge. The inner right-hand section of the wing flaps also struck the dumper body, which removed the complete section; this was found to the right of the aircraft's flight path some 40 m beyond the final location of the dumper body. The underside of the flap was full of earth and the fractures in the structure contained earth from the truck. The right-hand side panel of the dumper body also bore evidence of having been struck by a metal object. The truck broke up completely and parts of it were scattered over a considerable distance on and off the runway, the area covered being some 400 m long by 100 m wide. Three seconds before the collision with the truck the engine throttles were opened. The collision occurred under these conditions and in spite of the violence of the impact the aircraft remained airborne and flew on, although lift was precarious due to the loss on the right side of the tailplane complete with elevator and the inner section of the wing flap. The aircraft was banked to the right and this inclination increased so much that when the aircraft was approximately 1 500 m from the threshold of Runway 23 Left, the outer section of the right wing flap struck the cab of an excavator which was parked parallel to the right-hand edge of Runway 23 Left. The impact completely destroyed the cab and parts of the trailing edge of the wing flap were found embedded in the twisted framework of the excavator. The aircraft continued, veering to the right and increasing its bank angle towards that side until the right wing tip was scraping Taxiway "A", leaving a deep score in the pavement, damaging a telephone manhole and destroying some taxiway edge lights. A severed section of the right wing was found deeply embedded in the ground at this point and the first signs of the fire which burned the nearby grass were also in this area. The distance from the marks left by the landing gear in the grass and on the runway shoulder 167 m from the threshold of Runway 23 Left, to the score made in Taxiway "A" by the right wing tip, is approximately 2 500 m, and over this entire distance the aircraft left no mark or trace on the ground, except a few metres beyond the excavator. From this point a score of constant depth and width had been made in the grass over a distance of about 70 m, possibly by something suspended underneath the aircraft. Small fragments of glass fibre, the material used for the trailing edges of the aircraft's control surfaces, were found along this score. The evidence above proves that the aircraft had remained airborne from the time it collided with the truck until reaching Taxiway "A", as confirmed by the flight recorder data. After the traces left by the right wing tip on Taxiway "A", scores of varying depths were made in Taxiway "Ptt by the aileron and the outer section of the right flap. A few metres further on the right wing collided with the corner of the PCV repair hangar, knocking down a pillar, a cross tie and part of the roof corner. Various aircraft components were found inside the hangar, e.g. the flap guides and hinges, sections of the leading edge of the right aileron, etc., besides the fuel which was spilled from the fractured wing onto a PCV under repair and on parked cars and vans. The collision of the right wing with the PCV repair hangar hardly interrupted the aircraft along its flight path and it finally crashed against the front of a building, which was demolished by the impact. This was the main impact, during which the tail fin complete with rudder and engine No. 2, the tail unit and the left tailplane with its elevator broke off, together with what remained of the right tailplane and elevator removed earlier by the right landing gear leg. The left wing was also severed at its attachment to the centre section and was thrown more than 200 m, turning over in the process and falling on a house outside the airport; part of this house was burned out. Engines No. 1 and 3 broke away from the wings and were destroyed by the impact and fire. 16 people were injured while 72 occupants, including nine crew members were killed as well as one people in the building.
Probable cause:
The accident was the consequence of the combination of the following factors:
- Non-compliance with the meteorological minima for the approach procedure, as cleared,
- Failure to comply with the aircraft's operating procedures during the approach phase,
- Landing on a runway closed to traffic,
- During the final approach to the runway assigned and having reached a height of 800 feet above the ground, the aircraft flew into a fog bank which concealed it from the control tower operator,
- The aircraft's crew did not comply with the procedural minima for the approach for which it had been cleared, in that the crew descended below the minima without reporting the runway in sight or initiating a go-around procedure,
- The crew never reported to the control tower operator that the runway was in sight and no landing clearance was therefore given,
- The data obtained from the cockpit voice recorder revealed that the crew did not comply with the operational procedures laid down in the relevant manuals, in particular the requirement to call out the altimeter readings during the final approach phase.
Final Report:

Crash of a Douglas DC-10-10 in Chicago: 273 killed

Date & Time: May 25, 1979 at 1504 LT
Type of aircraft:
Operator:
Registration:
N110AA
Flight Phase:
Survivors:
No
Schedule:
Chicago - Los Angeles
MSN:
46510/22
YOM:
1971
Flight number:
AA191
Crew on board:
13
Crew fatalities:
Pax on board:
258
Pax fatalities:
Other fatalities:
Total fatalities:
273
Captain / Total flying hours:
22500
Captain / Total hours on type:
3000.00
Copilot / Total flying hours:
9275
Copilot / Total hours on type:
1200
Aircraft flight hours:
19871
Circumstances:
American Airlines Flight 191, a McDonnell-Douglas DC-10-10, crashed on takeoff from Chicago-O'Hare International Airport, Illinois, USA. The aircraft was destroyed and all 271 occupants were killed. Additionally, two persons on the ground sustained fatal injuries. At 14:59 hours local time Flight 191 taxied from the gate at O'Hare Airport. The flight was bound for Los Angeles, California, with 258 passengers and 13 crew members on board. Maintenance personnel who monitored the flight's engine start, push-back, and start of taxi did not observe anything out of the ordinary. The weather at the time of departure was clear, and the reported surface wind was 020° at 22 kts. Flight 191 was cleared to taxi to runway 32R for takeoff. The company's Takeoff Data Card showed that the stabilizer trim setting was 5° aircraft nose up, the takeoff flap setting was 10°, and the takeoff gross weight was 379,000 lbs. The target low pressure compressor (N1) rpm setting was 99.4 percent, critical engine failure speed (V1) was 139 kts indicated airspeed (KIAS), rotation speed (VR) was 145 KIAS, and takeoff safety speed (V2) was 153 KIAS. Flight 191 was cleared to taxi into position on runway 32R and hold. At 15:02:38, the flight was cleared for takeoff, and at 15:02:46 the captain acknowledged, "American one ninety-one under way." The takeoff roll was normal until just before rotation at which time sections of the No.1 (left) engine pylon structure came off the aircraft. Witnesses saw white smoke or vapor coming from the vicinity of the No. 1 engine pylon. During rotation the entire No. 1 engine and pylon separated from the aircraft, went over the top of the wing, and fell to the runway. Flight 191 lifted off about 6,000 ft down runway 32R, climbed out in a wings-level attitude. About nine seconds after liftoff, the airplane had accelerated to 172 knots and reached 140 feet of altitude. As the climb continued, the airplane began to decelerate at a rate of about one knot per second, and at 20 seconds after liftoff, and an altitude of 325 feet, airspeed had been reduced to 159 knots. At this point, the airplane began to roll to the left, countered by rudder and aileron inputs. The airplane continued to roll until impact, 31 seconds after liftoff, and in a 112-degree left roll, and 21-degree nose down pitch attitude. At 15:04 Flight 191 crashed in an open field and trailer park about 4,600 ft northwest of the departure end of runway 32R. The aircraft was demolished during the impact, explosion, and ground fire. The No.1 engine pylon failure during takeoff was determined to have been caused by unintended structural damage which occurred during engine/pylon reinstallation using a forklift. The engine/pylon removal and reinstallation were being conducted to implement two DC-10 Service Bulletins. Both required that the pylons be removed, and recommended that this be accomplished with the engines removed. The Service Bulletin instructions assumed that engines and pylons would be removed separately, and did not provide instructions to remove the engine and pylon as a unit. Additionally, removal of the engines and pylons as a unit was not an approved Maintenance Manual procedure. The lack of precision associated with the use of the forklift, essentially an inability to perform the fine manipulations necessary to accomplish reinstallation of the engine/strut assembly, in combination with the tight clearances between the pylon flange and the wing clevis resulted in damage to the same part that had just been inspected. Inspections of other DC-10 pylon mounts following the accident resulted in nine additional cracked mounts being identified.
Probable cause:
The asymmetrical stall and the ensuing roll of the aircraft because of the uncommanded retraction of the left wing outboard leading edge slats and the loss of stall warning and slat disagreement indication systems resulting from maintenance-induced damage leading to the separation of the no.1 engine and pylon assembly procedures which led to failure of the pylon structure. Contributing to the cause of the accident were the vulnerability of the design of the pylon attach points to maintenance damage; the vulnerability of the design of the leading edge slat system to the damage which produced asymmetry; deficiencies in FAA surveillance and reporting systems which failed to detect and prevent the use of improper maintenance procedures; deficiencies in the practices and communications among the operators, the manufacturer, and the FAA which failed to determine and disseminate the particulars regarding previous maintenance damage incidents; and the intolerance of prescribed operational procedures to this unique emergency.
Final Report: