Crash of a Beechcraft 65 Queen Air near Orlando: 5 killed

Date & Time: Dec 19, 1992 at 0739 LT
Type of aircraft:
Registration:
N555GC
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Sanford – Fort Lauderdale
MSN:
LC-164
YOM:
1965
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
8269
Captain / Total hours on type:
40.00
Aircraft flight hours:
3700
Circumstances:
Pilot reported level at 6,000 feet; no further transmissions were received. Radar data shows that after 5 minutes at cruise flight ground speed began to slow, and as speed reached 85 knots (VMC is 83 knots) aircraft made a rapid turn to the left and the speed dropped to 74 knots. Radar contact was then lost. Witnesses reported hearing and seeing aircraft with an engine sputtering and quitting, at which time no engine noise was audible. Engine would then restart, and at one point aircraft was observed initiating a climb after engine start. Engine restarted and obtained near full power, and a short time later sound of impact was heard. The left engine fuel servo was found contaminated with corrosion and dirt, and would not allow fuel flow to the engine. The fuel strainer for this engine was installed backwards allowing unfiltered fuel to enter the engine. The left propeller was not feathered and had no signs of rotation under power. Right engine fuel servo also contained corrosion and contamination. The aircraft did not have a current annual inspection. All five occupants were killed.
Probable cause:
The pilot's failure to feather the propeller to maintain altitude following a loss of power of the left engine. The power loss was due to an improperly maintained fuel system. In addition, the right engine lost power for an undetermined reason(s).
Final Report:

Crash of a Beechcraft B65 Queen Air near Madison: 2 killed

Date & Time: May 16, 1992 at 1400 LT
Type of aircraft:
Registration:
N30RR
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Allentown - Charlottesville
MSN:
LC-186
YOM:
1965
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
6003
Circumstances:
The instrument rated pilot was en route to his granddaughter's graduation exercises scheduled for the following day. He had received two preflight weather briefings from flight service and he was advised that marginal VFR conditions existed en route, and instrument meteorological conditions at his destination, and that VFRflight was not recommended. A witness who was below the mountain said he heard a low flying aircraft overhead. He stated that he caught a glimpse of the airplane and said it was 'well below the crest of the mountain' heading south. The weather as reported by the witness was about 200 overcast and visibility below 1 mile in fog. He also mentioned that the clouds had obscured the mountain. Shortly thereafter, he heard what was later determined to be the collision. Search personnel located the burning wreckage on top of Mitchells mountain 50 miles north of Charlottesville. Both occupants were killed.
Probable cause:
The pilot initiated VFR flight into known adverse weather conditions. Contributing to the accident was low ceiling, high terrain, and low altitude.
Final Report:

Crash of a Beechcraft 65 Queen Air in Meridian

Date & Time: Jul 17, 1991 at 1702 LT
Type of aircraft:
Registration:
N711SF
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Meridian – Tuscaloosa
MSN:
LC-139
YOM:
1962
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
943
Captain / Total hours on type:
34.00
Aircraft flight hours:
9200
Circumstances:
The pilot reported that shortly after takeoff the aircraft yawed to the right, left then right again. The passenger in the copilot seat stated the right engine rpm gauge indication needle was fluctuating. The pilot positioned the right engine mixture control to idle cutoff and the propeller control to feather. The propeller continued to windmill. Unable to maintain altitude, the pilot attempted to land on a highway but the aircraft collided with an unmarked power line, light pole, then the ground and was destroyed by a post crash fire. The right engine was recovered and due to impact damage, the propeller and fuel servo were replaced. The engine was placed on a test stand and was started and found to operate normally. The prop governor and damaged fuel servo were tested and found to operate normally. The damaged propeller was inspected and found to be free of preimpact failure or malfunction. No determination could be made as to the reason for the reported power fluctuation from the right engine. A witness stated gear retraction was delayed after takeoff.
Probable cause:
Loss of power from the right engine due to undetermined reasons. The failure of the propeller to feather was a factor in the accident.
Final Report:

Crash of a Beechcraft 65 Queen Air in Pioneer: 6 killed

Date & Time: Jun 30, 1991 at 0911 LT
Type of aircraft:
Registration:
N713JB
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Modesto – South Lake Tahoe
MSN:
LC-35
YOM:
1960
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
2830
Captain / Total hours on type:
27.00
Aircraft flight hours:
4958
Circumstances:
A Beech 65 collided with trees in mountainous terrain after an inflight loss of control. A pilot observed the airplane start a turn to the right, roll right and continued until inverted and enter into a spin. The aircraft was in a steep nose down attitude when it began its pull out. The engines were heard by a ground witness who initially mistook them for an approach motorcycle. The pilot initially flew the aircraft 45 days before the accident and logged 3.5 dual instruction hours. There was no record in the pilot's logbook of any additional flight training since the initial flight. The pilot satisfactorily completed a before in a Cessna 150 four days before the accident. Examination of the wreckage disclosed the right engine had broken exhaust valve, but the left propeller was feathered. There were no preexisting mechanical malfunctions or failures found with the left engine. The aircraft was destroyed and all six occupants were killed.
Probable cause:
Improper emergency procedures by the pilot, when he inadvertently shut down the left engine after encountering a partial loss of power in the right engine. Factors related to the accident were: improper installation of the right engine's #6 exhaust valve seat by other maintenance personnel, fatigue failure of the #6 exhaust valve, and the pilot's lack of familiarity with the aircraft.
Final Report:

Crash of a Beechcraft 65 Queen Air in Leonardtown

Date & Time: Jun 2, 1991 at 1130 LT
Type of aircraft:
Operator:
Registration:
N655KJ
Flight Phase:
Survivors:
Yes
Schedule:
Leonardtown - Leonardtown
MSN:
LC-129
YOM:
1962
Crew on board:
1
Crew fatalities:
Pax on board:
11
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2350
Captain / Total hours on type:
150.00
Aircraft flight hours:
6000
Circumstances:
The pilot reported that shortly after takeoff on a parachute jumping flight the left engine lost power, but a second later power was restored. Soon afterwards a total power loss occurred. According to the pilot, the propeller stopped rotating and did not windmill. He did not feather the left propeller. He made a shallow left turn toward an open field, while trying to return to the airport. He was unable to maintain adequate airspeed or altitude, and in order to maintain aircraft control, he reduced power on the right engine. He made a forced landing in a wheat field. The airplane came to a stop and all occupants escaped the airplane before it caught fire. The examination of the airplane did not disclose evidence of mechanical malfunction.
Probable cause:
The loss of power in one engine for undetermined reasons.
Final Report:

Crash of a Beechcraft 65 Queen Air in Nassau

Date & Time: Apr 29, 1989 at 0135 LT
Type of aircraft:
Registration:
N824Q
Flight Type:
Survivors:
Yes
Schedule:
Santa Ana - Nassau
MSN:
LC-28
YOM:
1960
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed while approaching Nassau Airport by night on a flight from Santa Ana, California. Both occupants were injured.

Crash of a Beechcraft 65 Queen Air in Elko: 2 killed

Date & Time: Nov 2, 1988 at 1453 LT
Type of aircraft:
Registration:
N9AG
Flight Type:
Survivors:
No
Schedule:
Elko - Farmington
MSN:
LC-51
YOM:
1960
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
884
Captain / Total hours on type:
103.00
Aircraft flight hours:
8945
Circumstances:
Approximately 10 minutes after takeoff, the pilot stated he was returning to land due to a problem. On final the aircraft rolled inverted and descended nose down into a residence. Engine examination revealed a failed supercharger intermediate drive shaft gear resulting in loss of supercharger on the right engine. The aircraft was approximately 300 lbs over max gross weight. The landing gear was down and the flaps were extended approx 20°. The left throttle was found in the full forward (high power) position. The right prop control was in full decrease rpm, high pitch and the right engine magneto switches were off. Witnesses had observed the aircraft descend to below traffic pattern altitude. At approx 200 feet agl a loud engine noise was heard and the slow flying aircraft pitched up, rolled right and descended vertically about 1/2 mile from the airport. The pilot had not declared an emergency or defined his problem. The pilot's last recorded flight in the Beech 65 was in February 1988. There was no record of a check-out or flight training in the aircraft. Both occupants were killed.
Probable cause:
Occurrence #1: loss of engine power (partial) - mech failure/malf
Phase of operation: climb - to cruise
Findings
1. (f) accessory drive assy, drive gear - worn
2. (f) exhaust system, turbocharger - failure, total
----------
Occurrence #2: loss of control - in flight
Phase of operation: approach - vfr pattern - final approach
Findings
3. (f) weather condition - gusts
4. (c) in-flight planning/decision - inadequate - pilot in command
5. (c) airspeed (vmc) - not maintained - pilot in command
6. (f) inadequate training (emergency procedure(s)) - pilot in command
7. (f) lack of recent experience in type of aircraft - pilot in command
8. (f) aircraft weight and balance - exceeded - company/operator management
----------
Occurrence #3: in flight collision with object
Phase of operation: descent - uncontrolled
Findings
9. Object - residence
Final Report:

Crash of a Beechcraft A65 Queen Air in Winnipeg

Date & Time: Jul 31, 1987
Type of aircraft:
Operator:
Registration:
C-GKDX
Flight Phase:
Survivors:
No
Site:
MSN:
LC-271
YOM:
1968
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Shortly after takeoff from Winnipeg Airport, the pilot encountered engine problems. The aircraft lost height and crashed on a factory located near the airport. The aircraft was destroyed but all five occupants were rescued.

Crash of a Beechcraft 65 Queen Air off Key Largo

Date & Time: Mar 3, 1987
Type of aircraft:
Registration:
N822Q
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
LC-42
YOM:
1960
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft was found crashed in shallow water near Key Largo, FL. Attempts to locate the pilot or current operator were fruitless. The circumstances surrounding the crash and the cause are unknown.
Probable cause:
Occurrence #1: miscellaneous/other
Phase of operation: unknown
Findings
1. (c) reason for occurrence undetermined
2. (f) flt with inadequate en route/destination facilities - performed - pilot in command
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: landing
Findings
3. (f) terrain condition - water, glassy
Final Report:

Crash of a Beechcraft 65 Queen Air in Montague: 1 killed

Date & Time: Apr 5, 1986 at 1430 LT
Type of aircraft:
Registration:
N810Q
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Oklahoma City - Bowie
MSN:
LC-26
YOM:
1960
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
10624
Captain / Total hours on type:
50.00
Aircraft flight hours:
5779
Circumstances:
The pilot was observed in the area for several minutes while he was performing steep climbs and descents, low passes, and buzzing. Witnesses reported power was removed from both engines simultaneously, as if the throttles were retarded, followed by a loud pop. The aircraft began to wobble slightly and then a surge of engine power was heard only seconds before tree impact occurred. The aircraft then yawed sharply and impacted the ground. The wreckage was found near Montague, about five miles northeast of Bowie Airport, the intended destination. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: loss of control - in flight
Phase of operation: maneuvering
Findings
1. (c) airspeed - not identified - pilot in command
2. (f) low pass - performed - pilot in command
3. (f) buzzing - performed - pilot in command
4. (f) overconfidence in personal ability - pilot in command
5. (f) ostentatious display - pilot in command
----------
Occurrence #2: in flight collision with object
Phase of operation: maneuvering
Findings
6. (c) object - tree(s)
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report: