Country
code

São Paulo

Crash of a Embraer EMB-820C Navajo in São Paulo: 1 killed

Date & Time: Jun 5, 2001 at 2030 LT
Registration:
PT-EHL
Flight Type:
Survivors:
No
Site:
Schedule:
Franca – São Paulo
MSN:
820-048
YOM:
1977
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2000
Captain / Total hours on type:
600.00
Aircraft flight hours:
5289
Circumstances:
The aircraft departed Franca Airport in the evening on a cargo flight to São Paulo, carrying one pilot and bank notes. On a night approach to São Paulo-Congonhas Airport, the pilot cancelled the IFR flight plan when he encountered technical problems with the right engine. He shut down the engine and continued the approach to runway 35R without informing ATC of his situation. Too high on the glide, he apparently decided to initiate a go-around when he lost control of the aircraft that rolled to the left, lost height and crashed in a residential area, bursting into flames. The aircraft was destroyed and the pilot was killed. Two people on the ground were injured.
Probable cause:
It was determined that the hydraulic pump on the right engine failed in flight, forcing the pilot to shut the engine down. It was reported that the pilot continued the approach in a single-engine configuration without informing ATC and that the aircraft was too high on the glide and approaching with an excessive speed. The pilot improperly analyzed the aircraft's flight conditions after shutting down the right engine, causing the aircraft to enter an approach configuration that was not compliant with the published procedures.
Final Report:

Crash of a Boeing 707-331C in São Paulo

Date & Time: Mar 7, 2001 at 0030 LT
Type of aircraft:
Operator:
Registration:
PT-MST
Flight Type:
Survivors:
Yes
Schedule:
Belém – Brasilía – São Paulo
MSN:
18711
YOM:
1964
Flight number:
SKC9101
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4200
Captain / Total hours on type:
2543.00
Copilot / Total flying hours:
3858
Copilot / Total hours on type:
361
Aircraft flight hours:
70422
Aircraft flight cycles:
28047
Circumstances:
The aircraft was completing a cargo flight from Belém to São Paulo with an intermediate stop in Brasilía, carrying three crew members and a load of various goods such as mail and fish. While descending to São Paulo-Guarulhos Airport in good weather conditions at an altitude of 10,000 feet, the crew encountered technical problems with the trim system. Several manual controls and tests were conducted and the system worked before failing again between 6,000 and 4,700 feet. The captain decided to continue the approach but the aircraft became unstable and nosed down on short final. It landed hard on runway 09R, causing the undercarriage to be torn off. The aircraft slid for about 1,000 metres then veered off runway to the left and came to rest in a grassy area. All three crew members escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
The exact cause of the technical problems on the trim system could not be determined with certainty. The following contributing factors were identified:
- The decisions of the crew and more particularly of the captain during the last phase of flight were incorrect,
- The crew training program for emergency situation was incomplete,
- Improper use of flaps and slats on final approach made the situation worse,
- The captain did not follow the procedure determined for such an emergency situation and decided to continue the approach maneuver, increasing the risk margin and placing the airplane in critical operating conditions,
- Due to deviations from the published standard operational procedures, such as failure to complete the approach briefing and not following the approach checklist, the coordination among the flight crew was poor, leading to further deviations and putting the crew in a critical situation.
Final Report:

Crash of a Rockwell 681BT Turbo Commander in São Paulo: 7 killed

Date & Time: Dec 16, 2000 at 2120 LT
Registration:
PT-IEE
Flight Phase:
Survivors:
No
Site:
Schedule:
São Paulo – Maringá
MSN:
681-6071
YOM:
1972
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
5000
Captain / Total hours on type:
600.00
Copilot / Total flying hours:
2500
Copilot / Total hours on type:
200
Circumstances:
After takeoff from runway 17 at São Paulo-Congonhas Airport, the crew was cleared to climb to 5,500 feet maintaining heading 270. Weather conditions were poor with clouds, atmospheric turbulences and strong winds. At an altitude of 5,300 feet, the aircraft lost height and descended to 4,700 feet, an altitude that was maintained for 17 seconds. Then the aircraft entered an uncontrolled descent and crashed in four houses located in the district of Vila Anhanguera, about 5,5 km southwest of the airport. The aircraft and all four houses were destroyed. All seven occupants were killed while on the ground, six people were injured, one seriously.
Probable cause:
The accident occurred in poor weather conditions. It was determined that during initial climb, the aircraft's attitude, speed and altitude varied suddenly and rapidly, causing the pilot flying a stressful situation insofar as he believed that artificial horizons presented technical problems. In such a situation, investigators consider probable the hypothesis that the pilot made inadequate corrections, exacerbating the abnormal situation in which he was operating. The following contributing factors were identified:
- The crew were suffered fatigue because they had been on duty for more than 15 hours and were unable to observe satisfactory rest time at Congonhas airport,
- This fatigue certainly affected the pilots in their decision-making,
- The urge to return home and distrust of instruments in difficult flight conditions seriously compromised the performance of pilots and their ability to make decisions,
- A direct contact with passengers was stressful as they were going through a period of mourning and were eager to return home to Maringá,
- Weather conditions were unfavorable and contributed to the anxiety of the crew,
- Poor assessment of these conditions by the pilots,
- The working time of the pilots exceeded the limitations and the operator did not take into account adequate rest conditions for the crew,
- The training of the captain in instrument flights in recent months was insufficient.
Final Report:

Crash of a Learjet 24D in Ribeirao Preto: 5 killed

Date & Time: Apr 7, 1999 at 1147 LT
Type of aircraft:
Registration:
PT-LEM
Flight Type:
Survivors:
No
Schedule:
São Paulo - Ribeirão Preto
MSN:
24-270
YOM:
1973
Country:
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
4000
Captain / Total hours on type:
4000.00
Copilot / Total flying hours:
6000
Copilot / Total hours on type:
100
Circumstances:
The aircraft departed São Paulo-Congonhas on a training flight to Ribeirão Preto-Leite Lopes Airport, carrying five crew members, instructor and pilots. On final approach to runway 18, during the last segment, just prior to touchdown, the aircraft rolled to the right, causing the right wing tip to struck the runway surface. The pilot-in-command overcorrected, the aircraft went out of control and crashed 420 metres past the first impact, bursting into flames. All five occupants were killed.
Probable cause:
Contributing Factors:
- There was the participation of individual psychological variables in the pilot-in-command's performance due to the excess of self-confidence and self-demand in his customary behavior, besides the dissimulation regarding his real qualification for the type of flight. The personality with traces of permissiveness and insecurity of the co-pilot also contributed to the occurrence, as it allowed the aircraft to be operated by an unqualified pilot, with no employment link with the company.
- There was a lack of adequate supervision by Manacá Táxi Aéreo, as it allowed a crew member who had not operated the type of aircraft for one year and had not made any type of flight for four months, besides not having any employment relationship with that company. It is also necessary to consider the failure of supervision at the organizational level due to the issue of an incorrect license by the DAC, giving rise to the possibility of its use for the revalidation of license in aircraft for which the pilot was not qualified to exercise the function of commander.
- The entire sequence of events began with pilot errors resulting from the pilot's lack of flight experience in the left-hand seat on the aircraft in question.
- The inadequate use of cockpit resources destined to the aircraft operation, due to an ineffective accomplishment of the tasks assigned to each crew member, besides the interpersonal conflict resulting from the co-pilot's intervention in the pilot in command operation, in the final approach phase, already close to the aircraft's touchdown, configure the collaboration of this factor to the accident.
- The inadequate use of the aircraft commands, by the pilot in command, making excessive aileron corrections in the final approach phase, near the landing.
- The pilot was qualified as a co-pilot on the equipment, but due to a typing error, he was issued a pilot license. Thus, the situation and operation of the pilot in question were totally irregular.
Final Report:

Crash of a Beechcraft A90 King Air in Franca: 2 killed

Date & Time: Mar 23, 1999 at 1910 LT
Type of aircraft:
Registration:
PT-OUL
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Franca – Ribeirão Preto
MSN:
LJ-125
YOM:
1966
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3500
Captain / Total hours on type:
650.00
Copilot / Total flying hours:
206
Circumstances:
Less than a minute after takeoff from Franca Airport, while climbing in poor weather conditions, the twin engine aircraft nosed down and crashed in a huge explosion about 1,500 metres past the runway end. The aircraft was destroyed and both pilots were killed. They were completing a cargo flight to Ribeirão Preto, carrying documents on behalf of Banco do Brasil.
Probable cause:
The following findings were identified:
- The crew was in a hurry to take off in order to avoid poor weather approaching the airport,
- The crew took off from an intersection with a taxiway,
- Immediately after takeoff, the aircraft entered clouds,
- Approximately one minute after liftoff, the aircraft impacted ground,
- After the first impact, the aircraft flew for another 200 metres and again collided with the ground and exploded,
- The aircraft was totally destroyed by a post crash fire,
- The pilot had a hearing problem that was stabilized and was being researched by HASP. Considering the relationship between ear and ear balance, spatial disorientation in the pilot in
in the face of the adverse conditions it experienced: flight conditions by instruments associated with “windshear”. Since the search could not be completed above mentioned, this aspect remains undetermined,
- Individual characteristics contributed due to the habits acquired by the pilot and his eventual practice of taking off from the taxiway, delaying the point from which the aircraft would achieve the best characteristics flight performance,
- Poor weather conditions with CB's, sudden changes in wind, strong turbulence and rain, were conducive to the emergence of the phenomenon of “Windshear”, representing a real risk to the operation of any aircraft, being that voluntary entry or not, in this type of training, results almost always in the loss of control of the aircraft with unforeseeable consequences. The crew faced these conditions when the aircraft took off,
- It was evident from the witness statements that the pilot was in a hurry to take off, in addition to having used runway 23 from the intersection and towards the sector most affected by poor weather.
Final Report:

Crash of a Mitsubishi MU-2B-25 Marquise in São Paulo

Date & Time: Jul 10, 1998
Type of aircraft:
Operator:
Registration:
PT-LTC
Flight Phase:
Survivors:
Yes
MSN:
314
YOM:
1975
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
During the takeoff roll at São Paulo-Congonhas Airport, the crew encountered an engine failure and decided to abort. The airplane was stopped on the main runway and all five occupants escaped uninjured. However, debris punctured a fuel tank and the aircraft caught fire and was severely damaged by fire and later written off.
Probable cause:
Uncontained failure on takeoff for unknown reasons.

Crash of a Fokker 100 in São Paulo: 99 killed

Date & Time: Oct 31, 1996 at 0827 LT
Type of aircraft:
Operator:
Registration:
PT-MRK
Flight Phase:
Survivors:
No
Site:
Schedule:
São Paulo – Rio de Janeiro
MSN:
11440
YOM:
1993
Flight number:
KK402
Country:
Crew on board:
6
Crew fatalities:
Pax on board:
89
Pax fatalities:
Other fatalities:
Total fatalities:
99
Captain / Total flying hours:
6433
Captain / Total hours on type:
2392.00
Copilot / Total flying hours:
3000
Copilot / Total hours on type:
230
Aircraft flight hours:
8171
Circumstances:
TAM flight 402 was a regular flight between São Paulo (CGH) and Rio de Janeiro (SDU). At 08:25 the flight received clearance for takeoff from runway 17R. Wind was given as 060 degrees. At 08:26:00 the throttles were advanced for takeoff power. Ten seconds later a double beep was heard. The captain said "O auto-throttle tá fora" and the copilot adjusted the throttles manually and informed the captain: "thrust check". With this information he confirmed that the takeoff power had been adjusted and verified. At 08:26:19 the airplane accelerated through 80 kts. At 08:26:32 the copilot indicated "V one". Two seconds later the airplane rotated at a speed of 131 kts. At 08:26:36 the air/ground switch transited from "ground" "to "air". The speed was 136 kts and the airplane was climbing at an angle of 10 degrees. At that same moment a shock was felt and the EPR of engine no. 2 dropped from 1.69 to 1.34, indicating the loss of power. In fact, the no. 2 engine thrust reverser had deployed. An eye witness confirmed to have seen at least two complete cycles of opening and closing of the no. 2 thrust reverser buckets during the flight. The loss of power on the right side caused the plane to roll to the right. The captain applied left rudder and left aileron to counteract the movement of the plane. The copilot advanced both thrust levers, but they retarded again almost immediately, causing the power of the no. 1 engine to drop to 1.328 EPR and engine no. 2 to 1,133 EPR. Both crew members were preoccupied by the movement of the throttles and did not know that the thrust reverser on the no. 2 engine had deployed. The throttles were forced forward again. At 08:26:44 the captain ordered the autothrottle to be disengaged. One second later the no. 2 thrust lever retarded again and remained at idle for two seconds. The airspeed fell to 126 kts. At 08:26:48 the copilot announced that he had disengaged the autothrottles. He then jammed the no. 2 thrust lever fully forward again. Both engines now reached 1,724 EPR. With the thrust reverser deployed, the airspeed declined at 2 kts per second. At 08:26:55 the stick shaker activated, warning of an impeding stall. The airplane rolled to a 39 degree bank angle and the GPWS activated: "Don't sink!". Seven seconds later the airplane impacted a building and crashed into a heavily populated neighborhood.
Probable cause:
The following findings were reported:
a. Contributing Factors
Psychological Aspect - Contributed
a) organizational aspect
The lack of information, instructions in writing and practice, contributed to the non-recognition of the abnormality during its unfolding.
b) Individual aspect
The unusual occurrence of the quick reduction of the lever, on a particularly difficult phase of the operation (transition from take-off run to flight); the nonoccurrence of failure discriminating (sound and visual) warnings, and the lack of cognizance and specific training for such abnormality bring on surprise and distraction of the crew members' attention.
- The release of the restriction of the lever of engine 2 at the idle detent without the occurrence of the abnormality warnings strengthened the tendency (in at least one of the crew members) to try to recover the power on the engine.
- The lack of warnings and the difficulties that are characteristic of such abnormality have diverted the crew members' concentration from the procedures provided for, to concentrate it on the solution of the abnormality, initially imagined as being an auto-throttle failure, and later the recovery of thrust
- The occurrence of auto-throttle failure warnings (before the 80 Kt) and the lack of specific reverse opening warnings (Master Caution and RSVS UNLK) have strengthened, in the crew members, the belief that they were experiencing an autothrottle failure (illusion).
b. Material Factor
(1). Desing Deficiency - Contributed
The reverser fault tree chart made recently by the manufacturer considering the Post-Mod version, even not taking into account a dormant fail, has indicated that the probability of an inadvertent opening of the reversers is of the order of 10"6. The Post-Mod version does not meet the airworthiness requirements of FAR/RBHA 25.1309.
On two phases of the complete reversers cycle, at the beginning of the opening and at the end of the shell closing, it is possible to apply power higher than IDLE with the shells partially open, which does not meet RBHA/FAR 25.933.
The reverser unlocked indication system is inhibited at speeds higher than 80 Kt and up to the height of 1000 feet, exactly at an instant when the pilots would need such information most.
The SECONDARY LOCK ACTUATORS (S/N 874 and S/N 870) that equipped the aircraft that suffered the accident, on the operational tests proposed and carried out, presented a performance much below the minimum acceptable to assure the safety and reliability of the system.
The applicable FAR 25.993(a)(3) requirements determine that each [reverse] system is to be provided with means to prevent the engine from producing power higher than idle power upon a failure on the reverse system [not stipulating the type of failure]. Such requirement has not been complied with, both in relation to the control system, which permitted the shells to open in flight, and in relation to protection, which became non-existent when the separation of the FEEDBACK CABLE occurred due to the unpredicted pilot's action on the lever, with the intention of recovering the power of the affected engine.
The TURNBUCKLE is installed on the side to which the connection moves when the reverser is commanded to open, i.e., the same side towards which the connection moves when the situation occurs in which the lever is forcibly held forward while the reverser is opening (deploying).
The THRUST SELECTOR VALVE may be moved with less than 2% of the normal functioning pressure, when the selector valve is de-energized, which was the condition at the time of the accident.
The inductive loads as those of SEC. LCK. ACTUATOR are detrimental to the contacts that command them, particularly on de-energization, in case there is no protection diode, which is apparently the case of SEC. LCK. ACTUATOR.
The THRUST REVERSER ACTUATOR, in the Post-Mod configuration, incorporated to the assembly line by the manufacturer, remains de-energized during the periods in which there is no commanding by the pilot, and this way it stays in an unstable and dangerous situation.
Design faults, an insufficient assessment of the fault tree diagram as compared to FAR 25.1309 and 25.933, and in the guidance to the operator not to train the abnormality that occurred on that phase, have indirectly contributed to the sequence of events that led to place the crew facing an unprecedented situation, without possibilities of recognizing and responding properly to avoid the loss of control.
c. Operational Factor
(1). Little experience on the aircraft - Indeterminate
Limitation of information and aids to the pilot. He had 230:00 total flight hours on this aircraft model, however the condition under which the unusual abnormality presented itself renders indeterminate the degree of experience that may be expected from a crew member to face such condition.
(2). Deficient Application of Control - Indeterminate
For three times, the thrust lever of engine 2 has been reduced and advanced. Such interventions on that lever have brought on the reduction of the thrust lever of the left hand engine, impairing the aircraft's performance. The non-return of the left hand lever to take-off thrust immediately, and the another four seconds delay in attaining such thrust, have contributed to deteriorate even more the aircraft's climbing capability.
The condition under which the unusual abnormality presented itself to the crew, and the lack of warning signals, has rendered the intentionality of the action indeterminate, and furthermore it was not possible to determine which of the two crew members has actuated the levers.
(3). Deficient Judgement - Indeterminate
The lack of cognizance, on the part of the crew members, for insufficiency of warning signals and information about the abnormality, has been a determinant for them to abandon the normal sequence of procedures, such as retracting the landing gear and actuating the Auto-Pilot, in order to take the initiatives of prioritizing the solution of an unusual situation installed in the cockpit, below safety height and that eventually brought on the loss of control of the aircraft, whereby it has also not been possible to determine which one of them took the initiative. Such facts render such aspect indeterminate.
d. Other Aspects
(1). External Inspection - Contributor
There is no condition of seeing the 'Secondary Lock' open, during the external inspection.
(2). Performing Action Below 400 feet - Contributor
Doctrinally, any action by a crew facing any abnormality in the cockpit environment below 400 feet is NOT RECOMMENDABLE.
The crew tried to manage the 'abnormality' concurrently with the control of the aircraft below 400 feet. Under such risk condition, a power reduction occurred on the other engine, compromising the aircraft's performance. As a consequence, the crew was obligated to prioritize the thrust needs to the detriment of other procedures.
(3). Inadequate Action In Face of an Unpredicted Failure - Contributor.
Based on the data collected on the SSFDR about the FUEL FLOW and EPR parameters, the lever of engine no. 2 was brought to the maximum power position, after the locking of said lever at the IDLE position.
Such locking occurred immediately after the lift-off, when the lever was reduced by itself to the 'IDLE' position, staying locked for about three (3) seconds. However, the system itself released the lever, inducing the copilot to bring it to the full power position, even after having informed the pilot about its locking.
It should be pointed out that the pilot has not requested such action after having been informed about the locking, as well as that the copilot has not asked whether such action should be done or not.
The airplane has not provided means for both pilots to be able to imagine how untimely such attitude would become at that extremely critical moment of the flight. In case the action has not been performed by the copilot, the suspicion falls upon the pilot, induced by the same reasons presented before.
Final Report:

Crash of an Embraer XC-95B Bandeirante in Queluz: 8 killed

Date & Time: Aug 30, 1996 at 0947 LT
Type of aircraft:
Operator:
Registration:
2315
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
São José dos Campos - São José dos Campos
MSN:
110-289
YOM:
1980
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
8
Circumstances:
The twin engine aircraft departed São José dos Campos Airport at 0840LT on a test flight on behalf of the Brazilian Aeronautics Institute of Technology. On board were six passengers and two pilots. About an hour into the flight, the aircraft struck a mountain located near Queluz. The aircraft was destroyed and all eight occupants were killed.

Crash of a Learjet 25C in Ribeirão Preto: 2 killed

Date & Time: Jun 4, 1996 at 1320 LT
Type of aircraft:
Registration:
PT-KBC
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
São Paulo – Uberaba – Ribeirão Preto
MSN:
25-165
YOM:
1974
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3500
Captain / Total hours on type:
250.00
Copilot / Total flying hours:
2000
Copilot / Total hours on type:
420
Circumstances:
The crew departed São Paulo on a training flight to Ribeirão Preto with an intermediate stop in Uberaba. On approach to Ribeirão Preto-Leite Lopes Airport, the instructor decided to reduce power on the left engine to simulate a failure and to complete a touch-and-go manoeuvre. After touchdown, the left engine power lever remained in the idle position so the captain took over control and attempted to take off as he judged it impossible to stop on the remaining runway. The aircraft took off but landed back about 92 metres past the runway end. Out of control, it collided with a truck and a tree and came to rest, bursting into flames. A man in the truck as well as one pilot were killed while three other pilots were injured. The aircraft was destroyed.
Probable cause:
The following findings were reported:
- There are indications of the presence of psychological variables that may have influenced the instructor's decision to perform the touch-and-go manoeuvre.
- There was inadequate supervision, at the technical and operational level, by the aircraft operating company, due to the lack of training, inadequate instruction and absence of flight simulator training.
- There was an error made by the pilots due to the inadequate use of the crew resources in the cockpit intended for the operation of the aircraft, due to an ineffective fulfillment of the tasks assigned to each of the crew and the non-observance of the operational rules.
- Even though the crew was qualified for the type of flight, there was inadequate planning regarding the absence of a takeoff and landing briefing.
- There was an error made by the copilot, when the delay in reducing the power levers, as soon as the locking of the left engine lever was established during the dash on the ground, with an inadequate assessment of the situation in this regard.
- There was the participation of the training process received, due to quantitative and qualitative deficiency, which did not attribute to pilots the full technical conditions to be developed in the activity, regarding the lack of simulator training, lack of a company training program that included CRM and local flights, among others.
- There are indications that the difficulties reported by the pilots in relation to the throttle were caused by the rupture of fibers in the cable that transfers its control to the FCU. This cable slides inside a corrugated cover and can be jammed if any fiber in the cable breaks.
Final Report:

Crash of a Learjet 25D in São Paulo: 9 killed

Date & Time: Mar 2, 1996 at 2316 LT
Type of aircraft:
Registration:
PT-LSD
Survivors:
No
Site:
Schedule:
Brasília – São Paulo
MSN:
25-243
YOM:
1978
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total flying hours:
2500
Captain / Total hours on type:
220.00
Copilot / Total flying hours:
330
Copilot / Total hours on type:
57
Aircraft flight hours:
6123
Circumstances:
The twin engine aircraft was completing a charter flight from Brasília to São Paulo, carrying seven members of the pop music group 'Mamonas Assassinas' and two pilots. On approach in limited visibility due to the night, absence of ground lights and clouds, the crew initiated a go-around as his position was erroneous (too high and the glide and excessive speed). The captain initiated a turn to the left when shortly later, at an altitude of 3,280 feet, the aircraft struck trees and crashed in a dense wooded area located about 11 km from the airport. The aircraft was destroyed by impact forces and all nine occupants were killed.
Probable cause:
The following findings were reported:
- The crew was tired due to a long duty period of 16 hours and 30 minutes without rest time,
- The captain showed excess of self-confidence,
- Physical fatigue worsened the level of situational stress of the crew,
- Lack of crew training programme,
- Poor crew coordination,
- Poor approach and landing planning,
- Lack of visibility, lack of ground lights (environment) and low clouds,
- The crew failed to follow the missed approach procedures,
- The copilot was inexperienced,
- Instead of a right turn to 092° and continue to 6,000 feet, the captain initiated a left turn, causing the aircraft to struck obstacles.
Final Report: