Country
code

Francisco Morazán

Crash of a De Havilland DH.114 Heron 1B in Tegucigalpa: 6 killed

Date & Time: May 26, 1970
Type of aircraft:
Operator:
Registration:
HR-ASN
Survivors:
No
MSN:
14009
YOM:
1953
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
On final approach to Tegucigalpa-Toncontin Airport, the crew lost control of the airplane that crashed in a little valley located 1,5 km short of runway 19 threshold. The aircraft was destroyed and all six occupants were killed.
Probable cause:
Loss of control on final approach at low altitude caused by turbulences.

Crash of a Douglas C-47A-25-DK in Tegucigalpa

Date & Time: Nov 25, 1969
Operator:
Registration:
HR-ANA
Survivors:
Yes
MSN:
13301
YOM:
1944
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
15
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The airplane flew over the runway 01 threshold at a speed of 85 knots when it was caught by a strong gust of wind. It gained height then turn to its right heading to the terminal. To avoid any collision, the pilot-in-command made a turn to the left when the left wingtip struck the ground, causing the aircraft to crash by the runway. All 18 occupants were rescued and the aircraft was damaged beyond repair.

Crash of a Douglas DC-6B in Tegucigalpa: 4 killed

Date & Time: Feb 20, 1967 at 0845 LT
Type of aircraft:
Operator:
Registration:
HR-SAS
Survivors:
Yes
Schedule:
San Pedro Sula – Tegucigalpa – San Salvador – Guatemala City – Mexico City
MSN:
42894/56
YOM:
1947
Flight number:
SH203
Country:
Crew on board:
5
Crew fatalities:
Pax on board:
50
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
13128
Captain / Total hours on type:
682.00
Copilot / Total flying hours:
5799
Copilot / Total hours on type:
206
Aircraft flight hours:
48871
Circumstances:
Flight 203 was a scheduled domestic flight from La Mesa Airport, Cortis Department, to Toncontín, Tegucigalpa, D.C., with three flight crew members, two stewardesses and fifty passengers on board. The gross weight of the aircraft at take-off was 75 023 lbs. After a routine pre-flight check which did not reveal any abnormality, the aircraft took off from La Mesa at 0815 hours. Its estimated flight time was 32 minutes and the en-route altitude was 7 500 ft. After 23 minutes of flight the aircraft contacted Toncontín control tower over "El Rancho" and requested authorization to use frequency 118.1 Mc/s. This was acknowledged by the tower which cleared the aircraft to enter the circuit for a landing on runway 01, the wind being calm. The crew then requested to use runway 19 but the tower refused because there was some traffic on runway 01 and several aircraft were waiting to land on that runway. The landing was initiated, 20° of flaps and the undercarriage were lowered; the pilot reported on base leg and extended the flaps to 300. According to the flight crew the indicated airspeed was 100 kt over the fence located before the threshold of runway 01. The landing was normal and smooth and immediately after the nose-wheel touched down the pilot-in-command called for withdrawal of the safety lock of the propeller reverse system. This was done; however the throttle controls would not shift to the desired position (rearward) to operate the propeller reverse system satisfactorily. Three consecutive attempts were made without success. The pilot evaluated the situation and, since the air- craft had passed the point where a go-around could be attempted, he decided to use the brakes only as they appeared to operate normally at the time. According to some reliable observers (aviation mechanics and tower controllers) one of the aircraft's tires burst approximately halfway down the runway and another tire, possibly on the opposite side, burst 50 m farther down. It was assumed that these tires were the two outermost tires. As the aircraft was nearing the end of the runway, the pilot-in-command became afraid of the pronounced slope ahead and veered to the left to execute a 180° turn (ground loop). The turn was successfully completed; however, due to the aircraft's inertia, the radius of the turn was too wide and the nose-wheel ran into a drainage ditch; the aircraft then skidded, the left undercarriage ran into the same ditch and stayed in it, the nose-wheel broke off, the left wing fuel tanks burst and the propellers of Nos. 1 and 4 engines were damaged. A fire resulting from the intense heat of the brakes and wheels, the spilled fuel and the dry grass immediately broke out and destroyed the aircraft. Four passengers were killed while 51 other occupants were evacuated. The aircraft was destroyed.
Probable cause:
According to the reports of the crew, the probable cause of the accident was the failure of the reverse pitch control mechanism. The Board was not able to confirm or deny this because the fire had obliterated all traces of any possible cause.
Final Report:

Crash of a Douglas DC-6 in Tegucigalpa

Date & Time: Jun 30, 1966
Type of aircraft:
Operator:
Registration:
HR-TNG
Flight Type:
Survivors:
Yes
Schedule:
Miami – Tegucigalpa
MSN:
42887
YOM:
1947
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The approach to Tegucigalpa-Toncontin Airport was completed in strong NNE winds. After touchdown on runway 01, the airplane went out of control, veered off runway, lost its undercarriage and came to rest in flames in a drainage ditch. All three crew members escaped uninjured while the aircraft was destroyed by fire.

Crash of a Curtiss C-46A-55-CK Commando in Tegucigalpa

Date & Time: Jun 7, 1962
Type of aircraft:
Operator:
Registration:
HR-SAL
Flight Type:
Survivors:
Yes
Schedule:
San Pedro Sula – Tegucigalpa
MSN:
248
YOM:
1945
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Upon landing at Tegucigalpa-Toncontin Airport, the left main gear collapsed. The airplane slid for several yards and came to rest, damaged beyond repair. Both pilots were slightly injured.
Probable cause:
Failure of the left main gear on landing.

Crash of a Ford 5 in Tegucigalpa: 16 killed

Date & Time: Nov 29, 1944 at 1500 LT
Type of aircraft:
Operator:
Registration:
XH-TAN
Flight Phase:
Survivors:
No
Schedule:
Tegucigalpa – San Pedro Sula
YOM:
1935
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
14
Pax fatalities:
Other fatalities:
Total fatalities:
16
Circumstances:
Shortly after lift off, while in initial climb, the right wing failed. The aircraft went out of control and crashed in a huge explosion. All 16 occupants were killed.
Probable cause:
It appears the loss of the right wing was caused by a structural failure due to excessive vibrations accumulated during operations on difficult and rough terrain.

Crash of a Ford 4 in Tegucigalpa

Date & Time: Mar 5, 1934
Type of aircraft:
Registration:
NC7120
Flight Phase:
Survivors:
Yes
MSN:
4-AT-034
YOM:
1928
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
10
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
Shortly after takeoff from Tegucigalpa-Toncontin Airport, while in initial climb, the three engine airplane collided with power lines, stalled and crashed in a ravine located about 300 metres past the runway end. An Italian passenger tried to escape and jumped out the cabin but fall in the ravine with his kid in his arms. The father was killed and his kid was injured. All 10 other occupants escaped uninjured and the aircraft was damaged beyond repair. It is believed that the takeoff was initiated with a tailwind component and the left main wheel or the left wing impacted an electric power line during initial climb. Some debris such as an engine (third image) were found 83 years later by a depth of 65 feet.
Crew:
Eugene 'Smokey' Rhoads, pilot,
Mr. Holmberg, mechanic.

Source and photos via Amado Aguiluz Ferrari, Coronel José Alfredo San Martín and Carlos Rosa Mejía.