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Canterbury Regional Council

Crash of a Piper PA-31-350 Navajo Chieftain in Christchurch: 8 killed

Date & Time: Jun 6, 2003 at 1907 LT
Registration:
ZK-NCA
Survivors:
Yes
Schedule:
Palmerston North – Christchurch
MSN:
31-7405203
YOM:
1974
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
8
Captain / Total flying hours:
4325
Captain / Total hours on type:
820.00
Aircraft flight hours:
13175
Circumstances:
The aircraft was on an air transport charter flight from Palmerston North to Christchurch with one pilot and 9 passengers. At 1907 it was on an instrument approach to Christchurch Aerodrome at
night in instrument meteorological conditions when it descended below minimum altitude, in a position where reduced visibility prevented runway or approach lights from being seen, to collide with trees and terrain 1.2 nm short of the runway. The pilot and 7 passengers were killed, and 2 passengers received serious injury. The aircraft was destroyed. The accident probably resulted from the pilot becoming distracted from monitoring his altitude at a critical stage of the approach. The possibility of pilot incapacitation is considered unlikely, but cannot be ruled out.
Probable cause:
Findings:
- The pilot was appropriately licensed and rated for the flight.
- The pilotís previously unknown heart disease probably would not have made him unfit to hold his class 1 medical certificate.
- The pilotís ability to control the aircraft was probably not affected by the onset of any incapacitation associated with his heart condition.
- Although the pilot was experienced on the PA 31 type on VFR operations, his experience of IFR operations was limited.
- The pilot had completed a recent IFR competency assessment, which met regulatory requirements for recent instrument flight time.
- The aircraft had a valid Certificate of Airworthiness, and the scheduled maintenance which had been recorded met its airworthiness requirements.
- The return of the cabin heater to service by the operator, after the maintenance engineer had disabled it pending a required test, was not appropriate but was not a factor in the accident.
- The cabin heater was a practical necessity for IFR operations in winter, and the required test should have been given priority to enable its safe use.
- The 3 unserviceable avionics instruments in the aircraft did not comply with Rule part 135, and indicated a less than optimum status of avionics maintenance. However there was sufficient
serviceable equipment for the IFR flight.
- The use of cellphones and computers permitted by the pilot on the flight had the potential to cause electronic interference to the aircraftís avionics, and was unsafe.
- The pilotís own cellphone was operating during the last 3 minutes of the flight, and could have interfered with his glide slope indication on the ILS approach.
- The aircraftís continued descent below the minimum altitude could not have resulted from electronic interference of any kind.
- The pilotís altimeter was correctly set and displayed correct altitude information throughout the approach.
- There was no aircraft defect to cause its continued descent to the ground.
- The aircraftís descent which began before reaching the glide slope, and continued below the glide slope, resulted either from a faulty glide slope indication or from the pilot flying a localiser approach instead of an ILS approach.
- When the aircraft descended below the minimum altitude for either approach it was too far away for the pilot to be able to see the runway and approach lights ahead in the reduced visibility at the time.
- The pilot allowed the aircraft to continue descending when he should have either commenced a missed approach or stopped the aircraftís descent.
- The pilotís actions or technique in flying a high-speed unstabilised instrument approach; reverting to hand-flying the aircraft at a late stage; not using the autopilot to fly a coupled approach and, if intentional, his cellphone call, would have caused him a high workload and possibly overload and distraction.
- The pilotís failure to stop the descent probably arose from distraction or overload, which led to his not monitoring the altimeter as the aircraft approached minimum altitude.
- The possibility that the pilot suffered some late incapacity which reduced his ability to fly the aircraft is unlikely, but cannot be ruled out.
- If TAWS equipment had been installed in this aircraft, it would have given warning in time for the pilot to avert the collision with terrain.
- While some miscommunication of geographical coordinates caused an erroneous expansion of the search area, the search for the aircraft was probably completed as expeditiously as possible in difficult circumstances.
Final Report:

Crash of a Fletcher FU-24-950 in Fairlie

Date & Time: Aug 30, 1997 at 0730 LT
Type of aircraft:
Registration:
ZK-DIL
Flight Phase:
Survivors:
Yes
MSN:
175
YOM:
1972
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
While turning onto the sowing run, at about 300 feet agl, a significant downdraught was encountered, together with a loss of at least 5 knots airspeed. The pilot responded by pushing the control column aggressively forward and turning towards the lower ground. At the same time, he operated the jettison lever. The rate of dump and the recovery from the downdraught were far less than anticipated, and the pilot found himself about to collide with rocks in a paddock. He pulled hard back, but was unable to avoid hitting the ground with the left wing. The aircraft flipped and slid backwards to a halt. The pilot's instructor was operating a second Fletcher on the same job, saw that there had been a crash, and, after jettisoning his own load, landed nearby and went to the pilot's assistance. Meteorological conditions were favourable for topdressing, but katabatic winds were likely to have been present in the valley, after a clear, cool night. By the time of these flights, a light northwesterly was in place, which could have added to a katabatic flow. There was very light turbulence. Shortly after the accident, light wind gusts were noted; a steady, stronger wind down the valley was established by mid morning. The accident pilot's training had been completed only the day before, and foremost in his mind was the need to avoid a stall. The combination of pushing forward more than necessary, and a turning flight-path, made the jettison ineffective. In the pull-up to avoid hitting the ground the jettison rate increased, but about one third of the load remained aboard after the accident. It was recommended, and accepted, that the pilot receive more dual training on the stall characteristics of the aircraft, with an emphasis on the speed margins available when manoeuvring at low speed. The agricultural operators association was to be asked to remind members of the effect of manoeuvring on jettison characteristics.

Crash of a Fletcher FU24-954 in Rangitata: 1 killed

Date & Time: Dec 28, 1988 at 1005 LT
Type of aircraft:
Registration:
ZK-EMZ
Flight Phase:
Survivors:
No
Schedule:
Rangitata - Rangitata
MSN:
280
YOM:
1981
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The aircraft took off at about 0950 to spray chemicals on a 10-hectare potato crop. The flight was expected to take about 25 minutes. At 1020 when the plane had not returned to the airstrip the loader driver attempted to contact the pilot using a portable VHF transceiver. There was no response. The aircraft was found to have crashed in a level stony paddock. Physical evidence showed that the ground impact had occurred with the plane in a descending left turn and a nose down attitude. The angle of bank was 20 to 30 degrees. The outer panel of the left wing was damaged at the tip and was separated from the airframe, lying about 20 metres away. After this initial impact the plane had cartwheeled, breaking up. There was no fire. This was not a survivable accident.
Probable cause:
There was evidence that the pilot had almost completed his task at this location and was probably making a reversal turn in order to carry out a " cleaning up " run down one of the boundaries when the crash occurred. No evidence of structural or mechanical failure could be found. There was no sign of collision with any obstacle, or of bird strike. The all-up weight and C of G were within the permitted limits. Witnesses agreed that the engine was running normally right up to the the moment of the crash. The sky conditions were partly cloudy with normal horizontal visibility. There had been drizzle earlier in the day but there was no precipitation at the time of the crash. The surface wind was light and variable. The weather was not considered to be a factor. An autopsy showed that the 47-year-old pilot had some slight arterial narrowing but not sufficient to cause sudden incapacitation. Tests for chemical poisoning proved negative. The crash investigator concluded that no probable cause for the accident could be established.

Crash of a Cessna 208 Caravan I off Kaikoura: 2 killed

Date & Time: Nov 27, 1987 at 2355 LT
Type of aircraft:
Registration:
ZK-SFB
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Christchurch - Wellington
MSN:
208-0059
YOM:
1985
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
While cruising by night at an altitude of 11,000 feet on a cargo flight from Christchurch to Wellington, the pilot encountered icing conditions. The airplane went out of control, entered a dive and crashed in the sea off Kaikoura. Both occupants were killed.
Probable cause:
The following findings were reported:
- Icing conditions,
- The aircraft was not equipped with deicing systems,
- The pilot was tired due to a duty period more than 18 hours,
- The pilot loaded and unloaded more than 10 tons of cargo during the day,
- The pilot was soaked by rain while doing so because no foul weather gear was provided,
- The pilot did not have sufficient rest time,
- The pilot did not have a proper brake time and meal,
- The pilot was not properly trained concerning indoctrination course and suffered hypoxia in flight.

Crash of a GAF Nomad N.24A in Lake Tekapo

Date & Time: Jul 20, 1987 at 1900 LT
Type of aircraft:
Operator:
Registration:
ZK-NMD
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Lake Tekapo - Hamilton
MSN:
36
YOM:
1977
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
After takeoff from Lake Tekapo, the aircraft encountered difficulties to gain height the stalled and crashed past the runway end. The pilot, sole on board, was seriously injured.
Probable cause:
It was determined that the stall during initial climb was the consequence of an excessive accumulation of frost on fuselage and wings. The aircraft was not deiced prior to takeoff.

Crash of a Fletcher FU-24A-950 in Orari Gorge: 1 killed

Date & Time: Apr 13, 1987 at 1700 LT
Type of aircraft:
Operator:
Registration:
ZK-DZA
Flight Phase:
Survivors:
No
MSN:
201
YOM:
1974
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
ZK-DZA was engaged in an aerial topdressing operation at Orari Gorge Station, situated about 16 km north-northwest of the small town of Geraldine in Canterbury. The day's work had commenced at 08:12 and by 16:30 100 tonnes of superphosphate fertilizer had been distributed over the farm in about 100 sorties. These operations had been uneventful apart from two instances of the engine stopping while idling on the ground. One of these events occurred at the start up after the lunch break and the other was after the halt taken at about 16:30 to enable the attachment of a Transland spreader unit to the plane. The pilot was unconcerned at these unwanted stoppages as the engine had a tendency to do this in warm ambient temperatures, and he attributed it to " vapour lock ". At about 16:55 the pilot took off again to spread a mixture of 575 kg of selenium pellets and between 100 and 150 kg of superphosphate over a higher area of the farm. The aircraft weight and CG were within the permitted limits. About five minutes later the loader driver heard " a thump " and on looking around sighted the plane on the side of a hill about one kilometer northwest of his location. The driver immediately radioed base to get them to inform the station manager that a crash had occurred. There was one eyewitness to the accident. A farmer working about 4 km away saw the Fletcher flying away from him and dropping a short trail of fertilizer before making " a funny move sideways " and then coming to a stop on the ground. He immediately returned to his house and telephoned Orari Gorge Station to raise the alarm. Station personnel arrived at the crash scene by 4WD vehicle within ten or fifteen minutes. They found the aircraft wrecked and the pilot dead. Fire had not occurred. The crash site was on a steep grassy slope 1,700 feet amsl. The aircraft had contacted the ground in roughly a landing attitude, at high rate of sink, and drifting to the left. It was severely damaged, with the main undercarriage legs separated and the nose leg folded back under the fuselage. The engine was displaced and the spreader torn off. Of the rest of the airframe only the tail section remained intact. Deceleration was rapid.The ground slide covered a distance of sixteen metres. This was not a survivable accident.
Probable cause:
The weather was calm with only high cloud. Examination of the engine revealed no evidence that it may have lost power in flight. An autopsy carried out on the pilot showed that he had received a broken neck and a ruptured heart in the impact. He was suffering from a moderately severe coronary heart disease at the time of death. The crash investigator concluded that this very experienced pilot may have had a heart attack and been seriously incapacitated in flight, prompting him to attempt an immediate emergency landing on the hillside.

Crash of a Fletcher FU24-954 in Waimate: 1 killed

Date & Time: Mar 21, 1984 at 0705 LT
Type of aircraft:
Operator:
Registration:
ZK-EMI
Flight Phase:
Survivors:
Yes
MSN:
260
YOM:
1979
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The single engine airplane departed Waimate Airport, bound to a local farm for a crop spraying mission, carrying one passenger and one pilot. Shortly after takeoff, while climbing to an altitude of about 300-400 feet, the aircraft entered a stratus area when the engine apparently lost power. The aircraft entered a nose-down attitude then crashed in the Waihao River. The passenger was killed and the pilot was seriously injured. The aircraft was totally destroyed.
Probable cause:
The pilot suffered a spatial disorientation while flying in low visibility due to clouds (stratus) after he encountered unknown technical problems with the engine.

Crash of a Cessna 404 Titan off Christchurch: 1 killed

Date & Time: Aug 8, 1977 at 2130 LT
Type of aircraft:
Registration:
ZK-TAS
Flight Type:
Survivors:
No
Schedule:
Wellington - Christchurch
MSN:
404-0067
YOM:
1977
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The pilot, sole on board, was completing a mail flight from Wellington to Christchurch. He departed FL100 and started the descent to Christchurch when he reported technical problems to ATC and later declared an emergency after an engine was shut down. Few seconds later, he lost control of the airplane that entered a spin and crashed into the sea. SAR operations were initiated but no trace of the aircraft nor the pilot was found.
Probable cause:
Due to lack of evidences, the exact cause of the accident could not be determined. However, the following causes have not been ruled out: a loss of control after the pilot suffered a spatial disorientation while trying to deal with an emergency situation in limited visibility (clouds), a loss of control because of airframe ice build-up, a structural failure with a severe fire in the engine bay, an explosion in hazardous cargo, a failure of the flying control system or a possible criminal mischief.

Crash of a De Havilland DHC-2 Beaver in Brothers Range: 2 killed

Date & Time: Mar 1, 1975
Type of aircraft:
Operator:
Registration:
ZK-COV
Flight Phase:
Survivors:
No
MSN:
1602
YOM:
1965
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
Crashed in unknown circumstances in Brothers Range, near Cave. The pilot Arthur Rudge and his son aged eight were killed.

Crash of a Fletcher FU-24 II in Clayton Station: 1 killed

Date & Time: Aug 30, 1972 at 1750 LT
Type of aircraft:
Operator:
Registration:
ZK-CFQ
Flight Phase:
Survivors:
No
MSN:
98
YOM:
1963
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
Late in the afternoon of 30/8/72 two aircraft were conducting an aerial topdressing operation at Clayton Station. One of the pilots observed the other aircraft operating normally. When he looked again moments later he saw smoke and flames on the side of a ridge in the working area. Realizing that there had been an accident he immediately flew back to the airstrip and raised the alarm. ZK-CFQ had struck the ground with its port wingtip while making a 180 degree RH turn within the confines of a valley. Physical evidence showed that the plane was banked at an angle of 68 degrees when the wingtip touched the slope. The aircraft was destroyed by impact forces and fuel from a ruptured tank ignited completing the destruction. Evidence also showed that the engine was producing high power at the moment of impact. The all-up weight and C of G were found to be well within the permitted limits. The other pilot reported seeing an interruption in the flow of fertilizer in the final sowing run, but there was no sign of a blockage in the hopper outlet. The hopper was empty. The weather was perfect for aerial topdressing, CAVU and still air. An autopsy revealed that the 34-year-old pilot had received no fatal injuries in the impact, but there was evidence of coronary occlusion due to arteriosclerosis heart disease. It was concluded that the pilot had died from a heart attack and traumatic hypoxia. It was not clear if the heart attack occurred before or at the time of impact. It would appear however, from the steep angle of bank so close to the ground, that pilot had become incapacitated and had lost control of his aircraft.
Source: ASN
Probable cause:
Loss of control at low height for undetermined reason.