Crash of a Boeing 747-412F in Halifax

Date & Time: Nov 7, 2018 at 0506 LT
Type of aircraft:
Operator:
Registration:
N908AR
Flight Type:
Survivors:
Yes
Schedule:
Chicago – Halifax
MSN:
28026/1105
YOM:
1997
Flight number:
KYE4854
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
21134
Captain / Total hours on type:
166.00
Copilot / Total flying hours:
7404
Copilot / Total hours on type:
1239
Aircraft flight hours:
92471
Aircraft flight cycles:
16948
Circumstances:
The Sky Lease Cargo Boeing 747-412F aircraft (U.S. registration N908AR, serial number 28026) was conducting flight 4854 (KYE4854) from Chicago/O’Hare International Airport, Illinois, U.S., to Halifax/Stanfield International Airport, Nova Scotia, with 3 crew members, 1 passenger, and no cargo on board. The crew conducted the Runway 14 instrument landing system approach. When the aircraft was 1 minute and 21 seconds from the threshold, the crew realized that there was a tailwind; however, they did not recalculate the performance data to confirm that the landing distance available was still acceptable, likely because of the limited amount of time available before landing. The unexpected tailwind resulted in a greater landing distance required, but this distance did not exceed the length of the runway. The aircraft touched down firmly at approximately 0506 Atlantic Standard Time, during the hours of darkness. After the firm touchdown, for undetermined reasons, the engine No. 1 thrust lever was moved forward of the idle position, causing the speed brakes to retract and the autobrake system to disengage, increasing the distance required to bring the aircraft to a stop. In addition, the right crab angle (4.5°) on initial touchdown, combined with the crosswind component and asymmetric reverser selection, caused the aircraft to deviate to the right of the runway centreline. During the landing roll, the pilot monitoring’s attention was focused on the lateral drift and, as a result, the required callouts regarding the position of the deceleration devices were not made. Although manual brake application began 8 seconds after touchdown, maximum braking effort did not occur until 15 seconds later, when the aircraft was 800 feet from the end of the runway. At this position, it was not possible for the aircraft to stop on the runway and, 5 seconds later, the aircraft departed the end of the runway at a speed of 77 knots and came to a stop 270 m (885 feet) past the end. The aircraft struck the approach light stanchions and the localizer antenna array. The No. 2 engine detached from its pylon during the impact sequence and came to rest under the left horizontal stabilizer, causing a fire in the tail section following the impact. The emergency locator transmitter activated. Aircraft rescue and firefighting personnel responded. All 3 crew members received minor injuries and were taken to the hospital. The passenger was not injured. During the overrun, the aircraft crossed a significant drop of 2.8 m (9 feet) approximately 166 m (544 feet) past the end of the runway and was damaged beyond repair.
Probable cause:
Findings as to causes and contributing factors:
These are conditions, acts or safety deficiencies that were found to have caused or contributed to this occurrence.
1. The ineffective presentation style and sequence of the NOTAMs available to the crew and flight dispatch led them to interpret that Runway 23 was not available for landing at Halifax/Stanfield International Airport.
2. The crew was unaware that the aircraft did not meet the pre-departure landing weight requirements using flaps 25 for Runway 14.
3. Due to the timing of the flight during the nighttime circadian trough and because the crew had had insufficient restorative sleep in the previous 24 hours, the crew was experiencing sleep-related fatigue that degraded their performance and cognitive functioning during the approach and landing.
4. Using unfactored (actual) landing distance charts may have given the crew the impression that landing on Runway 14 would have had a considerable runway safety margin, influencing their decision to continue the landing in the presence of a tailwind.
5. When planning the approach, the crew calculated a faster approach speed of reference speed + 10 knots instead of the recommended reference speed + 5 knots, because they misinterpreted that a wind additive was required for the existing conditions.
6. New information regarding a change of active runway was not communicated by air traffic control directly to the crew, although it was contained within the automatic terminal information service broadcast; as a result, the crew continued to believe that the approach and landing to Runway 14 was the only option available.
7. For the approach, the crew selected the typical flap setting of flaps 25 rather than flaps 30, because they believed they had a sufficient safety margin. This setting increased the landing distance required by 494 feet.
8. The crew were operating in a cognitive context of fatigue and biases that encouraged anchoring to and confirming information that aligned with continuing the initial plan, increasing the likelihood that they would continue the approach.
9. The crew recognized the presence of a tailwind on approach 1 minute and 21 seconds from the threshold; likely due to this limited amount of time, the crew did not recalculate the performance data to confirm that the runway safety margin was still acceptable.
10. An elevated level of stress and workload on short final approach likely exacerbated the performance-impairing effects of fatigue to limit the crew’s ability to determine the effect of the tailwind, influencing their decision to continue the approach.
11. The higher aircraft approach speed, the presence of a tailwind component, and the slight deviation above the glideslope increased the landing distance required to a distance greater than the runway length available.
12. After the firm touchdown, for undetermined reasons, the engine No. 1 thrust lever was moved forward of the idle position, causing the speed brakes to retract and the autobrake system to disengage, increasing the distance required to bring the aircraft to a stop.
13. The right crab angle (4.5°) on initial touchdown, combined with the crosswind component and asymmetric reverser selection, caused the aircraft to deviate to the right of the runway centreline.
14. During the landing roll, the pilot monitoring’s attention was focused on the lateral drift and, as a result, the required callouts regarding the position of the deceleration devices were not made.
15. The pilot flying focused on controlling the lateral deviation and, without the benefit of the landing rollout callouts, did not recognize that all of the deceleration devices were not fully deployed and that the autobrake was disengaged.
16. Although manual brake application began 8 seconds after touchdown, maximum braking effort did not occur until 15 seconds later, when the aircraft was 800 feet from the end of the runway. At this position, it was not possible for the aircraft to stop on the runway and, 5 seconds later, the aircraft departed the end of the runway at a speed of 77 knots and came to a stop 270 m (885 feet) past the end of the runway.
17. During the overrun, the aircraft crossed a significant drop of 2.8 m (9 feet) approximately 166 m (544 feet) past the end of the runway and was damaged beyond repair. While this uneven terrain was beyond the 150 m (492 feet) runway end safety area proposed by Transport Canada, it was within the recommended International Civil Aviation Organization runway end safety area of 300 m (984 feet).

Findings as to risk:
These are conditions, unsafe acts or safety deficiencies that were found not to be a factor in this occurrence but could have adverse consequences in future occurrences.
1. If the pilot monitoring does not call out approach conditions or approach speed increases, the pilot flying might not make corrections, increasing the risk of a runway overrun.

Other findings:
These items could enhance safety, resolve an issue of controversy, or provide a data point for future safety studies.
1. The investigation concluded that there was no reverted rubber hydroplaning and almost certainly no dynamic hydroplaning during this occurrence.
2. Although viscous hydroplaning can be expected on all wet runways, the investigation found that when maximum braking effort was applied, the aircraft braking was consistent with the expected braking on Runway 14 under the existing wet runway conditions.
Final Report:

Crash of a Piper PA-46-350P Malibu Mirage in Hurricane

Date & Time: Oct 21, 2018 at 1500 LT
Registration:
N413LL
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Hurricane - Salt Lake City
MSN:
46-36413
YOM:
2007
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7000
Captain / Total hours on type:
1500.00
Aircraft flight hours:
1088
Circumstances:
Shortly after takeoff, the pilot smelled smoke. As he began to turn the airplane back to the airport, the engine lost total power. He conducted a forced landing in a field just short of the airport, during which the airplane struck a metal fence and pipe. All occupants egressed, and the pilot then noticed that a fire had erupted under the airplane's engine cowling. Postaccident examination revealed that the airplane sustained fire damage to the roof and forward end of the baggage compartment along with the engine accessory area between the firewall and aft air baffles. Further examination revealed that one of the engine exhaust crossover pipe assemblies was misaligned at the slip joint. An engine manufacturer service bulletin (SB) called for inspections of the exhaust system slip and flange joints to identify misaligned exhaust components. The last maintenance event occurred about 7 1/2 flight hours before the accident, during which the SB was performed and resulted in the replacement of crossover pipes. The mechanic who had performed the most recent maintenance did not follow the correct procedures for reinstallation of the crossover pipe, and the inspector who reviewed his work did not examine the installation as it progressed but instead inspected the pipes after they were installed and essentially hidden from view by their protective heat shield. As a result of the misaligned engine exhaust crossover pipe, hot exhaust gases escaped into the engine compartment and started a fire, which compromised critical engine fuel and oil lines, and resulted in the loss of engine power.
Probable cause:
The mechanic's failure to properly align the engine exhaust crossover pipe during replacement, and his supervisor's failure to properly inspect the installation, which resulted in an in-flight fire and the loss of engine power.
Final Report:

Crash of a Sukhoi Superjet 100-95B in Yakutsk

Date & Time: Oct 10, 2018 at 0321 LT
Type of aircraft:
Operator:
Registration:
RA-89011
Survivors:
Yes
Schedule:
Ulan-Ude - Yakutsk
MSN:
95019
YOM:
2012
Flight number:
SYL414
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
87
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
13125
Captain / Total hours on type:
1080.00
Copilot / Total flying hours:
3200
Copilot / Total hours on type:
1300
Aircraft flight hours:
8115
Aircraft flight cycles:
3320
Circumstances:
Following an uneventful flight from Ulan-Ude, the crew initiated the approach to Yakutsk-Platon Oyunsky Intl Airport Runway 23L. Due to work in progress, the runway 05R threshold was displaced by 1,150 metres, reducing the landing distance to 2,248 metres for the runway 23L on which the touchdown zone lighting system was unserviceable. On approach, the crew was informed by ATC that the friction coefficient was 0,45. The crew completed the landing on runway 23L with a slight tailwind component of 4 knots and started the braking procedure. Unable to stop within the remaining distance, the aircraft overran, entered the construction area and collided with the junction of a concrete section under reconstruction, causing both main landing gear to collapse (the left main gear was torn off). The aircraft slid for another 250 metres before coming to rest. All 92 occupants evacuated safely and the aircraft was damaged beyond repair.
Probable cause:
The cause of the aviation accident with the RRJ 95B RA-89011 aircraft when landing at night with one deactivated thrust reverser was the transfer to the crew of incorrect information about the value of the friction coefficient, which led to the landing on an icy runway, the average normative friction coefficient which was less than 0.3, which did not allow landing in accordance with current regulations. This led to a significant increase in landing distance, rolling the aircraft out of the runway and collision with the junction of the reconstructed section of the runway with a height of about 0.4 m, which led to the destruction of the main landing gear supports and damage to the engines with fuel leakage without causing a fire.
The contributing factors were the following:
- Absence of a connecting ramp (which was not envisaged by the reconstruction project) between the current and the part of the runway being reconstructed;
- inefficiency of the SMS of Yakutsk Airport JSC in terms of identification and control of risks associated with the possibility of ice formation at the runway, and insufficient control over the implementation of the SMS by aviation authorities;
- erroneous determination of the Xc value at the last measurement;
- inefficiency of ice removal procedure during runway cleaning due to lack of chemical reagents for ice removal and/or thermal machines at the airfield;
- lack of information from the RRJ-95LR-100 RA 89038 aircraft crew about actual rolling out of the runway, which was an aviation incident and was subject to investigation;
- failure by airport and ATC officials to take appropriate action after receiving the RRJ-95LR-100 RA-89038 low friction report from the aircraft crew.
Final Report:

Crash of an Antonov AN-32 in Khartoum

Date & Time: Oct 3, 2018
Type of aircraft:
Operator:
Flight Type:
Survivors:
Yes
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The airplane was engaged in an exercise with a second Sudanese Air Force Antonov AN-32. After touchdown on runway 18, the crew started the braking procedure when the airplane was struck by the AN-32 from behind. After collision, both airplanes went out of control and came to rest on the runway edge. There were no casualties while both aircraft were destroyed. It appears that the AN-32 landed shortly after the AN-26 and was unable to stop in a timely manner.

Crash of an Antonov AN-26 in Khartoum

Date & Time: Oct 3, 2018
Type of aircraft:
Operator:
Registration:
7706
Flight Type:
Survivors:
Yes
MSN:
104 04
YOM:
1980
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The airplane was engaged in an exercise with a second Sudanese Air Force Antonov AN-32. After touchdown on runway 18, the crew started the braking procedure when the airplane was struck by the AN-32 from behind. After collision, both airplanes went out of control and came to rest on the runway edge. There were no casualties while both aircraft were destroyed. It appears that the AN-32 landed shortly after the AN-26 and was unable to stop in a timely manner.

Crash of a Dassault Falcon 50 in Greenville: 2 killed

Date & Time: Sep 27, 2018 at 1346 LT
Type of aircraft:
Registration:
N114TD
Survivors:
Yes
Schedule:
St Petersburg - Greenville
MSN:
17
YOM:
1980
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
11650
Copilot / Total flying hours:
5500
Aircraft flight hours:
14002
Circumstances:
The flight crew was operating the business jet on an on-demand air taxi flight with passengers onboard. During landing at the destination airport, the cockpit voice recorder (CVR) recorded the sound of the airplane touching down followed by the pilot's and copilot's comments that the brakes were not operating. Air traffic controllers reported, and airport surveillance video confirmed, that the airplane touched down "normally" and the airplane's thrust reverser deployed but that the airplane continued down the runway without decelerating before overrunning the runway and impacting terrain. Postaccident examination of the airplane's brake system revealed discrepancies of the antiskid system that included a broken solder joint on the left-side inboard transducer and a reversal of the wiring on the right-side outboard transducer. It is likely that these discrepancies resulted in the normal braking system's failure to function during the landing. Before the accident flight, the airplane had been in long-term storage for several years and was in the process of undergoing maintenance to bring the airplane back to a serviceable condition, which in-part required the completion of several inspections, an overhaul of the landing gear, and the resolution of over 100 other unresolved discrepancies. The accident flight and four previous flights were all made with only a portion of this required maintenance having been completed and properly documented in the airplane's maintenance logs. A pilot, who had flown the airplane on four previous flights along with the accident pilot (who was acting as second-in-command during them), identified during those flights that the airplane's normal braking system was not operating when the airplane was traveling faster than 20 knots. He remedied the situation by configuring the airplane to use the emergency, rather than normal, braking system. That pilot reported this discrepancy to the operator's director of maintenance, and it is likely that maintenance personnel from the company subsequently added an "INOP" placard near the switch on the date of the accident. The label on the placard referenced the antiskid system, and the airplane's flight manual described that with the normal brake (or antiskid) system inoperative, the brake selector switch must be positioned to use the emergency braking system. Following the accident, the switch was found positioned with the normal braking system activated, and it is likely that the accident flight crew attempted to utilize the malfunctioning normal braking system during the landing. Additionally, the flight crew failed to properly recognize the failure and configure the airplane to utilize the emergency braking system, or utilize the parking brake, as described in the airplane's flight manual, in order to stop the airplane within the available runway.
Probable cause:
The operator's decision to allow a flight in an airplane with known, unresolved maintenance discrepancies, and the flight crew's failure to properly configure the airplane in a way that would have allowed the emergency or parking brake systems to stop the airplane during landing.
Final Report:

Crash of a Beechcraft 200 Super King Air in Oscoda: 1 killed

Date & Time: Sep 25, 2018 at 0613 LT
Operator:
Registration:
N241CK
Flight Type:
Survivors:
No
Schedule:
Detroit - Oscoda
MSN:
BB-272
YOM:
1977
Flight number:
K985
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3806
Captain / Total hours on type:
201.00
Aircraft flight hours:
13933
Circumstances:
The airline transport pilot of the multiengine airplane was cleared for the VOR approach. The weather at the airport was reported as 400 ft overcast with 4 miles visibility in drizzle. When the airplane failed to arrive at the airport as scheduled, a search was initiated, and the wreckage was located soon thereafter. Radar data indicated that the pilot was provided vectors to intercept the final approach course. The last radar return indicated that the airplane was at 2,200 ft and 8.1 miles from the runway threshold. It impacted terrain 3.5 miles from the runway threshold and left of the final approach course. According to the published approach procedure, the minimum descent altitude was 1,100 feet, which was 466 ft above airport elevation. Examination of the wreckage revealed that the airplane had impacted the tops of trees and descended at a 45° angle to ground contact; the airplane was destroyed by a postcrash fire, thus limiting the examination; however, no anomalies were observed that would have precluded normal operation. The landing gear was extended, and approach flaps had been set. Impact and fire damage precluded an examination of the flight and navigation instruments. Autopsy and toxicology of the pilot were not performed; therefore, whether a physiological issue may have contributed to the accident could not be determined. The location of the wreckage indicates that the pilot descended below the minimum descent altitude (MDA) for the approach; however, the reason for the pilot's descent below MDA could not be determined based on the available information.
Probable cause:
The pilot's descent below minimum descent altitude during the non precision instrument approach for reasons that could not be determined based on the available information.
Final Report:

Crash of a Honda HA-420 HondaJet in Foz do Iguaçu

Date & Time: Sep 24, 2018 at 1342 LT
Type of aircraft:
Operator:
Registration:
PR-TLZ
Survivors:
Yes
Schedule:
Curitiba – Foz do Iguaçu
MSN:
420-00068
YOM:
2017
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5600
Captain / Total hours on type:
77.00
Copilot / Total flying hours:
660
Copilot / Total hours on type:
14
Circumstances:
The airplane departed Curitiba-Afonso Pena Airport at 1240LT on an executive flight to Foz do Iguaçu, carrying one passenger and two pilots. Following an uneventful flight, the crew started the descent to Foz do Iguaçu-Cataratas Airport. The aircraft was stabilized and landed on wet runway 32. After touchdown, the crew encountered difficulties to stop the aircraft that overran and came to rest into a ravine. All three occupants evacued safely and the aircraft was damaged beyond repair.
Probable cause:
The following findings were identified:
- The approach was considered stabilized;
- The required landing distance of 6,431t (1,960m) was compatible for the operation, since the LDA of runway 32 at SBFI was 7,201ft (2,195m);
- There was no evidence of malfunction of the aircraft brake system that could have caused the runway excursion;
- At the time of landing, the runway was wet with a significant amount of water on the pavement;
- The estimated deceleration corresponded to what would be expected on a very wet runway (> 3mm of water) with hydroplaning of the tires at higher speeds;
- The friction and macrotexture measurements had normal parameters and did not contribute to the aircraft's poor deceleration;
- The characteristics of the precipitation over threshold 14 associated with the large variations in wind direction and intensity were consistent with the windshear phenomenon, resulting from a microburst;
- The PR-TLZ sensors did not detect the occurrence of windshear during the landing approach;
- A sudden increase in the calibrated speed that peaked at 32kt altered the aircraft's lift and, consequently, reduced the tires' grip on the ground, resulting in poor braking in the parts where the ground speed was lower;
- The speedbrakes were not extended during the run after landing, contrary to what was prevised in the AFM;
- The aircraft ran the full length of the runway, overpassed its limits and crashed into a ravine;
- There was a windshear alert issued about 30 seconds after the landing of the PRTLZ by an aircraft that was at the threshold 32;
- The aircraft had substantial damage; and
- The crewmembers and the passenger left unharmed.
Contributing factors:
- Control skills – undetermined
Despite the low contribution of the speedbrakes to the reduction of the landing distance, this device represents a deceleration resource through aerodynamic drag that should not be neglected, especially during landing on wet runways, and could have contributed to avoiding runway excursion.
- Adverse meteorological conditions – a contributor
The large variation in wind intensity peaked at 32 kt. This variation lasted 13 seconds and raised the indicated speed from 76 kt to 108 kt. Considering that the speed of 108 kt was very close to the VREF (111 KCAS), it can be stated that this phenomenon altered the aircraft's lift and, consequently, reduced the tires' grip on the ground, leading to poor braking.
Final Report:

Crash of a De Havilland DHC-2 Beaver in Igiugig

Date & Time: Sep 20, 2018 at 1530 LT
Type of aircraft:
Operator:
Registration:
N121AK
Flight Phase:
Survivors:
Yes
MSN:
121
YOM:
1951
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
12496
Captain / Total hours on type:
5000.00
Circumstances:
The pilot of the float-equipped airplane reported that, during the initial climb after a water takeoff, about 200 feet, he turned right, and the engine lost power. He immediately switched fuel tanks and attempted to restart the engine to no avail. The airplane descended and struck trees, and the right wing impacted terrain. The airplane sustained substantial damage to the right wing. The pilot reported that there were no preaccident mechanical failures or malfunctions with the airplane that would have precluded normal operation. The pilot reported to the Federal Aviation Administration inspector that, during the initial climb and after the engine lost power, he noticed that the center tank, which was selected for takeoff, was empty. He added that passengers stated that the engine did regain power after switching tanks, but the airplane had already struck trees. The pilot reported as a recommendation to more closely follow checklists.
Probable cause:
The pilot's selection of an empty fuel tank for takeoff, which resulted in fuel starvation and the subsequent total loss of engine power.
Final Report:

Crash of a Cessna 340A in Saint Clair County: 1 killed

Date & Time: Sep 6, 2018 at 2347 LT
Type of aircraft:
Operator:
Registration:
C-GLKX
Flight Type:
Survivors:
No
Schedule:
Saint Thomas - Saint Clair County
MSN:
340A-1221
YOM:
1981
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
690
Captain / Total hours on type:
51.00
Aircraft flight hours:
4038
Circumstances:
The private pilot of the multi-engine airplane was conducting an instrument approach during night visual meteorological conditions. About 1.3 nautical miles (nm) from the final approach fix, the right engine lost total power. The pilot continued the approach and notified air traffic control of the loss of power about 1 minute and 13 seconds later. Subsequently, the pilot contacted the controller again and reported that he was unable to activate the airport's pilot-controlled runway lighting. In the pilot's last radio transmission, he indicated that he was over the airport and was going to "reshoot that approach." The last radar return indicated that the airplane was about 450 ft above ground level at 72 kts groundspeed. The airplane impacted the ground in a steep, vertical nose-down attitude about 1/2 nm from the departure end of the runway. Examination of the wreckage revealed that the landing gear and the flaps were extended and that the right propeller was not feathered. Data from onboard the airplane also indicated that the pilot did not secure the right engine following the loss of power; the left engine continued to produce power until impact. The airplane's fuel system held a total of 203 gallons. Fuel consumption calculations estimated that there should have been about 100 gallons remaining at the time of the accident. The right-wing locker fuel tank remained intact and contained about 14 gallons of fuel. Fuel blight in the grass was observed at the accident site and the blight associated with the right wing likely emanated from the right-wing tip tank. The elevator trim tab was found in the full nose-up position but was most likely pulled into this position when the empennage separated from the aft pressure bulkhead during impact. Examination of the airframe and engine revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation. Although there was adequate fuel on board the airplane, the pilot may have inadvertently moved the right fuel selector to the OFF position or an intermediate position in preparation for landing instead of selecting the right wing fuel tank, or possibly ran the right auxiliary fuel tank dry, which resulted in fuel starvation to the right engine and a total loss of power. The airplane manufacturer's Pilot Operating Handbook (POH) stated that the 20-gallon right- and left-wing locker fuel tanks should be used after 90 minutes of flight. However, 14 gallons of fuel were found in the right-wing locker fuel tank which indicated that the pilot did not adhere to the POH procedures for fuel management. The fuel in the auxiliary fuel tank should be used when the main fuel tank was less than 180 pounds (30 gallons) per tank. As a result of not using all the fuel in the wing locker fuel tanks, the pilot possibly ran the right auxiliary fuel tank empty and was not able to successfully restart the right engine after he repositioned the fuel selector back to the right main fuel tank. Postaccident testing of the airport's pilot-controlled lighting system revealed no anomalies. The airport's published approach procedure listed the airport's common traffic advisory frequency, which activated the pilot-controlled lighting. It is possible that the pilot did not see this note or inadvertently selected an incorrect frequency, which resulted in his inability to activate the runway lighting system. In addition, the published instrument approach procedure for the approach that the pilot was conducting indicated that the runway was not authorized for night landings. It is possible that the pilot did not see this note since he gave no indication that he was going to circle to land on an authorized runway. Given that the airplane's landing gear and flaps were extended, it is likely that the pilot intended to land but elected to go-around when he was unable to activate the runway lights and see the runway environment. However, the pilot failed to reconfigure the airplane for climb by retracting the landing gear and flaps. The pilot had previously failed to secure the inoperative right engine following the loss of power, even though these procedures were designated in the airplane's operating handbook as "immediate action" items that should be committed to memory. It is likely that the airplane was unable to climb in this configuration, and during the attempted go-around, the pilot exceeded the airplane's critical angle of attack, which resulted in an aerodynamic stall. Additionally, the pilot had the option to climb to altitude using singleengine procedures and fly to a tower-controlled airport that did not have any landing restrictions, but instead, he decided to attempt a go-around and land at his destination airport.
Probable cause:
The pilot's improper fuel management, which resulted in a total loss of right engine power due to fuel starvation; the pilot's inadequate flight planning; the pilot's failure to secure the right engine following the loss of power; and his failure to properly configure the airplane for the go-around, which resulted in the airplane's failure to climb, an exceedance of the critical angle of attack, and an aerodynamic stall.
Final Report: