Crash of a Cessna S550 Citation II in Indianapolis: 2 killed

Date & Time: May 22, 2019 at 1243 LT
Type of aircraft:
Operator:
Registration:
N311G
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Indianapolis - Minden
MSN:
550-0041
YOM:
1985
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3530
Circumstances:
The pilot was conducting a personal cross-country flight in a turbofan-powered airplane. Shortly after departure, the airplane entered a witness-estimated 90° left bank with the nose parallel to the horizon; as the airplane began to roll out of the turn, the nose remained at or below the horizon before it dropped and the airplane impacted the ground. Flight track data revealed that, shortly after departure, the airplane's ground speed immediately began decreasing from its maximum of 141 knots during takeoff and continued decreasing until the last recorded data point, which showed that the airplane had a ground speed of 100 knots. The surface wind reported about 10 minutes before the accident was from 170° at 9 knots, gusting to 14 knots, which resulted in a 1- to 2-knot tailwind component. Given this information and the airplane's configuration at the time of the accident, the airplane's indicated airspeed (IAS) would have been between about 86 and 93 knots. The airplane's stall speed was calculated to be 100 knots IAS (KIAS) with a bank angle of 45° and 118 KIAS with a bank angle of 60°. Thus, the pilot failed to maintain airspeed or accelerate after departure, which resulted in an aerodynamic stall A pilot who had flown with the accident pilot twice before the accident reported that, during these flights, the pilot had flown at reduced power settings and slower-than-normal airspeeds. During the flight 1 year before the accident, he reached over and pushed the power levers forward himself. He also stated that every time he had flown with the pilot, he was "very behind the airplane." Postaccident examination of the engines revealed no signs of preimpact mechanical failures or malfunctions that would have precluded normal operation, and both engines exhibited circumferential rub marks on all rotating stages, blade tip bending opposite the direction of rotation, and debris ingestion through the gas path, indicating that the engine had power at impact. Further, the right engine full authority digital electronic control (FADEC) nonvolatile memory recorded no faults. (The left engine FADEC could not be downloaded due to damage.) The Airplane Flight Manual stated that the pilot must, in part, advance the throttle lever to the maximum takeoff detent for the FADEC's nonvolatile memory to record a logic trend snapshot 2 seconds after takeoff. The lack of a FADEC logic trend snapshot is consistent with the pilot not fully advancing the throttles during the takeoff and initial climb and is likely why he did not attain or maintain sufficient airspeed. The flight track data, pilot witness account, and airplane damage are consistent with the pilot failing to fully advance the power levers while maneuvering shortly after takeoff, which led to his failure to maintain sufficient airspeed and resulted in the exceedance of the airplane's critical angle of attack and a subsequent aerodynamic stall.
Probable cause:
The pilot's failure to fully advance the power levers during the takeoff and initial climb, which led to his failure to maintain sufficient airspeed and resulted in the exceedance of the airplane's critical angle of attack and a subsequent aerodynamic stall.
Final Report:

Crash of a Beechcraft 60 Duke in Loveland: 1 killed

Date & Time: May 15, 2019 at 1248 LT
Type of aircraft:
Operator:
Registration:
N60RK
Flight Type:
Survivors:
No
Schedule:
Broomfield – Loveland
MSN:
P-79
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
7000
Captain / Total hours on type:
100.00
Aircraft flight hours:
3119
Circumstances:
The commercial pilot was relocating the multiengine airplane following the completion of an extensive avionics upgrade, which also included the installation of new fuel flow transducers. As the pilot neared the destination airport, he reported over the common traffic advisory frequency that he had "an engine out [and] smoke in the cockpit." Witnesses observed and airport surveillance video showed fire emanating from the airplane's right wing. As the airplane turned towards the runway, it entered a rightrolling descent and impacted the ground near the airport's perimeter fence. The right propeller was found feathered. Examination of the right engine revealed evidence of a fire aft of the engine-driven fuel pump. The fuel pump was discolored by the fire. The fire sleeves on both the fuel pump inlet and outlet hoses were burned away. The fuel outlet hose from the fuel pump to the flow transducer was found loose. The reason the hose was loose was not determined. It is likely that pressurized fuel sprayed from the fuel pump outlet hose and was ignited by the hot turbocharger, which resulted in the inflight fire.
Probable cause:
A loss of control due to an inflight right engine fire due to the loose fuel hose between the engine-driven fuel pump and the flow transducer.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in Sayaxché: 2 killed

Date & Time: Apr 13, 2019
Operator:
Registration:
N2613
Flight Phase:
Flight Type:
Survivors:
No
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
In the morning, the Guatemala Army Forces were informed by ATC that a PA-31 entered the Guatemala Airspace without prior permission. The twin engine airplane crashed in a wooded area located near the farm of Sepens located in the region of Sayaxché, Petén. The aircraft was partially destroyed by impact forces and both occupants were killed. A sticker was set on the fuselage with the registration N2613 which is wrong.

Crash of a Rockwell Sabreliner 60 near Bajamar

Date & Time: Mar 22, 2019
Type of aircraft:
Operator:
Registration:
N990PA
Flight Type:
Survivors:
Yes
MSN:
306-114
YOM:
1976
Location:
Country:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft crashed in unknown circumstances in an isolated and uninhabited area located about 14 km east of Bajamar, Honduras. The airplane was engaged in an illegal mission (drug smuggling flight) as a pack of cocaine and a gun were found in the wreckage. The crew disappeared and was not recovered.

Crash of a BAe 125-600A in San Pedro de Peralta: 1 killed

Date & Time: Mar 10, 2019
Type of aircraft:
Operator:
Registration:
N18BA
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
256046
YOM:
1974
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The aircraft was engaged in an illegal flight, carrying two pilots and a load of 200 kg of cocaine. En route, the crew apparently encountered an unexpected situation and was forced to attempt an emergency landing when the airplane crashed in a wooded area located near San Pedro de Peralta. A pilot was killed while the second was seriously injured. Originally registered N299GS, the aircraft was cancelled from the US registered on 15 February 2018 and exported to Mexico. The registration N18BA is false.