Crash of a Cessna 208B Grand Caravan in Clonbullogue: 2 killed

Date & Time: May 13, 2018 at 1438 LT
Type of aircraft:
Operator:
Registration:
G-KNYS
Survivors:
No
Schedule:
Clonbullogue - Clonbullogue
MSN:
208B-1146
YOM:
2005
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
2157
Aircraft flight hours:
4670
Aircraft flight cycles:
6379
Circumstances:
The Cessna 208B aircraft took off from Runway 27 at Clonbullogue Airfield (EICL), Co. Offaly at approximately 13.14 hrs. On board were the Pilot and a Passenger (a child), who were seated in the cockpit, and 16 skydivers, who occupied the main cabin. The skydivers jumped from the aircraft, as planned, when the aircraft was overhead EICL at an altitude of approximately 13,000 feet. When the aircraft was returning to the airfield, the Pilot advised by radio that he was on ‘left base’ (the flight leg which precedes the approach leg and which is normally approximately perpendicular to the extended centreline of the runway). No further radio transmissions were received. A short while later, it was established that the aircraft had impacted nose-down into a forested peat bog at Ballaghassan, Co. Offaly, approximately 2.5 nautical miles (4.6 kilometres) to the north-west of EICL. The aircraft was destroyed. There was no fire. The Pilot and Passenger were fatally injured.
Probable cause:
Impact with terrain following a loss of control in a steeply banked left-hand turn. The following contributing factors were reported:
- The steeply banked nature of the turn being performed,
- Propeller torque reaction following a rapid and large increase in engine torque,
- The aircraft’s speed while manoeuvring during the steeply banked turn,
- Insufficient height above ground to effect a successful recovery.
Final Report:

Crash of a De Havilland DHC-6 Twin Otter 300 at Perris Valley

Date & Time: May 24, 2017 at 1515 LT
Operator:
Registration:
N708PV
Survivors:
Yes
Schedule:
Perris Valley - Perris Valley
MSN:
489
YOM:
1976
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3358
Captain / Total hours on type:
2131.00
Copilot / Total flying hours:
1893
Copilot / Total hours on type:
12
Aircraft flight hours:
37885
Circumstances:
The pilot of the twin-engine, turbine-powered airplane reported that, while providing flights for skydivers throughout the day, he had a potential new hire pilot flying with him in the right seat. He added that, on the eighth flight of the day, the new pilot was flying during the approach and "approximately 200 feet south from the threshold of [runway] 15 at approximately 15 feet AGL [above ground level] the bottom violently and unexpectedly dropped out. [He] believe[d] some kind of wind shear caused the aircraft [to] slam onto [the] runway and bounce into the air at a 45 to 60-degree bank angle to the right." The prospective pilot then said, "you got it." The pilot took control of the airplane and initiated a go-around by increasing power, which aggravated the "off runway heading." The right wing contacted the ground, the airplane exited the runway to the right and impacted a fuel truck, and the right wing separated from the airplane. The impact caused the pilot to unintentionally add max power, and the airplane, with only the left engine functioning, ground looped to the right, coming to rest nose down.
Probable cause:
The prospective pilot's improper landing flare and the pilot's delayed remedial action to initiate a go-around, which resulted in a runway excursion.
Final Report:

Crash of a Pilatus PC-6/B2-H4 Turbo Porter in Cecina

Date & Time: May 20, 2017 at 1200 LT
Operator:
Registration:
S5-CEI
Survivors:
Yes
Schedule:
Cecina - Cecina
MSN:
778
YOM:
1977
Location:
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The pilot, sole on board, was returning to Cecina Airfield following a skydiving flight in the area. After touchdown on a grassy area, the single engine aircraft veered to the left, impacted a drainage ditch and came to rest. The pilot escaped uninjured and the aircraft was damaged beyond repair.

Crash of a Pilatus PC-6/B2-H4 Turbo Porter in Ferreira do Alentejo: 1 killed

Date & Time: Jun 19, 2016 at 1750 LT
Operator:
Registration:
D-FSCB
Flight Phase:
Survivors:
Yes
Schedule:
Figueira dos Cavaleiros - Figueira dos Cavaleiros
MSN:
634
YOM:
1967
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1400
Captain / Total hours on type:
900.00
Aircraft flight hours:
6556
Circumstances:
On the afternoon of the 19th of June 2016 a Pilatus PC-6 aircraft, German registration DFSCB, took off from the airfield of Figueira dos Cavaleiros (LPFC) for its 17th launch of skydivers that day. On this flight there were 8 persons on board: 1 pilot, 5 skydivers and 2 passengers that were jumping in tandem with two of the skydivers. The meteorology featured a day with clear sky, the wind blew from 040° with 10 kt and the air temperature was around 32° C. The Pilatus took off for a local skydiving training flight and started a climb to an altitude of 14.500 ft. During the initial climb at a rate of 1.000 feet per minute, when crossing 7.000 feet above mean sea level, according to some of the skydivers in the group, a sound similar to the cracking/ripping of a metal structure was heard, and simultaneously the aircraft pitched up to a high nose-up attitude while yawing to the right, causing a severe flight instability. Suddenly, the entire rear fuselage structure disintegrated. According to the reports, some occupants were pushed against the structure of the aircraft before they were thrown outside. During the following seconds the skydivers who did not suffer serious injuries, managed to jump out of the plane and triggered their parachutes. Two of them were seriously injured before leaving the aircraft, their emergency parachutes being automatically deployed by the barometric opening mechanism. As a result, the disintegration of the remaining aircraft parts continued until the impact with the ground. Fragments of the aircraft parts were found over a length of approximately 1.500 meters and a width of about 500 meters and were widely dispersed, with an alignment with the direction of flight from west to east. The pilot was thrown out of the remains of the cockpit and hit the ground at about 400 meters from the impact site of the cabin. He did not trigger his parachute and it was not, nor is it a procedure to be equipped with an emergency parachute with an automatic barometric opening mechanism.
Probable cause:
The investigation considers that, after the fracture of the HT-trim attachment accessory, the horizontal stabilizer was loose, uncontrolled and vibrated, causing the fracture of the left side of the horizontal stabilizer.
Contributing factors:
- Failure on the inspection method by part 145 organization to the critical parts identified on SB 53-001 R1.
- The weakness of regulator (ANAC) oversight to the aircraft operator.
Final Report:

Crash of a Pilatus PC-6/B2-H4 Turbo Porter in Cecina: 2 killed

Date & Time: Jun 11, 2016 at 1230 LT
Operator:
Registration:
S5-CMB
Flight Phase:
Survivors:
Yes
Schedule:
Cecina - Cecina
MSN:
932
YOM:
2000
Location:
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
670
Copilot / Total flying hours:
3300
Copilot / Total hours on type:
1700
Aircraft flight hours:
6705
Circumstances:
The aircraft, operated by Skydive Kalifornia (aka Skydive Toscana) was involved in a local skydiving flight from Cecina Airfield. When the aircraft reached the assigned altitude, six of the seven skydivers bailed out. When the seventh skydiver elected to jump, his auxiliary parachute accidentally opened while the skydiver was still in the cabin. He was sucked outside and collided with the right horizontal stabilizer that later detached. The aircraft entered an uncontrolled descent and crashed in a field. The aircraft was destroyed by impact forces and both pilots were killed. There was no fire. All seven skydivers were uninjured.
Probable cause:
The cause of the accident is attributable to the detachment of the horizontal stabilizer following the impact with a skydiver dragged by his auxiliary parachute that accidentally opened while he was still inside the aircraft. This detachment led to the loss of governability of the aircraft.
The following factors contributed to the incident:
- The conformation of the throwing material, with closing flap of the safety flap covering the pin, which, tending to come out of its seat, did not guarantee adequate protection of the locking pin from accidental interference.
- The conformation of the structure of the right front seat, which interferes with the closing system of the auxiliary parachute bag, which determined the opening.
- The non-optimal disposition of the skydivers and the DL on board the aircraft (first skydiver to go out not immediately to the door and DL with his back addressed to the skydiver student).
Final Report:

Crash of a Cessna 208B Grand Caravan in Lodi

Date & Time: May 12, 2016 at 1413 LT
Type of aircraft:
Registration:
N1114A
Flight Phase:
Survivors:
Yes
Schedule:
Lodi - Lodi
MSN:
208B-0309
YOM:
1992
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
17
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7050
Captain / Total hours on type:
253.00
Aircraft flight hours:
12848
Circumstances:
The commercial pilot reported that, after takeoff on the local skydiving flight, the engine experienced a total loss of power. He initiated a turn toward the airport, but realized the airplane would not reach the runway and chose to perform a forced landing to an open field. During the landing roll, the airplane exited the field, crossed a road, impacted a truck, and continued into a vineyard, where it nosed over. Postaccident examination of the engine revealed that the fuel pressure line that connects the fuel control unit to the airframe fuel pressure transducer was fractured below the fuel control unit fitting's swaged seat. In addition, a supporting clamp for the fuel pressure fuel line was fractured and separated. The operator reported that the fractured fuel line had been replaced the night before the accident and had accumulated about 4 hours of operational time. The previously-installed line had also fractured. Metallurgical examination of the two fractured fuel lines revealed that both fuel lines fractured due to reverse bending fatigue through the tube wall where a ferrule was brazed to the outside of the tube. There were no apparent anomalies or defects at the crack initiation sites. Examination of the supporting clamp determined that it fractured due to unidirectional bending fatigue where one of the clamp's tabs met the clamp loop, with the crack initiating along the inward-facing side of the clamp. The orientation of the reverse bending fatigue cracks and the spacing of the fatigue striations on the tube fracture surfaces were consistent with high-cycle bending fatigue due to a vibration of the tube. The cushioned support clamp is designed to prevent such vibrations from occurring. However, if the clamp tab is fractured, it cannot properly clamp the tube and will be unable to prevent the vibration. The presence of the fractured clamp combined with the fact that the two pressure tubes failed in similar modes in short succession indicated that the clamp most likely failed first, resulting in the subsequent failure of the tubes. Since the clamp was likely fractured when the first fractured fuel pressure line was replaced, the clamp was either not inspected or inadequately inspected at the time of the maintenance.
Probable cause:
A total loss of engine power due to a fatigue fracture of the fuel pressure line that connected the fuel control unit and the fuel flow transducer due to vibration as the result of a fatigue fracture of an associated support clamp. Contributing to the accident was the mechanic's inadequate inspection of the fuel line support clamp during the previous replacement of the fuel line.
Final Report:

Crash of a De Havilland DHC-6 Twin Otter 100 in Fentress

Date & Time: Apr 9, 2016 at 1700 LT
Operator:
Registration:
N122PM
Survivors:
Yes
Schedule:
Fentress - Fentress
MSN:
15
YOM:
1966
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6000
Captain / Total hours on type:
1000.00
Aircraft flight hours:
53624
Circumstances:
The pilot reported that he was landing in gusty crosswind conditions following a parachute jump flight, and that the gusty conditions had persisted for the previous 10 skydiving flights that day. The pilot further reported that during the landing roll, when the nose wheel touched down, the airplane became "unstable" and veered to the left. He reported that he applied right rudder and added power to abort the landing, but the airplane departed the runway to the left and the left wing impacted a tree. The airplane spun 180 degrees to the left and came to rest after the impact with the tree. The left wing was substantially damaged. The pilot did not report any mechanical malfunctions or failures with the airplane that would have precluded normal operation.
Probable cause:
The pilot's failure to maintain directional control during the aborted landing in gusty crosswind conditions, which resulted in a runway excursion and a collision with a tree.
Final Report:

Crash of an IAI Arava 201 near Fátima: 22 killed

Date & Time: Mar 15, 2016 at 1430 LT
Type of aircraft:
Operator:
Registration:
E-206
Flight Phase:
Survivors:
No
Schedule:
Shell - Shell
MSN:
090
YOM:
1992
Location:
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
19
Pax fatalities:
Other fatalities:
Total fatalities:
22
Circumstances:
The twin engine airplane departed Shell Airport at 1251LT for a local training exercice with a crew of three and 19 paratroopers on board. About an hour into the flight, the crew informed ground he was returning to his base due to the deterioration of the weather conditions. Shortly later, the aircraft entered an uncontrolled descent and crashed in a wooded area. All 22 occupants were killed. Up to date, this is the worst accident involving an IAI Arava 201.

Crash of a De Havilland DHC-6 Twin Otter 200 in Dubai

Date & Time: Oct 2, 2015
Operator:
Registration:
DU-SD4
Survivors:
Yes
Schedule:
Dubai - Dubai
MSN:
132
YOM:
1968
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Following an uneventful skydiving mission over the Dubai Drop Zone, the pilot was returning to his base. Upon landing on runway 06, the twin engine aircraft went out of control, veered off runway to the left, struck an embankment and came to rest with the right wing torn off. The pilot was uninjured and the aircraft was damaged beyond repair.

Crash of a Technoavia SMG-92 Turbo Finist in Casale Monferrato

Date & Time: Aug 29, 2015 at 1430 LT
Operator:
Registration:
HA-YDJ
Flight Phase:
Survivors:
Yes
Schedule:
Casale Monferrato - Casale Monferrato
MSN:
02-001
YOM:
1993
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
10
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
600
Captain / Total hours on type:
35.00
Aircraft flight hours:
800
Circumstances:
The single engine aircraft departed Casale Monferrato-Francesco Cappa Airfield on a local skydiving mission, the 13th sortie of the day, carrying seven skydivers, three tourists and one pilot). Shortly after rotation from a grassy runway, the pilot encountered engine problems. The aircraft continued in a flat attitude, collided with a hedge and few trees before coming to rest in a wooded area located 300 metres past the runway end. All 11 occupants were injured, some of them seriously. The aircraft was damaged beyond repair.
Probable cause:
The accident is the consequence of an engine failure caused by the loss of connection in the power module between the quill shaft and the PT shaft.
The following contributing factors were identified:
- A control system of the aircraft as part of 'aircraft operator CAMO not sufficiently thorough,
- The inaccurate, non-timely and incorrect reporting by the user of the aircraft of critical parameters for monitoring engine life,
- A national regulation, in force at the time of the accident, relating to the flight activity for launching paratroopers, which did not provide, in fact, adequate surveillance technique by the aeronautical authority on the aircraft used in this activity,
- The absence of adequate retention and safety devices for paratroopers on board the aircraft.
Final Report: