Crash of a Fairchild C-119G Flying Boxcar in Castle Crags State Park: 3 killed

Date & Time: Sep 16, 1987 at 1730 LT
Operator:
Registration:
N48076
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Montague - Redding
MSN:
11005
YOM:
1952
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
The Fairchild C-119G airtanker had been dispatched to a fire about six miles west of Castle Crags State Park, California at 17:05 and departed the Siskiyou County Airport, CA (SIY) shortly thereafter. N48076, another airtanker of the same kind, a leadplane, and an air attack arrived at the fire at the same time. Two more airtankers followed shortly thereafter. The leadplane identified the target, the approach and departure routes, indicated the target was at an elevation of 4,500 feet, that the ridge on final approach was to be crossed at 6,600 feet, advised there was no wind, there was good visibility, and that there was no turbulence except a "1.5g bump" going across the head of the fire. The leadplane directed one of the C-119 airtankers to drop first. That airtanker aborted their first run because of excess speed. On the second pass, it crossed the ridge at a different point, permitting a somewhat longer final approach. That drop was a successful one. The run was made through a saddle then down a creek to the fire some two miles down stream with a planned exit down stream into a larger canyon. The leadplane then directed the mishap C-119G airtanker to drop next. The mishap airtanker used the same approach as the first airtanker. The mishap airtanker reached the uphill side of the fire when the crew reported trouble maintaining proper speed and dropped their retardant on the fire. At about the time the pilot dropped the retardant, a structural failure occurred and the right wing separated from the airframe along with the tip of the left wing and the tail booms. The fuselage with both engines and most of the left wing attached encountered terrain impact and burned as a unit.
Source: https://www.fs.usda.gov/managing-land/fire
Probable cause:
In-flight loss of control following the structural failure of the right wing.

Crash of a Piper PA-61 Aerostar (Ted Smith 601P) in Corona

Date & Time: Sep 14, 1987 at 1130 LT
Registration:
N902RG
Flight Phase:
Survivors:
Yes
Schedule:
Corona – Carlsbad
MSN:
61-0666-7963311
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4634
Captain / Total hours on type:
120.00
Aircraft flight hours:
1295
Circumstances:
The airplane was refueled before it departed on the accident flight; the pilot did not supervise the fueling. Shortly after takeoff, the pilot advised the Ontario departure controller that both engines were experiencing a power loss and that he suspected jet fuel contamination. The airplane collided with a berm during the ensuing forced landing. The investigation revealed that the FBO fueled the airplane with 131.3 gallons of Jet A fuel. Investigators did not locate any witnesses who saw the pilot preflight the airplane. The pilot sustained severe head injuries and could not recall if he had preflighted the airplane - the right front seat passenger was not present when the pilot boarded the aircraft.
Probable cause:
Occurrence #1: loss of engine power (partial) - nonmechanical
Phase of operation: climb - to cruise
Findings
1. All engines
2. (c) fluid, fuel grade - incorrect
3. (c) refueling - improper - fbo personnel
4. (f) inadequate initial training - fbo personnel
5. (c) preflight planning/preparation - improper - pilot in command
----------
Occurrence #2: forced landing
Phase of operation: descent - emergency
----------
Occurrence #3: on ground/water collision with object
Phase of operation: landing - roll
Findings
6. Terrain condition - berm
Final Report:

Crash of a Partenavia P.68C Victor off New Orleans

Date & Time: Sep 11, 1987 at 0629 LT
Type of aircraft:
Registration:
N1352W
Survivors:
Yes
Schedule:
Hammond - New Orleans
MSN:
232
YOM:
1982
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
15164
Captain / Total hours on type:
30.00
Aircraft flight hours:
913
Circumstances:
The pilot began an ILS runway 18R approach at night to the Lakefront Airport. He reported that after the aircraft broke out of the clouds at 1,700 feet, he transitioned to a visual approach. He stated that as he continued, the approach seemed normal, except the VASI lights seemed too far down the runway. He remembered that just before impact, the VASI was providing a red over red indication, but he did not worry as he perceived the aircraft was over the end of the runway and he was about to flare. At about that time, the aircraft impacted with water, well short of the runway. As the aircraft sank, the pilot escaped thru a hole in the windshield. Subsequently, he was found by passing fishermen. The pilot believed he had gotten a false perception of the runway location due to reflection of lights off of calm lake water.
Probable cause:
Occurrence #1: undershoot
Phase of operation: approach - vfr pattern - final approach
Findings
1. (f) light condition - dark night
2. (f) terrain condition - water, glassy
3. (c) in-flight planning/decision - improper - pilot in command
4. (c) unsafe/hazardous condition warning - disregarded - pilot in command
5. (c) distance - misjudged - pilot in command
6. (f) visual/aural perception - pilot in command
7. (c) altitude - misjudged - pilot in command
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: approach - vfr pattern - final approach
Findings
8. Terrain condition - water
Final Report:

Crash of a Lockheed P2V-5F Neptune in the White Sands Missile Range: 2 killed

Date & Time: Sep 10, 1987 at 1530 LT
Type of aircraft:
Registration:
N96271
Flight Phase:
Flight Type:
Survivors:
No
Site:
MSN:
426-5315
YOM:
1954
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
At approximately 3:00 p.m. on September 10, 1987, the Army called Black Hills Aviation to suppress a fire started by a FAADS missile. The missile was fired more than two hours before the crash. A P2V aircraft, Forest Service Number N96271 ["Tanker 07"], owned by Black Hills, was dispatched in response to the request for aerial fire suppression. Tanker 07 was piloted by Nathan Kolb and co-piloted by Woodard Miller, employees of Black Hills Aviation who were not Department of Defense personnel. Tanker 07 obtained authorization to enter the missile range's airspace from the missile range air controller. During the flight, Tanker 07 crashed on the missile range and both pilots were killed. The crash site was located approximately fifteen miles into the interior of the missile range, and was inside the testing site for the FAADS Project.
Probable cause:
Following the crash, an attorney from the Army Judge Advocate General's [JAG] Office at the missile range ordered markers to be placed at the crash site, and aerial photographs were taken. At that time, the Army JAG Officer anticipated litigation regarding the crash. Personnel at the missile range contacted the National Transportation Safety Board [NTSB] and the Army Safety Center in Fort Rucker, Alabama, and inquired whether either of these entities wished to investigate the crash. The NTSB replied that it was not interested in investigating, but would do so if specifically requested to do so by the missile range. Neither entity actually investigated the crash. Colonel Gary Epperson of the missile range was appointed to conduct an Army Regulation 15-6 Collateral Investigation into the facts and circumstances of the crash. The scope of the AR 15-6 investigation encompassed only the activities of the Army in regard to the crash of Tanker 07, and did not seek to determine the precise cause of the crash. Colonel Epperson's investigation consisted of viewing the crash scene, meeting with eyewitnesses to the crash, and asking for written statements.
Final Report:

Crash of a Cessna 208 Caravan I in Bulverde

Date & Time: Sep 4, 1987 at 2245 LT
Type of aircraft:
Operator:
Registration:
N807LA
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
San Antonio – Dallas
MSN:
208-0026
YOM:
1985
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3100
Captain / Total hours on type:
750.00
Aircraft flight hours:
222
Circumstances:
After leveling at 5,500 feet, the standby power annunciator light illuminated, followed by loss of oil pressure. The pilot turned back toward the airport, but there was a progressive loss of engine power and the prop went to a feathered position. During an emergency landing at night, the aircraft hit a power line and trees, then crashed. During an engine teardown, disassembly of the reduction gearbox scavenge pump revealed that a retaining nut and tang washer (w/i the scavenge pump) had backed off and lodged between the spur gears, which resulted in a sheared scavenge pump drive shaft. In turn, this resulted in the loss of oil pressure and allowed the prop to feather.
Probable cause:
Occurrence #1: airframe/component/system failure/malfunction
Phase of operation: cruise - normal
Findings
1. (c) lubricating system, oil scavenge pump - loose
2. (c) lubricating system, oil scavenge pump - jammed
3. (c) lubricating system, oil scavenge pump - failure, total
4. Initiated
----------
Occurrence #2: loss of engine power (total) - mech failure/malf
Phase of operation: cruise
Findings
5. (c) fluid, oil - starvation
----------
Occurrence #3: forced landing
Phase of operation: descent - emergency
----------
Occurrence #4: in flight collision with object
Phase of operation: landing
Findings
6. (f) light condition - night
7. (f) object - wire, transmission
8. (f) object - tree(s)
----------
Occurrence #5: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report:

Crash of a Cessna 421A Golden Eagle I near Coral Springs: 1 killed

Date & Time: Sep 2, 1987 at 1615 LT
Type of aircraft:
Registration:
N421DT
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Fort Lauderdale – New Port Richey
MSN:
421A-0017
YOM:
1967
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2000
Circumstances:
The aircraft had been abandoned in the Bahamas for approximately 7 months. A pilot, with no known flight time in a Cessna 421, flew it to Fort Lauderdale. Except to avoid clouds, he made the flight at a low altitude and airspeed. When asked why, he said he was trying to save the engines. The pilot then departed toward an area of dark clouds and thunderstorms. When he did not arrive at the destination, a search was initiated. The aircraft was found 4 days later where it crashed in a steep nose down attitude. Radar data showed the aircraft made several heading changes and was returning to the dep airport before it crashed. The forward part of the aircraft was buried in a swamp, but the aft edges of the wings, fuselage and empennage were visible above water. The props had rotational damages; no preimpact mechanical failure or malfunction was evident. An exam of the right eng revealed its #2 pushrods and rocker arms/shafts/retainers had been removed before flight. Also, a #2 spark plug was stowed with its ignition lead attached. The aircraft owner was not found. The pilot's medical certificate was dated 5/28/85.
Probable cause:
Occurrence #1: in flight encounter with weather
Phase of operation: cruise - normal
Findings
1. (f) procedures/directives - not followed - pilot in command
2. (f) operation with known deficiencies in equipment - performed - pilot in command
3. (c) flight into known adverse weather - initiated - pilot in command
4. (f) weather condition - thunderstorm
5. (f) weather condition - clouds
6. (f) weather condition - unfavorable wind
7. Initiated
----------
Occurrence #2: loss of control - in flight
Phase of operation: cruise
Findings
8. (c) airspeed - not maintained - pilot in command
9. (c) stall - inadvertent - pilot in command
10. (f) lack of familiarity with aircraft - pilot in command
11. (f) lack of total experience in type of aircraft - pilot in command
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Findings
12. Terrain condition - water
Final Report:

Crash of a McDonnell Douglas MD-82 in Detroit: 156 killed

Date & Time: Aug 16, 1987 at 2045 LT
Type of aircraft:
Operator:
Registration:
N312RC
Flight Phase:
Survivors:
Yes
Schedule:
Saginaw - Detroit - Phoenix - Santa Ana
MSN:
48090
YOM:
1981
Flight number:
NW255
Crew on board:
6
Crew fatalities:
Pax on board:
149
Pax fatalities:
Other fatalities:
Total fatalities:
156
Captain / Total flying hours:
20859
Captain / Total hours on type:
1359.00
Copilot / Total flying hours:
8044
Copilot / Total hours on type:
1604
Aircraft flight hours:
14928
Circumstances:
A McDonnell Douglas DC-9-82 operating Northwest Airlines flight 255 was destroyed when it crashed onto a road during takeoff from Detroit-Metropolitan Wayne County Airport, Michigan, USA. Just one of the 155 occupants survived the accident. Additionally, Two persons on the ground were killed. Flight NW255 was a regularly scheduled passenger flight between Saginaw, Michigan and Santa Ana, California, with en route stops at Detroit and Phoenix, Arizona. About 18:53, flight 255 departed Saginaw and about 19:42 arrived at its gate at Detroit. About 20:32, flight 255 departed the gate with 149 passengers and 6 crewmembers on board. During the pushback, the flightcrew accomplished the BEFORE (engine) START portion of the airplane checklist, and, at 20:33, they began starting the engines. The flight was then cleared to "taxi via the ramp, hold short of (taxiway) delta and expect runway three center [3C] (for takeoff)..." The ground controller amended the clearance, stating that the flight had to exit the ramp at taxiway Charlie. The crew was requested to change radio frequencies. The first officer repeated the taxi clearance, but he did not repeat the new radio frequency nor did he tune the radio to the new frequency. At 20:37, the captain asked the first officer if they could use runway 3C for takeoff as they had initially expected 21L or 21R. After consulting the Runway Takeoff Weight Chart Manual, the first officer told the captain runway 3C could be used for takeoff. During the taxi out, the captain missed the turnoff at taxiway C. When the first officer contacted ground control, the ground controller redirected them to taxi to runway 3C and again requested that they change radio frequencies. The first officer repeated the new frequency, changed over, and contacted the east ground controller. The east ground controller gave the flight a new taxi route to runway 3C, told them that windshear alerts were in effect, and that the altimeter setting was 29.85 inHg. The flightcrew acknowledged receipt of the information. At 20:42, the local controller cleared flight 255 to taxi into position on runway 3C and to hold. He told the flight there would be a 3-minute delay in order to get the required "in-trail separation behind traffic just departing." At 20:44:04, flight 255 was cleared for takeoff. Engine power began increasing at 20:44:21. The flightcrew could not engage the autothrottle system at first, but, at 20:44:38, they did engage the system, and the first officer called 100 knots at 20:44:45. At 20:44:57, the first officer called "Rotate." Eight seconds later, the stall warning stick shaker activated, accompanied by voice warnings of the supplemental stall recognition system (SSRS). The takeoff warning system indicating that the airplane was not configured properly for takeoff, did not sound at any time prior or during takeoff. After flight 255 became airborne it began rolling to the left and right before the left wing hit a light pole in a rental car lot. After impacting the light pole, flight 255 continued to roll to the left, continued across the car lot, struck a light pole in a second rental car lot, and struck the side wall of the roof of the auto rental facility in the second rental car lot. The airplane continued rolling to the left when it impacted the ground on a road outside the airport boundary. The airplane continued to slide along the road, struck a railroad embankment, and disintegrated as it slid along the ground. Fires erupted in airplane components scattered along the wreckage path. Three occupied vehicles on the road and numerous vacant vehicles in the auto rental parking lot along the airplane's path were destroyed by impact forces and or fire. One passenger, a 4-year-old child was injured seriously.
Probable cause:
The flight crew's failure to use the taxi checklist to ensure that the flaps and slats were extended for take-off. Contributing the accident was the absence of electrical power to the airplane take-off warning system which thus did not warn the flight crew that the airplane was not configured properly for take-off. The reason for the absence of electrical power could not be determined.
Final Report:

Crash of a Cessna 421C Golden Eagle III in Clifton

Date & Time: Aug 16, 1987 at 1514 LT
Registration:
N26596
Flight Type:
Survivors:
Yes
Schedule:
Clifton – Deer Valley
MSN:
421C-1208
YOM:
1982
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4002
Captain / Total hours on type:
2436.00
Aircraft flight hours:
1611
Circumstances:
The flight departed runway 25 at Greenlee County Airport, Clifton, AZ on a VFR flight to Deer Valley Airport, Phoenix, AZ. The pilot and ground witnesses reported that shortly after lift-off, grayish/white smoke emanated from the left engine. The pilot was unable to feather the propeller, circled the airport about 2 times at a low altitude and landed between the runways. The post crash investigation disclosed the fire originated in the vicinity of the left engine turbocharger. The turbocharger oil line housing was found fractured. The housing was missing when the engines were shipped to Teledyne Continental Motors (TCM). The engine crates were opened before safety board investigators arrived at TCM to conduct the engine examination. The left engine exam disclosed external high temp distress and minor detonation signatures.
Probable cause:
Occurrence #1: fire
Phase of operation: takeoff - initial climb
Findings
1. Fluid, oil - fire
2. (c) lubricating system, oil line - fractured
3. (f) fluid, oil - leak
----------
Occurrence #2: forced landing
Phase of operation: descent - emergency
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: maneuvering - turn to landing area (emergency)
Findings
4. (f) emergency procedure - inadequate - pilot in command
5. (f) propeller feathering - not performed - pilot in command
Final Report: