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Crash of a Cessna 560 Citation V near Staunton: 4 killed

Date & Time: Jun 4, 2023 at 1525 LT
Type of aircraft:
Operator:
Registration:
N611VG
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Elizabethton - Ronkonkoma
MSN:
560-0091
YOM:
1990
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
The airplane departed Elizabethton Airport in Tennessee on a private flight to Ronkonkoma-Long Island-McArthur Field (Islip), New York. Approaching the destination, the airplane did not initiate a descent but an almost 180 turn and continued to the southwest. As there was no radio contact with the pilot anymore and as it was approaching the Washington DC area, ATC informed the authorities about the situation and two F-16 fighters were dispatched. The military pilots were unable to establish any contact with the crew. Flying at an altitude of 34,000 feet, the Cessna entered a right turn then an uncontrolled descent and spiraled to the ground before crashing in a wooded and hilly terrain located near Staunton, Virginia, some 600 km southwest from the destination airport. All four occupants were killed.
Probable cause:
Failure of the cabin pressurization system suspected.

Crash of a Beechcraft C90 King Air in Islip

Date & Time: May 18, 2001 at 1725 LT
Type of aircraft:
Operator:
Registration:
N270TC
Flight Type:
Survivors:
Yes
Schedule:
East Hampton - Ronkonkoma
MSN:
LJ-858
YOM:
1979
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2439
Captain / Total hours on type:
98.00
Copilot / Total flying hours:
1613
Copilot / Total hours on type:
114
Aircraft flight hours:
6581
Circumstances:
After about a 20 minute flight, while on final approach for landing, the airplane experienced a loss of engine power on both engines, and the pilot-in-command (PIC) performed a forced landing into trees about 1/2 mile from the airport. The left and right boost pumps and the left and right transfer pumps, were observed in the "OFF" position. According to the PIC, after he exited the airplane, he returned to the cockpit and "shut off the fuel panel. The fuel quantity indicator toggle switch was observed in the "TOTAL" position. Examination of the fuel system revealed both engine nacelle tanks, both wing center section tanks, and the right wing fuel tanks were not compromised. About 1 quart of fuel was drained from the left and right engine nacelle tanks, respectively. Less than a quart of fuel was drained from the right wing tanks. The left wing tanks were compromised during the accident; however there was and no evidence of a fuel spill. Examination of the left and right wing center tanks revealed approximately 27 gallons (approximately 181 lbs) of fuel present in each tank. Battery power was connected to the airplane, and when the fuel transfer pump switches were turned to the "ON" position, fuel was observed being pumped from the left and right wing center tanks to their respective nacelle tanks. The accident flight was the third flight of the day for the flight crew and airplane. According to a flight log located in the cockpit, the flight crew indicated 750 lbs of fuel remained at the time of the takeoff. According to the airplane flight manual (AFM),"Fuel for each engine is supplied from a nacelle tank and four interconnected wing tanks...The outboard wing tanks supply the center section wing tank by gravity flow. The nacelle tank draws its fuel supply from the center section tank. Since the center section tank is lower than the other wing tanks and the nacelle tank, the fuel is transferred to the nacelle tank by the fuel transfer pump in the low spot of the center section tank...." Additionally, with the transfer pumps inoperative, all wing fuel except 28 gallons from each wing will transfer to the nacelle tank through gravity feed.
Probable cause:
The pilot’s failure to activate the fuel transfer pumps in accordance with the checklist, which resulted in fuel exhaustion.
Final Report:

Crash of a Cessna 425 Conquest in Ronkonkoma: 3 killed

Date & Time: Dec 16, 1996 at 1840 LT
Type of aircraft:
Registration:
N425EW
Survivors:
No
Schedule:
Macon – Ronkonkoma
MSN:
425-0150
YOM:
1983
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
10846
Captain / Total hours on type:
2089.00
Circumstances:
The pilot had received clearance for the ILS Runway 6 approach and was advised that the previous landing traffic reported '...breaking out at minimums.' Radar data revealed that the airplane descended in instrument meteorological conditions to the decision height altitude of 294 feet, approximately 3 miles from the missed approach point. The pilot did not perform the missed approach procedure. The airplane leveled off and continued at or below decision height altitude for approximately 28 seconds, traveling a distance of approximately 1 mile. Four low altitude alerts appeared on the tower controller's display. The controller stated he withheld the alert because '...it was a critical phase of flight and the aircraft appeared to be climbing...' The airplane collided with trees and terrain approximately 1.5 miles from the approach end of the landing runway.
Probable cause:
The pilot's early descent to decision height and his failure to perform the missed approach procedure. A factor was the failure of air traffic control to issue a safety advisory.
Final Report:

Crash of a Lockheed PV-1 Ventura near Smithtown: 3 killed

Date & Time: Jan 26, 1956 at 1633 LT
Type of aircraft:
Registration:
N2000C
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Ronkonkoma - Ronkonkoma
MSN:
5243
YOM:
1943
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
800
Captain / Total hours on type:
600.00
Aircraft flight hours:
2216
Circumstances:
N2000C took off at 1625 on January 26, 1956, from MacArthur Field, Ronkonkoma, Long Island, New York, its home base, on a local flight with three pilots. They were Bernard J. Malloy, check pilot, and Pilots Raymond Hamberg and Hugo D. Filangeri. The purpose of the flight was to qualify Pilot Hamberg on the Lockheed PV-1 aircraft, a type he had never piloted. The takeoff of N 2000C was normal, toward the northwest, and made under VFR (Visual Flight Rules) conditions with Pilot Hamberg occupying the left or captain's to scat and Pilot Malloy, as check pilot, seated on the right as copilot; Pilot Filangeri acted as observer. Subsequently the PV-1 was seen over the Smithtown area, flying westerly at an estimated altitude of 2,500-3,000 feet, where a witness reported that the engines sounded normal but that the aircraft appeared to be flying at a slow airspeed. Witnesses stated that shortly thereafter the engine power sounded as though it was cut momentarily and then came back on. At an altitude of approximately 2,000 feet the aircraft was seen to dip down and pull up, slightly nose-high, and then fall off to the left, making two to three turns of a descending spiral, and disappear behind the tree-topped horizon. Flames erupted frost the woods over the point where the aircraft was last seen, followed quickly by a large column of black smoke. All three pilots were killed.
Probable cause:
The Board determines that the probable cause of this accident loss of control resulting in a stall at an altitude too low to effect recovery. The following findings were reported:
- Weather was not a major factor,
- The altitude probably did not exceed 3,500 feet above the ground during the eight minutes the aircraft wan in the air,
- There wan no fire prior to impact,
- There was no evidence of failure of the airframe or malfunction of controls as far as could be drained,
- There was no evidence of power failure of either engine,
- The purpose of the flight was pilot familiarization and included slow flight,
- The aircraft was observed to stall at low airspeed approximately 2,000-2,500 feet above the ground.
Final Report:

Crash of a Douglas DC-6 in Ronkonkoma: 3 killed

Date & Time: Apr 4, 1955 at 1555 LT
Type of aircraft:
Operator:
Registration:
N37512
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
New York-Idlewild – Ronkonkoma – LaGuardia
MSN:
43001
YOM:
1947
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
9763
Captain / Total hours on type:
549.00
Copilot / Total flying hours:
9018
Copilot / Total hours on type:
1156
Aircraft flight hours:
22068
Circumstances:
N37512, under the command of Captain S. C. Hoyt, UAL New York area flight manager, departed New York International Airport at 1428 on a Visual Flight Rules flight plan for an estimated two-hour flight in the vicinity of MacArthur Field, Islip. The aircraft was properly dispatched on a routine check flight, and Captains V. H. Webb and H. M. Dozier were aboard for the purpose of receiving their periodic instrument proficiency check. Upon completion of the checks, the flight was scheduled to return to LaGuardia Airport. At 1501 the flight reported to the company by radio that they were “doing air work around Hempstead.” Another message was received by the company at 1527 reporting that the flight was going to make an ILS (Instrument Landing System) approach at Islip (MacArthur Field). Shortly thereafter, the flight contacted the MacArthur tower, requesting approval for an ILS approach and landing. Permission was granted by the tower, and a normal landing was made on runway 32. The aircraft was taxied to the intersection of runways 28 and 32 and the crew prepared for takeoff. The 1532 MacArthur weather observation showed scattered clouds at 20,000 feet, broken clouds at 25,000; visibility over 15 miles; temperature 53; dew-point 30; wind NNW at 20 knots, gusts to 30 knots. When the flight departed New York International Airport, weather was approximately the same and the forecast for the New York area indicated that it would be similar over the area for the duration of the flight. At 1548, the MacArthur controller cleared the flight to take position on runway 32 and take off. The aircraft took position on the runway but did not immediately take off, hence a second takeoff clearance was transmitted at 1550. The gross weight of the aircraft at takeoff from MacArthur Field was approximately 61,050 pounds, which was well below the maximum allowable. The load was correctly distributed with respect to center of gravity limits. The aircraft became airborne approximately, 1,500 to 1,800 feet down the runway. The takeoff appeared normal, as did the initial portion of the climb, and the aircraft remained on the runway heading. When about 50 feet high, the right wing lowered and the aircraft started turning to the right, at which time the landing gear was retracting. The aircraft continued a climbing turn and the degree of bank increased to approximately vertical by the time the heading changed about 90 degrees and the aircraft had attained an estimated altitude of 150 feet. The nose dropped sharply and the aircraft dived into the ground, striking on the right wing and nose. It then cartwheeled and came to rest right side up. An intense fire started and consumed a large portion of the wreckage in spite of the prompt arrival of fire fighting equipment on the field.
Probable cause:
The Board determines that the probable cause of this accident was unintentional movement of No. 4 throttle into the reverse range just before breaking ground, with the other three engines operating at high power output, which resulted in the aircraft very quickly becoming uncontrollable once airborne. The following findings were reported:
- No evidence of failure or malfunctioning of the structure powerplants, propellers, or electrical system was found,
- In reducing power to zero thrust during an instrument takeoff with a simulated engine out, No. 4 propeller was unintentionally reversed before the aircraft became airborne,
- Evidence indicated that No. 4 throttle was moved out of reverse by the pilot into the forward position in an attempt to unreverse, but the reverse warning flag was not lifted, resulting in increased reverse thrust,
- An outboard propeller on a DC-6 reversing as the aircraft becomes airborne, in conjunction with high power output of the other three engines, at takeoff configuration and airspeed causes the aircraft to become almost immediately uncontrollable,
- There was insufficient time and altitude for any pilot corrective measures to become effective.
Final Report: